Science.gov

Sample records for fourth quarterly technical

  1. PFBC HGCU Test Facility. Fourth quarterly technical progress report, CY 1992

    SciTech Connect

    Not Available

    1993-01-01

    This is the thirteenth Technical Progress Report submitted to the Department of Energy (DOE) in connection with the cooperative agreement between the DOE and Ohio Power Company for the Tidd PFBC Hot Gas Clean Up Test Facility. This report covers the period of work completed during the Fourth Quarter of CY 1992. The following are highlights of the activities that occurred during this report period: Initial operation of the Advanced Particle Filter (APF) occurred during this quarter. The following table summarizes the operating dates and times. HGCU ash lockhopper valve plugged with ash. Primary cyclone ash pluggage. Problems with the coal water paste. Unit restarted warm 13 hours later. HGCU expansion joint No. 7 leak in internal ply of bellows. Problems encountered during these initial tests included hot spots on the APP, backup cyclone and instrumentation spools, two breakdowns of the backpulse air compressor, pluggage of the APF hopper and ash removal system, failure (breakage) of 21 filter candles, leakage of the inner ply of one (1) expansion joint bellows, and numerous other smaller problems. These operating problems are discussed in detail in a subsequent section of this report. Following shutdown and equipment inspection in December, design modifications were initiated to correct the problems noted above. The system is scheduled to resume operation in March, 1993.

  2. PFBC HGCU Test facility. Technical progress report, Fourth quarter, CY 1994

    SciTech Connect

    1995-01-01

    During this quarter, the Tidd Hot Gas Clean Up System completed a 691-hour test run which began during the third quarter. Table 1 summarizes all test runs since initial operation. Following this test run the system was shut down and the filter opened for inspection and recandling. The system remained out of service during the remainder of the quarter. In addition to monitoring and evaluating the performance of the HGCU system during testing, engineering effort was devoted to posttest inspection of the APF (Advanced Particle Filter) and evaluation of the effects of totally spoiling the primary cyclone. In addition, the authors worked with Westinghouse in the selection of replacement candles that were installed during the fourth quarter. During the unit outage this quarter, the primary cyclone upstream of the APF was modified to force all of the ash to pass through the cyclone and enter the APF without using spoiling air. Appendices to this report describe the dust shroud support strap design; an analysis of the effect of support-transferred vibrations on the failure of ceramic candle filters; the Tidd APF operation; the Tidd APF boroscope inspection; a general inspection of Tidd filter internals; tally of Tidd filters; ash formations in the W-APF-October 1994 post-test inspection; characterization of the as-manufactured and PFBC-exposed 3M CVI-SiC composite filter matrix; strength characterization of the first and second generation candle filters after 1,705 hours of PFBC operation at Tidd; and filters used in the December 1994 recandling effort at Tidd.

  3. PFBC HGCU Test Facility. Fourth quarterly technical progress report, [October--December 1993

    SciTech Connect

    Not Available

    1994-01-01

    The APF was shut down on September 23, 1993 and no operation was performed during this quarter. This report summarizes inspection, candle reinstallation, retrofit and accelerometer testing conducted during this three month outage.

  4. Orcas Power and Light Company [fourth quarterly] technical progress report, July--September 1992

    SciTech Connect

    Not Available

    1992-12-31

    After a year of operating the G-Van, OPALCO concluded that the company transportation needs were not being met by the G-Van. The previous quarterly report mentioned battery problems with the Solectria (No. 51). This problem is one of reduced range and power and has been determined to be caused by one or more individual monoblock failures. The local Solectria representative and Solectria headquarters personnel have been aware of this unsatisfactory condition and are continuing their attempt to solve it. The Solectria and G-Van continue to be used intermittently by company personnel for errands and engineering trips. Generally, the smaller, compact size of the Solectria make it the most preferred by company drivers. Clearly the G-Van is not selected for use because of its size and weight. It is important to note that the driver dissatisfaction is not related to the fact that it is an electric van, but more its lack of maneuverability.

  5. Orcas Power and Light Company [fourth quarterly] technical progress report, July--September 1992

    SciTech Connect

    Not Available

    1992-01-01

    After a year of operating the G-Van, OPALCO concluded that the company transportation needs were not being met by the G-Van. The previous quarterly report mentioned battery problems with the Solectria (No. 51). This problem is one of reduced range and power and has been determined to be caused by one or more individual monoblock failures. The local Solectria representative and Solectria headquarters personnel have been aware of this unsatisfactory condition and are continuing their attempt to solve it. The Solectria and G-Van continue to be used intermittently by company personnel for errands and engineering trips. Generally, the smaller, compact size of the Solectria make it the most preferred by company drivers. Clearly the G-Van is not selected for use because of its size and weight. It is important to note that the driver dissatisfaction is not related to the fact that it is an electric van, but more its lack of maneuverability.

  6. Studies of clusters. Fourth quarterly technical progress report, April 1, 1993--June 30, 1993

    SciTech Connect

    Farley, J.W.

    1993-08-01

    Positive cluster ions were produced, and the mass spectrum was measured using a radiofrequency quadrupole mass spectrometer. Mass spectra are attached, showing the cluster ions produced using pure ammonia. They have the general formula (NH {sub 3}){sub n}H {sub m}{sup +}, where n and m are integers. Peaks with different numbers of hydrogens can barely be resolved. This shows that the ion source can produce cluster ions. The development of sensitive laser techniques is necessary for probing the clusters. During this quarter, we succeeded in using a weak diode laser was used to probe a bean of negative molecular ion. The work on the visible absorption spectrum of D{sub 2}O{sup +} continues, and is now in the analysis phase. The work on the infrared vibrational -- rotational spectrum of H{sup 15}NO{sup {minus}} continues. In the second ion beam machine, a complete reworking of the voltages has been completed, and is being reassembled.

  7. Molecular biological enhancement of coal biodesulfurization. Fourth quarterly technical progress report

    SciTech Connect

    Litchfield, J.H.; Fry, I.; Wyza, R.E.; Palmer, D.T.; Zupancic, T.J.; Conkle, H.N.

    1990-06-14

    The objective of this project is to produce one or more microorganisms capable of removing the organic and inorganic sulfur in coal. The original specific technical objectives of the project were to: clone and characterize the genes encoding the enzymes of the ``4S`` pathway (sulfoxide/sulfone/sulfonate/sulfate) for release of organic sulfur from coal; return multiple copies of genes to the original host to enhance the biodesulfurization activity of that organism; transfer this pathway into a fast-growing chemolithotropic bacterium; conduct a batch-mode optimization/analysis of scale-up variables.

  8. Tidd PFBC Demonstration Project fourth quarterly technical progress report, CY 1992

    SciTech Connect

    Not Available

    1993-01-01

    This is the 23rd technical progress report submitted to the Department of Energy in connection with the cooperative agreement between the DOE and the Ohio Power Company for the Tidd PFBC Demonstration Plant. This report covers the period from October 1, 1992 to December 31, 1992. Major activities during this period involve: (1) The unit was operated for a total of 714 hours (including gas turbine air prewarming). There were seven gas turbine starts, seven bed preheater starts, and seven operating periods with coal fire. The peak gross output of 64 MWH was achieved for the period of 1000 to 1100 hours on November 23, 1992. The longest coal fire was 285 hours beginning at 1211 hours on November 25, 1992. (2) Total gross generation was 24,643, and coal consumption was 11,900 tons. (3) The hot gas clean up system was commissioned. (4) Active end fluidization system to address sparge duct cracking and deformation problem was jointly initiated by ABB carbon, B&W and AEPSC. (5) All testing continued using Plum Run dolomite. This approach was taken as a conservative means to avoid sintering and unit trips which were encountered during the previous two start-ups in September using limestone and (6) monitoring of solid, liquid and gaseous waste streams, as detailed in the operations phase monitoring requirements in the EMP, were performed.

