DOT National Transportation Integrated Search
1972-08-01
One objective of this study was to determine what correlation existed between the modulus of subgrade reaction as determined by the Plate Bearing Test and the deflection determined by the first snsor of the Lane Wells "Dynaflect". The Research and De...
Evaluation of Chem-Crete : final report.
DOT National Transportation Integrated Search
1982-01-01
Two test sections, one on new construction and the other on a maintenance resurfacing project, were installed in the fall of 1980 to evaluate the proprietary product Chem-Crete. Laboratory tests and dynaflect and density measurements were performed o...
Evaluation of temperature effects on bituminous pavement deflections in Virginia.
DOT National Transportation Integrated Search
1976-01-01
Eight satellite projects with asphaltic layer thicknesses varying from 3.5 inches (88 mm) to 13.5 inches (338 mm) were tested for dynaflect deflections during the four seasons of 1974-75. The projects were located throughout Virginia. The evaluation ...
DOT National Transportation Integrated Search
2007-08-01
Field and laboratory testing programs were conducted to develop models that predict the resilient modulus of subgrade soils from : the test results of DCP, CIMCPT, FWD, Dynaflect, and soil properties. The field testing program included DCP, CIMCPT, F...
Recycling of water-susceptible pavements
NASA Astrophysics Data System (ADS)
Maupin, G. W.
1980-05-01
Several bituminous concrete interstate pavements that experienced failures suspected to have been caused by stripping were investigated. On two projects, the degree of deterioration, potential serviceability, and possible remedial measures were studied. Cores were taken to determine the degreee of stripping and tensile strength, and dynaflect tests were performed. An emulsion mix design was developed for stripped bituminous concrete removed from another project with the expectation that it could be used as a surface mix on a highway with a low traffic volume. While this expectation was not realized, it was concluded that the material is suitable for use in a base mix. A maintenance resurfacing on a fourth project that experienced stripping failure is being monitored and the performance is being evaluated.