  9. Tidd PFBC Demonstration Project fourth quarterly technical progress report, CY 1992

    SciTech Connect

    Not Available

    1993-01-01

    This is the 23rd technical progress report submitted to the Department of Energy in connection with the cooperative agreement between the DOE and the Ohio Power Company for the Tidd PFBC Demonstration Plant. This report covers the period from October 1, 1992 to December 31, 1992. Major activities during this period involve: (1) The unit was operated for a total of 714 hours (including gas turbine air prewarming). There were seven gas turbine starts, seven bed preheater starts, and seven operating periods with coal fire. The peak gross output of 64 MWH was achieved for the period of 1000 to 1100 hours on November 23, 1992. The longest coal fire was 285 hours beginning at 1211 hours on November 25, 1992. (2) Total gross generation was 24,643, and coal consumption was 11,900 tons. (3) The hot gas clean up system was commissioned. (4) Active end fluidization system to address sparge duct cracking and deformation problem was jointly initiated by ABB carbon, B W and AEPSC. (5) All testing continued using Plum Run dolomite. This approach was taken as a conservative means to avoid sintering and unit trips which were encountered during the previous two start-ups in September using limestone and (6) monitoring of solid, liquid and gaseous waste streams, as detailed in the operations phase monitoring requirements in the EMP, were performed.

  10. Great Plains Coal Gasification Project, Mercer County, North Dakota. Quarterly technical and environmental report, fourth quarter, 1983. [Great Plains, Mercer County, North Dakota

    SciTech Connect

    Not Available

    1983-01-01

    Activities remain on schedule to meet Great Plains Gasification Associates' full gas production date. Gasification Plant: detailed engineering in the Contractors' home office was completed in the fourth quarter. The remaining engineering tasks, which include field support activities and special projects, will be performed by the Contractors' Field Engineering Group. A substantial amount of construction progress was achieved during the fourth quarter. Although the Plant's construction activities are still slightly behind schedule, it is currently forecasted that the construction schedule will be regained by the end of June 1984. Start-Up operations are continuing at a rapid pace. The current emphasis is on system turnover and commissioning activities. The environmental permitting for the construction phase is complete. Freedom Mine: mine development activities remain on schedule.

  11. United States housing, fourth quarter 2013

    Treesearch

    Delton Alderman

    2017-01-01

    In the beginning of 2013, the U.S. housing construction market indicated increases in all sectors; yet, by the fourth quarter’s end, only housing under construction improved. Moderation and declines are to be expected in the fourth quarter, as winter is setting in. Permits, starts, housing under construction, completions, and new and existing house sales all exceeded...

  12. Surfactant studies for bench-scale operation. Fourth quarterly technical progress report, April 1, 1993--June 30, 1993

    SciTech Connect

    Hickey, G.S.; Sharma, P.K.

    1993-07-23

    A phase 2 study has been initiated to investigate surfactant- assisted coal liquefaction, with the objective of quantifying the enhancement in liquid yields and product quality. This report covers the fourth quarter of work. The major accomplishments were (1) Completion of coal liquefaction autoclave reactor runs and related analysis with Illinois {number_sign}6 coal with time as a variable at 375{degree}C, and pressures of 1800 psig; (2) an investigation into the mechanism of the effect that the lignosulfonate surfactant has in enhancing liquefaction yields; and (3) completion of a bench-scale test with the surfactant in the continuous flow Catalytic Two Stage Liquefaction Process (CTSL) reactor at HRI.

  13. An advanced control system for fine coal flotation. Fourth quarterly technical progress report, July 1, 1996--September 30, 1996

    SciTech Connect

    Adel, G.T.; Luttrell, G.H.

    1997-03-04

    A model-based flotation control scheme is being implemented to achieve optimal performance in the handling and treatment of fine coal. The control scheme monitors flotation performance through on-line analysis of ash content. Then, based on the economic and metallurgical performance of the circuit, variables such as reagent dosage, pulp density and pulp level are adjusted using model-based control algorithms to compensate for feed variations and other process disturbances. Recent developments in sensor technology are being applied for on-line determination of slurry ash content. During the fourth quarter of this project, a final attempt was made to calibrate a video-based ash analyzer for use in this application. It was concluded that the low ash content and the coarse particle size of the flotation tailings slurry at the Maple Meadow plant site made the video-based system unsuitable for this application. Plans are now underway to lease a nuclear-based analyzer as the primary sensor for this project.

  14. A novel carbon-based process for flue gas cleanup. Fourth quarterly technical progress report, April 1--June 30, 1992

    SciTech Connect

    Gangwal, S.K.; Silveston, P.L.

    1992-07-01

    The objective of this project is to demonstrate the preliminary technical and economic feasibility of a novel carbon-based process for removal of at least 95% SO{sub 2} and at least 75% NO{sub x} from coal combustion flue gas. In the process, flue gas leaving the electrostatic precipitator (ESP) is passed through a trickle bed of activated carbon catalyst employing a periodic flush of low strength sulfuric acid. The SO{sub 2} is oxidized to SO{sub 3} and removed as medium strength sulfuric acid. The SO{sub 2}-free flue gas is then mixed with NH{sub 3}, and the NO{sub x} in the gas is subjected to selective catalytic reduction (SCR) to N{sub 2} over a fixed bed of activated carbon catalyst. In the previous three quarters, a detailed project management plan was prepared describing the experimental setup, work plan, and test plan. The experimental system was completed for SO{sub 2} conversion at Waterloo and for NO{sub x} conversion at RTI. Shakedown experiments were completed. In the present quarter, the NO{sub x} removal performance of two additional modified carbon catalysts (MCCII and MCCIII) was studied. MCCII showed NO{sub x} removal efficiency which was similar to that observed for MCCI. However, MCCI was considerably less active for NO{sub x} removal. SO{sub 2} removal experiments with NO present in the feed gas were performed with MCCI. SO{sub 2} removal efficiency was consistently about 98% over each of 10 cycles and was very similar to that observed earlier with no NO present in the feed. Finally, a preliminary economic evaluation of the process was performed and a project review meeting was held. The economic evaluation showed that the Rn-Waterloo process was competitive with SCR/IFGD and other combined SO{sub 2}/NO{sub x}, removal processes.

  15. Development of the selective hydrophobic coagulation process. Fourth quarterly technical progress report, July 1, 1992--September 30, 1992

    SciTech Connect

    Yoon, R.H.; Luttrell, G.H.

    1992-12-31

    A novel technique for selectively coagulating and separating coal from dispersed mineral matter has been developed at Virginia Tech. The process, Selective Hydrophobic Coagulation (SHC), has been studied since 1986 under the sponsorship of the US Department of Energy. The SHC process differs from oil agglomeration, shear or polymer flocculation, and electrolytic coagulation processes in that it does not require reagents or additives to induce the formation of coagula. In most cases, simple pH control is all that is required to (i) induce the coagulation of coal particles and (ii) effectively disperse particles of mineral matter. If the coal is oxidized, a small dosage of reagents can be used to enhance the process. The technical work program was initiated on July 1, 1992. Force-distance curves were generated for DDOA Br-coated mica surfaces in water and used to calculate hydrophobicity constants and decay lengths for this system; and a new device for the measurement of water contact angles, similar to the Wilhelmy plate balance, has been built 225 kg samples of Pittsburgh No. 8 and Elkhom No. 3 seam coals were obtained; a static mixer test facility for the study of coagula growth was set up and was undergoing shakedown tests at the end of the quarter; a bench-scale lamella thickener was being constructed; and preliminary coagula/ mineral separation tests were being conducted in a bench-scale continuous drum filter.

  16. (Shippingport Atomic Power Station). Quarterly operating report, fourth quarter 1980

    SciTech Connect

    Not Available

    1980-01-01

    At the beginning of the fourth quarter of 1980, the Shippingport Atomic Power Station remained shutdown for the normally planned semiannual maintenance and testing program, initiated September 12, 1980. Operational testing began on November 7. Maximum power was achieved November 28 and was maintained throughout the remainder of the quarter except as noted. The LWBR Core has generated 19,046.07 EFPH from start-up through the end of the quarter. During this quarter, approximately 0.000025 curies of Xe 133 activity were released from the station. During the fourth quarter of 1980, 1081 cubic feet of radioactive solid waste was shipped out of state for burial. These shipments contained 0.037 curies of radioactivity.

  17. Short-term energy outlook: Quarterly projections, fourth quarter 1997

    SciTech Connect

    1997-10-14

    The Energy Information Administration (EIA) prepares quarterly short-term energy supply, demand, and price projections for printed publication in January, April, July, and October in the Short-Term Energy Outlook. The details of these projections, as well as monthly updates on or about the 6th of each interim month, are available on the internet at: www.eia.doe.gov/emeu/steo/pub/contents.html. The forecast period for this issue of the Outlook extends from the fourth quarter of 1997 through the fourth quarter of 1998. Values for the fourth quarter of 1997, however, are preliminary EIA estimates (for example, some monthly values for petroleum supply and disposition are derived in part from weekly data reported in EIA`s Weekly Petroleum Status Report) or are calculated from model simulations that use the latest exogenous information available (for example, electricity sales and generation are simulated by using actual weather data). The historical energy data, compiled in the fourth quarter 1997 version of the Short-Term Integrated Forecasting System (STIFS) database, are mostly EIA data regularly published in the Monthly Energy Review, Petroleum Supply Monthly, and other EIA publications. Minor discrepancies between the data in these publications and the historical data in this Outlook are due to independent rounding. The STIFS model is driven principally by three sets of assumptions or inputs: estimates of key macroeconomic variables, world oil price assumptions, and assumptions about the severity of weather. 19 tabs.

  18. Quarterly environmental data summary for fourth quarter 1997

    SciTech Connect

    1997-12-31

    The Quarterly Environmental Data Summary (QEDS) for the fourth quarter of 1997 is prepared in support of the Weldon Spring Site Remedial Action Project Federal Facilities Agreement. The data presented constitute the QEDS. The data were received from the contract laboratories, verified by the Weldon Spring Site verification group and, except for air monitoring data and site KPA generated data (uranium analyses), merged into the data base during the fourth quarter of 1997. Air monitoring data presented are the most recent complete sets of quarterly data. Air data are not stored in the data base and KPA data are not merged into the regular data base. Significant data, defined as data values that have exceeded defined ``above normal`` level 2 values, are discussed in this letter for Environmental Monitoring Plan (EMP) generated data only. Above normal level 2 values are based, in ES and H procedures, on historical high values, DOE Derived Concentration Guides (DCGs), NPDES limits and other guidelines. The procedures also establish actions to be taken in response to such data. Data received and verified during the fourth quarter were within a permissible range of variability except for those which are detailed.

  19. Bench-scale testing of the micronized magnetite process. Fourth quarterly technical progress report, April--June 1995

    SciTech Connect

    1995-08-10

    The main accomplishments of Custom Coals and the project subcontractors, during this period, included: continued purchase of small equipment and supplies for the circuit; completed the circuit commissioning task; procured one lot of PennMag Grade-K and one lot Grade-L magnetite; completed work on analytical investigations; completed Classifying Circuit Component Testing on Pittsburgh No. 8 coal; completed the final Heavy-Media cyclone component testing on the Pittsburgh No. 8 seam using Grade-K and Grade-L magnetites; continued QA/QC tests on wet screening, wet splitting, Marcy Balance, and reproducibility checks on component tests and component test samples; and completed the magnetite recovery circuit component testing with and without screens using the Grade-K magnetite and the Pittsburgh No. 8 coal seam. This report contains a short discussion of the project description, objectives, budget, schedule, and teaming arrangement. It also includes a detailed discussion of the above mentioned project accomplishments and plans, organized by the various task series within the project work plan. The final section contains an outline of the specific project goals for the next quarterly reporting period.

  20. Applied Meteorology Unit (AMU) Quarterly Report Fourth Quarter FY-04

    NASA Technical Reports Server (NTRS)

    Bauman, William; Wheeler, Mark; Lambert, Winifred; Case, Jonathan; Short, David

    2004-01-01

    This report summarizes the Applied Meteorology Unit (A MU) activities for the fourth quarter of Fiscal Year 2004 (July -Sept 2004). Tasks covered are: (1) Objective Lightning Probability Forecast: Phase I, (2) Severe Weather Forecast Decision Aid, (3) Hail Index, (4) Shuttle Ascent Camera Cloud Obstruction Forecast, (5) Advanced Regional Prediction System (ARPS) Optimization and Training Extension and (5) User Control Interface for ARPS Data Analysis System (ADAS) Data Ingest.

  1. Evaluation of using cyclocranes to support drilling and production of oil and gas in wetland areas. Fourth quarterly technical progress report, Second quarter, 1993

    SciTech Connect

    Eggington, W.J.

    1993-09-01

    The planned program falls under wetlands area research related to drilling, production, and transportation of oil and gas resources. Specifically the planned program addresses an evaluation of using cyclocraft to transport drill rigs, mud, pipes and other materials and equipment in a cost effective and environmentally safe manner to support oil and gas drilling and production operations in wetland areas. The cyclocraft is a proven hybrid aircraft that utilizes aerostatic and aerodynamic lift. This type of aircraft has considerable payload capacity, VTOL capability, high controllability, low operating cost, low downwash and high safety. The benefits of using a cyclocraft to transport drill rigs and materials over environmentally-sensitive surfaces would be significant. The cyclocraft has considerable cost and operational advantages over the helicopter. The major activity during the second quarter of 1993 was focussed on completion of Task 4, Preliminary Design. The selected design has been designated H.1 Cyclocraft by MRC. Also during the report period, Task 6, Ground Support, was completed and a report containing the results was submitted to DOE. This task addressed the complete H.1 Cyclocraft system, i.e. it included the need personnel, facilities and equipment to support cyclocraft operations in wetland areas.

  2. CO{sub 2} Huff-n-Puff process in a light oil shallow shelf carbonate reservoir. Quarterly technical progress report, Fourth quarter 1995

    SciTech Connect

    Wehner, S.; Prieditis, J.

    1996-02-05

    The principle objective of the Central Vacuum Unit (CVU) CO{sub 2} Huff-n-Puff (H-n-P) project is to determine the feasibility and practicality of the technology in a waterflooded shallow shelf carbonate environment. The results of parametric simulation of the CO{sub 2} H-n-P process, coupled with the CVU reservoir characterization components will determine if this process is technically and economically feasible for field implementation. The technology transfer objective of the project is to disseminate the knowledge gained through an innovative plan in support of the Department of Energy`s objective of increasing domestic oil production and deferring the abandonment of shallow shelf carbonate (SSC) reservoirs. Texaco Exploration and Production Inc`s. (TEPI) mid-term plans are to implement a full-scale miscible CO{sub 2} project in the CVU. TEPI has concluded all of the Tasks associated with the First Budget Period. The DOE approved the TEPI continuation application. Budget Period No. 2 is now in progress. Initial injection of CO{sub 2} began in November, and after a short shut-in period for the soak, the well was returned to production in late December, 1995.

  3. Applied Meteorology Unit (AMU) Quarterly Report - Fourth Quarter FY-09

    NASA Technical Reports Server (NTRS)

    Bauman, William; Crawford, Winifred; Barrett, Joe; Watson, Leela; Wheeler, Mark

    2009-01-01

    This report summarizes the Applied Meteorology Unit (AMU) activities for the fourth quarter of Fiscal Year 2009 (July - September 2009). Tasks reports include: (1) Peak Wind Tool for User Launch Commit Criteria (LCC), (2) Objective Lightning Probability Tool. Phase III, (3) Peak Wind Tool for General Forecasting. Phase II, (4) Update and Maintain Advanced Regional Prediction System (ARPS) Data Analysis System (ADAS), (5) Verify MesoNAM Performance (6) develop a Graphical User Interface to update selected parameters for the Hybrid Single-Particle Lagrangian Integrated Trajectory (HYSPLlT)

  4. Petroleum profits in the fourth quarter of 1990

    SciTech Connect

    Not Available

    1991-02-12

    The information in this report concerning fourth-quarter income was obtained from companies' public releases, which are issued in advance of their required filings of Form 10Q or Form 10K with the Securities and Exchange Commission. Topics outlined include: overview of fourth quarter profits, crude oil prices and oil and gas earnings, refining margins and refining/marketing income, overall profitability, and quarterly financial data.

  5. Petroleum profits in the fourth quarter of 1990

    SciTech Connect

    Not Available

    1991-02-12

    The information in this report concerning fourth-quarter income was obtained from companies` public releases, which are issued in advance of their required filings of Form 10Q or Form 10K with the Securities and Exchange Commission. Topics outlined include: overview of fourth quarter profits, crude oil prices and oil and gas earnings, refining margins and refining/marketing income, overall profitability, and quarterly financial data.

  6. Weldon Spring Site Remedial Action Project quarterly environmental data summary (QEDS) for fourth quarter 1998

    SciTech Connect

    1999-02-01

    This report contains the Quarterly Environmental Data Summary (QEDS) for the fourth quarter of 1998 in support of the Weldon Spring Site Remedial Action Project Federal Facilities Agreement. The data, except for air monitoring data and site KPA generated data (uranium analyses) were received from the contract laboratories, verified by the Weldon Spring Site verification group, and merged into the database during the fourth quarter of 1998. KPA results for on-site total uranium analyses performed during fourth quarter 1998 are included. Air monitoring data presented are the most recent complete sets of quarterly data.

  7. Solar Energy Technologies Program Newsletter - Fourth Quarter 2009

    SciTech Connect

    DOE Solar Energy Technologies Program

    2009-12-31

    The Fourth Quarter 2009 edition of the Solar Energy Technologies Program newsletter summarizes the activities for the past three months, funding opportunities, highlights from the national labs, and upcoming events.

  8. Quarterly Performance/Technical Report

    DTIC Science & Technology

    2006-06-30

    National Marrow Donor Program® HLA Typing for Bone Marrow Transplantation Task 1: Product Validation Description: The objective of this study is to evaluate... Bone Marrow Transplantation Activity: During the past quarter, Scientific Services staff worked with a panel of cell processing experts to revise the...Technical Report April 1, 2006 - June 30, 2006 National Marrow Donor Program® HLA Typing for Bone Marrow Transplantation Task 2: Validation of the

  9. Development and testing of industrial scale, coal fired combustion system, Phase 3. Fourth quarterly technical progress report, October 1, 1992--December 31, 1992

    SciTech Connect

    Zauderer, B.

    1993-02-15

    A major part of the work in this quarter was on the combustor tests in task 2. Three of the six planned tests in this task were completed. The first two were parametric tests of nominal one shift, (8 hour) duration on coal. Due to failure of the UV detector in the first test only several hours of coal fired operation were completed. In the second test, coal fired operation continued for the planned one shift until the 4 ton coal bin was empty. After reviewing this work with DOE, it was decided to focus the remaining test on longer duration operation with each test at one optimum condition. The third test was planned for two shift coal fired operation. Due to a problem with the pilot gas ignitor, combustion was delayed by 5 hours from 7 AM to Noon. As a result coal fired operation was limited to one shift between 3 PM and 11 PM. Throughout this period the combustor remained at one fixed condition with the use of computer control. Results for these three tests are presented in this report. Most of the work on the task 4 design and cost of a 20 MW combined gas-steam turbine power plant using the air cooled combustor was completed in the previous quarter. The results obtained by the A/E subcontractor on the installation desip and cost were evaluated in the present quarter and they are summarized in this report.

  10. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2005-01-01

    A quarterly listing of RTO technical publications is presented. The topics include: Handbook on the Analysis of Smaller-Scale Contingency Operations in Long Term Defence Planning; 2) Radar Polarimetry and Interferometry; 3) Combat Casualty Care in Ground-Based Tactical Situations: Trauma Technology and Emergency Medical Procedures; and 4) RTO Technical Publications: A Quarterly Listing

  11. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2005-01-01

    A quarterly listing of RTO technical publications is presented. The topics include: Handbook on the Analysis of Smaller-Scale Contingency Operations in Long Term Defence Planning; 2) Radar Polarimetry and Interferometry; 3) Combat Casualty Care in Ground-Based Tactical Situations: Trauma Technology and Emergency Medical Procedures; and 4) RTO Technical Publications: A Quarterly Listing

  12. Applied Meteorology Unit (AMU) Quarterly Report - Fourth Quarter FY-10

    NASA Technical Reports Server (NTRS)

    Bauman, William; Crawford, Winifred; Barrett, Joe; Watson, Leela; Wheeler, Mark

    2010-01-01

    Three AMU tasks were completed in this Quarter, each resulting in a forecast tool now being used in operations and a final report documenting how the work was done. AMU personnel completed the following tasks (1) Phase II of the Peak Wind Tool for General Forecasting task by delivering an improved wind forecasting tool to operations and providing training on its use; (2) a graphical user interface (GUI) she updated with new scripts to complete the ADAS Update and Maintainability task, and delivered the scripts to the Spaceflight Meteorology Group on Johnson Space Center, Texas and National Weather Service in Melbourne, Fla.; and (3) the Verify MesoNAM Performance task after we created and delivered a GUI that forecasters will use to determine the performance of the operational MesoNAM weather model forecast.

  13. Natural gas imports and exports. Fourth quarter report, 1998

    SciTech Connect

    1998-12-31

    The Office of Natural Gas and Petroleum Import and Export Activities prepares quarterly reports summarizing the data provided by companies authorized to import or export natural gas. Companies are required, as a condition of their authorizations, to file quarterly reports. This report is for the fourth quarter of 1998 (October through December). Attachment A shows the percentage of takes to maximum firm contract levels and the weighted average per unit price for each of the long-term importers during the five most recent reporting quarters. Attachment B shows volumes and prices of gas purchased by long-term importers and exporters during the past 12 months. Attachment C shows volume and price information pertaining to gas imported on a short-term or spot market basis. Attachment D shows the gas exported on a short-term or spot market basis to Canada and Mexico.

  14. US Energy Industry Financial Developments, 1993 fourth quarter, April 1994

    SciTech Connect

    Not Available

    1994-04-14

    This report traces key financial trends in the US energy industry for the fourth quarter of 1993. Financial data (only available for publicly-traded US companies) are included in two broad groups -- fossil fuel production and rate-regulated electric utilities. All financial data are taken from public sources such as energy industry corporate reports and press releases, energy trade publications, and The Wall Street Journal`s Earnings Digest; return on equity is calculated from data available from Standard and Poor`s Compustat data service. Since several major petroleum companies disclose their income by lines of business and geographic area, these data are also presented in this report. Although the disaggregated income concept varies by company and is not strictly comparable to corporate income, relative movements in income by lines of business and geographic area are summarized as useful indicators of short-term changes in the underlying profitability of these operations. Based on information provided in 1993 fourth quarter financial disclosures, the net income for 82 petroleum companies -- including 18 majors -- was unchanged between the fourth quarter of 1992 and the fourth quarter of 1993. An 18-percent decline in crude oil prices resulted in a deterioration of the performance of upstream (oil and gas production) petroleum companies during the final quarter of 1993. However, prices for refined products fell much less than the price of crude oil, resulting in higher refined product margins and downstream (refining, marketing and transport) petroleum earnings. An increase in refined product demand also contributed to the rise in downstream income.

  15. Calorimetry exchange program quarterly data report, fourth quarter CY92

    SciTech Connect

    Barnett, T.M.

    1992-12-31

    The goals of the Calorimetry Sample Exchange Program are: (1) discuss measurement differences (2) review and improve analytical measurements and methods (3) discuss new measurement capabilities (4) provide data to DOE on measurement capabilities to evaluate shipper- receiver differences (5) provide characterized or standard materials as necessary for exchange participants (6) provide a measurement control program for plutonium analysis A sample Of PUO2 powder is available at each participating site for NDA measurement, including either or both calorimetry and high-resolution gamma-ray spectroscopy, the elements which are typically combined to provide a calorimetric assay of plutonium. The facilities measure the sample as frequently and to the level of precision which they desire, and then submit the data to the Exchange for analysis. The data report includes summary tables for each measurement and charts showing the performance of each laboratory. Comparisons are made to the accepted values for the exchange sample and to data previously reported by that laboratory. This information is presented, in the form of quarterly reports as this document provides and as annual reports, intended for use by Exchange participants in measurement control programs, or to indicate when bias corrections may be appropriate. No attempt, however, has been made to standardize methods or frequency of data collection, calibration, or operating procedures. Direct comparisons between laboratories may, therefore, be misleading since data have not been collected to the same precision or for the same time periods. A meeting of the participants of the Calorimetry Exchange is held annually at EG&G Mound Applied Technologies. The purposes of this meeting are to discuss measurement differences, problems, and new measurement capabilities, and to determine the additional activities needed to fulfill the goals of the Exchange.

  16. Systems and economic analysis of microalgae ponds for conversion of CO{sub 2} to biomass. Fourth quarterly technical progress report, June 16, 1994--September 15, 1994

    SciTech Connect

    Benemann, J.R.; Oswald, W.J.

    1994-12-28

    The threat of global warming, mounting concerns about air and water pollution, prospective food shortages, and declining reserves of low-cost fossil fuels, have spawned a burgeoning interest in photobiological processes using microalgae as a method of large-scale utilization of CO{sub 2} for the production of fuels, food, and waste treatment. The major activity during this quarter was the development of cost data for the algal production system, including alternatives to the basic design previously used. The results of this work are still being developed and will be reported in the Final Report. This progress report summarizes a study of a production processes for one specific alga, Botryococcus braunii. This alga is of particular interest in this project as it produces an almost pure hydrocarbon fuel, and does so in rather large amounts. Technology for the production of this organism has, however, not yet been developed. This progress report reviews the literature on this interesting alga and suggests potential methods for its production. 62 refs.

  17. Studies of incipient oxidation of pyrite for improved rejection. Technical progress report for the fourth quarter, July 1, 1993--September 30, 1993

    SciTech Connect

    Yoon, R.H.; Richardson, P.E.

    1993-10-01

    One major objective of this work is to determine the Eh-pH conditions under which pyrite is stable and then to determine the mechanism of the initial stages of pyrite oxidation. It is known that moderate oxidation of pyrite produces a hydrophobic surface product. This hydrophobic product makes it extremely difficult to depress pyrite in coal flotation circuits. The eventual objective of this work is to prevent pyrite oxidation in order to better depress pyrite in coal flotation circuits. In this work clean, unoxidized pyrite surfaces are being produced by fracturing pyrite electrodes in an electrochemical cell. It has been shown that by holding the potential at different values during fracture and measuring the current passed at fracture, pyrite oxidation or reduction can be precisely controlled, or prevented. In the previous quarterly report, pyrite oxidation in pH 9.2 buffer solution was discussed. During this report period, the initial stages of pyrite oxidation in pH 4.6 buffer solution were studied, and the results compared with those in pH 9.2 solution. The effect of anodic and cathodic potential limits on the subsequent photocurrent and voltammetry behavior of freshly-fractured pyrite electrodes was also determined.

  18. AGEX II: Technical quarterly, Volume 2

    SciTech Connect

    Ekdahl, C.

    1995-03-01

    The AGEX II Technical Quarterly publishes short technical contributions on above ground experiments that use pulsed power and laser drivers. The Quarterly is intended to provide rapid exposure of timely technical ideas and results as well as a means for documenting AGEX II progress and scientific quality for the AGEX II community. Suitable topics include experimental results, diagnostic apparatus, theoretical design, and scaling, among others.

  19. Development of a video-based slurry sensor for on-line ash analysis. Fourth quarter technical progress report, July 1--September 30, 1995

    SciTech Connect

    Adel, G.T.; Luttrell, G.H.

    1995-10-20

    Automatic control of fine coal cleaning circuits has traditionally been limited by the lack of sensors for on-line ash analysis. Although several nuclear-based analyzers are available, none have seen widespread acceptance. This is largely due to the fact that nuclear sensors are expensive and tend to be influenced by changes in seam type and pyrite content. Recently, researchers at VPI and SU have developed an optical sensor for phosphate analysis. The sensor uses image processing technology to analyze video images of phosphate ore. It is currently being used by Texasgulf for off-line analysis of dry flotation concentrates. The primary advantages of optical sensors over nuclear sensors are that they are significantly cheaper, are not subject to measurement variations due to changes in high atomic number minerals, are inherently safer and require no special radiation permitting. The purpose of this work is to apply the knowledge gained in the development of an optical phosphate analyzer to the development of an on-line ash analyzer for fine coal slurries. During the past quarter, a study was conducted to determine if monochromatic illumination could be used as a means of enhancing the differences observed between coal and mineral matter under reflected light. After extensive testing, monochromatic illumination was found to provide no advantages over white light. In fact, white light appeared to provide slightly better resolution of ash content. Initial testing of the sample presentation system at the plant site indicated that froth formation in the sample tube was indeed a problem as predicted by Pittston representatives. A slight modification in the design of the tube and a modification in the time required to bring the slurry level into the focal plane of the camera were found to eliminate the frothing problem.

  20. Hydrocarbon-oil encapsulated bubble flotation of fine coal. Technical progress report for the fourth quarter, July 1, 1991--September 30, 1991

    SciTech Connect

    Peng, F.F.

    1995-01-01

    This report is concerned with the progress made during the fourth period of the research Project, Grant no. DE-FG22-90-PC90314. A main portion of this reporting period has been consumed in the following tasks: (i) induction time measurement for the coal particles prepared by using various modes of collector addition techniques; (ii) ultrasonic energy dispersed collector flotation tests; (iii) natural floatability measurement using Hallimond tube flotation cell; (iv) preparation and operation of 3-inch column cell, and (v) preparation of wettability measurement using film flotation method. The coal samples used in this period of work are four ranks of coal samples from Mammoth (Anthracite), Lower Kittanning, Upper Freeport and Pittsburgh No. 8 seam coals. The results showed that a drastic improvement in the flotation rate and yield were achieved by using the ultrasonic energy dispersed collector flotation compared to that of conventional flotation. The techniques of direct liquid addition and addition of ultrasonic energy dispersed collector are mainly for alteration of the hydrophobicity distribution of coal particle surfaces. On the contrary, the gasified collector addition to the gas phase technique is for alteration of the chemical properties of bubble surfaces. Among these techniques, however, the results showed that the hydrocarbon oil encapsulated bubble flotation is more selective than either ultrasonic energy dispersed collector flotation process or conventional flotation process. Induction time measurement was continued and extended to the coal samples received in this period of work, using oil free air bubble and oil-coated air bubbles. Induction time for oil-coated bubbles is significantly shorter than that of oil-free bubbles for all the coal samples used. A good agreement between flotation responses and induction time were obtained for all the coal samples under the conditions of various modes of collector dispersion.

  1. The Savannah River Site's Groundwater Monitoring Program: Fourth quarter 1991

    SciTech Connect

    Rogers, C.D. )

    1992-06-02

    The Environmental Protection Department/Environmental Monitoring Section (EPD/EMS) administers the Savannah River Site's (SRS) Groundwater Monitoring Program. During fourth quarter 1991, EPD/EMS conducted extensive sampling of monitoring wells. EPD/EMS established two sets of criteria in 1986 to assist in the management of sample results. The flagging criteria do not define contamination levels; instead, they aid personnel in sample scheduling, interpretation of data, and trend identification. Beginning in 1991, the flagging criteria are based on EPA drinking water standards and method detection limits. A detailed explanation of the current flagging criteria is presented in the Flagging Criteria section of this document. Analytical results from fourth quarter 1991 are listed in this report.

  2. Final Screening Program, Third and Fourth Quarters. Version 3.1. Task 4. Volume 1.

    DTIC Science & Technology

    1988-05-01

    network, but historical occurrences are present within ISP distribution patterns for both the alluvial and Denver aquifers . Third and Fourth Quarter...FY86) APPENDIX C--THIRD AND FOURTH QUARTERS (FY86) ALLUVIAL AND DENVER AQUIFER COMPOUND DISTRIBUTIOýN PLOTS C-RMA-04D/FIN•PT. TOC.Iii 05/20/88 TABLE...Level Measurement Well Network, Third and Fourth Quarter, Fiscal Year 1986 2 Water Level Elevation Alluvial Aquifer , Third Quarter, Fiscal Year 1986

  3. Results for the Fourth Quarter Calendar Year 2015 Tank 50H Salt Solution Sample

    SciTech Connect

    Crawford, C.

    2016-01-11

    In this memorandum, the chemical and radionuclide contaminant results from the Fourth Quarter Calendar Year 2015 (CY15) sample of Tank 50H salt solution are presented in tabulated form. The Fourth Quarter CY15 Tank 50H samples were obtained on October 29, 2015 and received at Savannah River National Laboratory (SRNL) on October 30, 2015. The information from this characterization will be used by Defense Waste Processing Facility (DWPF) & Saltstone Facility Engineering for the transfer of aqueous waste from Tank 50H to the Salt Feed Tank in the Saltstone Production Facility, where the waste will be treated and disposed of in the Saltstone Disposal Facility. This memorandum compares results, where applicable, to Saltstone Waste Acceptance Criteria (WAC) limits and targets. Data pertaining to the regulatory limits for Resource Conservation and Recovery Act (RCRA) metals will be documented at a later time per the Task Technical and Quality Assurance Plan (TTQAP) for the Tank 50H saltstone task. The chemical and radionuclide contaminant results from the characterization of the Fourth Quarter Calendar Year 2015 (CY15) sampling of Tank 50H were requested by SRR personnel and details of the testing are presented in the SRNL Task Technical and Quality Assurance Plan.

  4. Natural gas imports and exports; Fourth quarterly report, 1993

    SciTech Connect

    1993-12-31

    The Office of Fuels Programs prepares quarterly reports summarizing the data provided by companies authorized to import or export natural gas. Companies are required, as a condition of their authorizations, to file quarterly reports with the OFP. This report is for the fourth quarter of 1993 (October--December). Attachment A shows the percentage of takes to maximum firm contract levels and the weighted average per unit price for each of the long-term importers during the 5 most recent reporting quarters. Attachment B shows volumes and prices of gas purchased by long-term importers and exporters during the past 12 months. Attachment C shows volume and price information for gas imported on a short-term basis. Attachment D shows the gas exported on a short-term basis to Canada and Mexico. During 1993, data indicates gas imports grew by about 10 percent over the 1992 level (2328 vs. 2122 Bcf), with Canadian and Algerian imports increasing by 8 and 82 percent, respectively. During the same time period, exports declined by 41 percent (144 vs. 243 Bcf). Exports to Canada decreased 47 percent from the 1992 level (50 vs. 95 Bcf) and exports to Mexico decreased by 60 percent (38 vs. 95 Bcf).

  5. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2004-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information. Contents include the following: RTO Technical Publications: A Quarterly Listing. Implications of Multilingual Interoperability of Speech Technology for Military Use. Non-Lethal Weapons and Future Peace Enforcement Operations.

  6. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2004-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information. Contents include the following: RTO Technical Publications: A Quarterly Listing. Implications of Multilingual Interoperability of Speech Technology for Military Use. Non-Lethal Weapons and Future Peace Enforcement Operations.

  7. Rulison Site groundwater monitoring report fourth quarter, 1996. Revision 4

    SciTech Connect

    1997-04-01

    Project Rulison, a joint US Atomic Energy Commission (AEC) and Austral Oil Company (Austral) experiment, was conducted under the AEC`s Plowshare Program to evaluate the feasibility of using a nuclear device to stimulate natural gas production in low-permeability, gas-producing geologic formations. The experiment was conducted on September 10, 1969, and consisted of detonating a 40-kiloton nuclear device at a depth of 2,568 m below ground surface. This report summarizes the results of the fourth quarter 1996 groundwater sampling event for the Rulison Site, which is located approximately 65 kilometers (km) (40 miles [mi]) northeast of Grand Junction, Colorado. The sampling was performed as part of a quarterly groundwater monitoring program implemented by the US Department of Energy (DOE) to monitor the effectiveness of remediation of a drilling effluent pond located at the site. The effluent pond was used for the storage of drilling mud during drilling of the emplacement hole for a 1969 gas stimulation test.

  8. Mixed Waste Management Facility Groundwater Monitoring Report, Fourth Quarter 1998 and 1998 Summary

    SciTech Connect

    Chase, J.

    1999-04-29

    During fourth quarter 1998, ten constituents exceeded final Primary Drinking Water Standards (PDWS) in groundwater samples from downgradient monitoring wells at the Mixed Waste Management Facility. No constituents exceeded final PDWS in samples from the upgradient monitoring wells.

  9. The Savannah River Site Groundwater Monitoring Program Fourth Quarter 2000 (October thru December 2000)

    SciTech Connect

    Dukes, M.D.

    2001-08-02

    This report summarizes the Groundwater Monitoring Program conducted by SRS during fourth quarter 2000. It includes the analytical data, field data, data review, quality control, and other documentation for this program.

  10. Notable deals in the pharmaceutical industry in the fourth quarter of 2016.

    PubMed

    D'Souza, P

    2017-01-01

    During the fourth quarter of 2016, Cortellis Competitive Intelligence had 889 new deals added as part of its ongoing coverage of pharmaceutical licensing activity. This was an increase on both the last quarter (865) but a decrease from the same quarter for the previous year (915). This article will focus on highlighting a number of the most valuable and notable deals forged during the quarter, as well as a selection of deals from some of the most prolific deal makers. An update on milestones, options and terminated deals of significance will also be presented, along with an early outlook on the next quarter's pharmaceutical licensing activity. Copyright 2017 Clarivate Analytics.

  11. H-Area Acid/Caustic Basin Groundwater Monitoring Report. Fourth Quarter 1994 and 1994 summary

    SciTech Connect

    Chase, J.A.

    1995-03-01

    During fourth quarter 1994, samples collected from the four HAC monitoring wells at the H-Area Acid/Caustic Basin were analyzed for selected heavy metals, herbicides/pesticides, indicator parameters, major ions, radionuclide indicators, and other constituents. Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS) or the Savannah River Site (SRS) flagging criteria or turbidity standard during fourth quarter are the focus of this report.

  12. Metallurgical Laboratory Hazardous Waste Management Facility groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Thompson, C.Y.

    1993-03-01

    During fourth quarter 1992, samples from 18 groundwater monitoring wells of the AMB series at the Metallurgical Laboratory Hazardous Waste Management Facility were analyzed for certain heavy metals, indicator parameters, radionuclides, volatile organic compounds, and other constituents. Six parameters exceeded final Primary Drinking Water Standards (PDWS) and the Savannah River Site Flag 2 criteria during the quarter. The results for fourth quarter 1992 are fairly consistent with the rest of the year`s data. Tetrachloroethylene exceeded the final PDWS in well AMB 4D only two of the four quarters; in the other three wells in which it was elevated, it was present at similar levels throughout the year. Trichloroethylene consistently exceeded its PDWS in wells AMB 4A, 4B, 4D, 5, and 7A during the year. Trichloroethylene was elevated in well AMB 6 only during third and fourth quarters and in well AMB 7 only during fourth quarter. Total alpha-emitting radium was above the final PDWS for total radium in well AMB 5 at similar levels throughout the year and exceeded the PDWS during one of the three quarters it was analyzed for (third quarter 1992) in well AMB 10B.

  13. CNA’s Integrated Ship Database: Fourth Quarter CY 2012 Update

    DTIC Science & Technology

    2014-03-01

    CNA’s Integrated Ship Database Fourth Quarter CY 2012 Update Gregory N. Suess • Lynette A. McClain CNA Interactive Software DIS-2014-U-006685-Final...3 Accessing the database ...13 Changes in database content for this quarter . . . . . . . . . . 25 Routine update of source data

  14. P-Area Acid/Caustic Basin Groundwater Monitoring Report. Fourth quarterly report and summary 1993

    SciTech Connect

    Not Available

    1994-03-01

    During fourth quarter 1993, samples from the six PAC monitoring wells at the P-Area Acid/Caustic Basin were collected and analyzed for indicator parameters, groundwater quality parameters, parameters characterizing suitability as a drinking water supply, and other constituents. Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS) or the Savannah River Site (SRS) flagging criteria or turbidity standard during the quarter are discussed in this report. During fourth quarter 1993, no constituents exceeded the final PDWS. Aluminum and iron exceeded the SRS Flag 2 criteria in five wells. Manganese exceeded its Flag 2 criterion in three wells, while specific conductance exceeded its Flag 2 criterion in one well.

  15. Natural gas imports and exports, fourth quarter report 1999

    SciTech Connect

    2000-03-01

    The Office of Natural Gas and Petroleum Import and Export Activities prepares quarterly reports showing natural gas import and export activity. Companies are required to file quarterly reports. Attachments show the percentage of takes to maximum firm contract levels and the weighted average per unit price for each of the long-term importers during the five most recent quarters, volumes and prices of gas purchased by long-term importers and exporters during the past 12 months, volume and price data for gas imported on a short-term or spot market basis, and the gas exported on a short-term or spot market basis to Canada and Mexico.

  16. Metallurgical Laboratory (HWMF) Groundwater Monitoring Report, Fourth Quarter 1994

    SciTech Connect

    Chase, J.A.

    1995-03-01

    Groundwater flow direction and rate in the M-Area Aquifer Zone were similar to previous quarters. Conditions affecting determination of groundwater flow directions and rates in the Upper Lost Lake Aquifer Zone, Lower Lost Lake Aquifer Zone, and the Middle Sand Aquifer Zone of the Crouch Branch Confining Units were also similar to previous quarters. During second quarter 1994, SRS received South Carolina Department of Health and Environmental Control approval for constructing five point-of-compliance wells and two plume definition wells near the Met Lab Hazardous Waste Management Facility. This project began in July 1994 and is complete; however, analytical data from these wells are not yet available.

  17. Innovative Clean Coal Technology (ICCT): 500 MW demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NO{sub x}) emissions from coal-fired boilers. Technical progress report, Fourth quarter 1992

    SciTech Connect

    Not Available

    1992-12-31

    This quarterly report discusses the technical progress of an Innovative Clean Coal Technology (ICCT) demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NO{sub x}) emissions from coal-fired boilers. The primary goal of this project is the characterization of the low NO{sub x} combustion equipment through the collection and analysis of long-term emissions data. A target of achieving fifty percent NO{sub x} reduction using combustion modifications has been established for the project. The project provides a stepwise retrofit of an advanced overfire air (AOFA) system followed by low NO{sub x} burners (LNB). During each test phase of the project, diagnostic, performance, long-term, and verification testing will be performed. These tests are used to quantify the NO{sub x } reductions of each technology and evaluate the effects of those reductions on other combustion parameters such as particulate characteristics and boiler efficiency. Baseline, AOFA, and LNB without AOFA test segments have been completed. Analysis of the 94 days of LNB tong-term data collected show the full load NO{sub x} emission levels to be approximately 0.65 lb/MBtu. Flyash LOI values for the LNB configuration are approximately 8 percent at full load. Corresponding values for the AOFA configuration are 0.94 lb/MBtu and approximately 10 percent. Abbreviated diagnostic tests for the LNB+AOFA configuration indicate that at 500 MWe, NO{sub x} emissions are approximately 0.55 lb/MBtu with corresponding flyash LOI values of approximately 11 percent. For comparison, the long-term, full load, baseline NO{sub x} emission level was approximately 1.24 lb/MBtu at 5.2 percent LOI. Comprehensive testing of the LNB+AOFA configuration will be performed when the stack particulate emissions issue is resolved.

  18. 500 MW demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NOx) emissions from coal-fired boilers. Technical progress report, fourth quarter, 1994, October 1994--December 1994

    SciTech Connect

    1995-09-01

    This quarterly report discusses the technical progress of an innovative Clean Coal Technology (ICCT) demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NOx) emissions from coal-fired boilers. The project is being conducted at Georgia Power Company`s Plant Hammond Unit 4 located near Rome, Georgia. The primary goal of this project is the characterization of the low NOx combustion equipment through the collection and analysis of long-term emissions data. The project provides a stepwise evaluation of the following NOx reduction technologies: Advanced overfire air (AOFA), Low NOx burners (LNB), LNB with AOFA, and Advanced Digital Controls and Optimization Strategies. The project has completed the baseline, AOFA, LNB, and LNB+AOFA test segments, fulfilling all testing originally proposed to DOE. Analysis of the LNB long-term data collected show the full load NOx emission levels to be near 0.65 lb/MBtu. This NOx level represents a 48 percent reduction when compared to the baseline, full load value of 1.24 lb/MBtu. These reductions were sustainable over the long-term test period and were consistent over the entire load range. Full load, fly ash LOI values in the LNB configuration were near 8 percent compared to 5 percent for baseline. Results from the LNB+AOFA phase indicate that full load NOx emissions are approximately 0.40 lb/MBtu with a corresponding fly ash LOI value of near 8 percent. Although this NOx level represents a 67 percent reduction from baseline levels, a substantial portion of the incremental change in NOx emissions between the LNB and LNB+AOFA configurations was the result of operational changes and not the result of the AOFA system. Phase 4 of the project is now underway.

  19. The Savannah River Site`s Groundwater Monitoring Program. Fourth quarter, 1989

    SciTech Connect

    Not Available

    1989-12-31

    The Environmental Monitoring Section of the Environmental and Health Protection (EHP) Department administers the Savannah River Site`s Groundwater Monitoring Program. During fourth quarter 1989 (October--December), EHP conducted routine sampling of monitoring wells and drinking water locations. EHP collected the drinking water samples from Savannah River Site (SRS) drinking water systems supplied by wells. EHP established two sets of flagging criteria in 1986 to assist in the management of sample results. The flagging criteria aid personnel in sample scheduling, interpretation of data, and trend identification. An explanation of flagging criteria for the fourth quarter is presented in the Flagging Criteria section of this document. All analytical results from fourth quarter 1989 are listed in this report, which is distributed to all waste-site custodians.

  20. Quarterly environmental radiological survey summary -- fourth quarter 1997: 100, 200, 300, and 600 areas

    SciTech Connect

    McKinney, S.M.

    1998-01-27

    Routine radiological surveys are part of near-facility environmental monitoring which monitors and helps direct the reduction of the radiological areas at the Hanford Site. The routine radiological surveys are performed by the Southern Area Remediation Support Group and the Site Support Services Radiological Control Group as directed by Environmental Monitoring and Investigations. The surveys performed have included inactive waste sites; outdoor radiological control areas; tank farm perimeters and associated diversion boxes, lift stations, and vent stations; perimeters of active or uncovered waste sites such as burial grounds, retention basins, ponds, process trenches, and ditches; underground pipelines; and road and rail surfaces. This report provides a synopsis of the radiological surveys performed in support of near-facility environmental monitoring at the Hanford Site during calendar year 1997. The Fourth Quarter 1997 survey results and the status of actions required are also discussed. A waste site survey schedule, Routine Environmental Monitoring Schedule Calendar Year 1997, WHC-SP-0098-8, was developed by Environmental Monitoring and Investigations and reviewed by the Southern Area Remediation Support Group and the Site Support Services Radiological Control Group. Environmental Monitoring and Investigations reviews the radiological survey reports and files a copy for historical purposes and reference. Radiological conditions are tracked and trends noted. All sites are surveyed at least once each year. The survey frequencies for particular sites are based on site history, radiological conditions, and general maintenance. Special surveys may be conducted at irregular frequencies if conditions warrant (e.g., growth of deep-rooted vegetation is noted at a waste site). Radiological surveys are conducted to detect surface contamination and document changes in vegetation growth, biological intrusion, erosion, and general site maintenance conditions. Survey data are

  1. F-Area Acid/Caustic Basin Groundwater Monitoring Report. Fourth Quarter 1994, Groundwater Monitoring Report

    SciTech Connect

    Chase, J.A.

    1994-12-22

    During fourth quarter 1994, samples from the FAC monitoring wells at the F-Area Acid/Caustic Basin were collected and analyzed for herbicides/pesticides, indicator parameters, metals, nitrate, radionuclide indicators, volatile organic compounds, and other constituents. Piezometer FAC 5P was dry and could not be sampled. New monitoring wells FAC 9C, 10C, 11C, and 12C were sampled for the first time during third quarter.

  2. P-Area Acid/Caustic Basin Groundwater Monitoring Report. Fourth Quarter 1994 and 1994 summary

    SciTech Connect

    Chase, J.A.

    1995-03-01

    During fourth quarter 1994, groundwater from the six PAC monitoring wells at the P-Area Acid/Caustic Basin was analyzed for herbicides/pesticides, indicator parameters, metals, nitrate, radionuclide indicators, and other constituents. Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS) or the Savannah River Site (SRS) flagging criteria or turbidity standard during the quarter are discussed in this report.

  3. Mixed Waste Management Facility FSS Well Data Groundwater Monitoring Report. Fourth Quarter 1994 and 1994 summary

    SciTech Connect

    Chase, J.A.

    1995-03-01

    During fourth quarter 1994, ten constituents exceeded final Primary Drinking Water Standards (PDWS) in groundwater samples from downgradient monitoring wells at the Mixed Waste Management Facility, the Old Burial Ground, the E-Area Vaults, the proposed Hazardous Waste/Mixed Waste Disposal Vaults, and the F-Area Sewage Sludge Application Site. No constituent exceeded final PDWS in samples from the upgradient monitoring wells. The groundwater flow directions and rates in the three hydrostratigraphic units were similar to those of previous quarters.

  4. P-Area Acid/Caustic Basin groundwater monitoring report, fourth quarter 1991 and 1991 summary

    SciTech Connect

    Not Available

    1992-03-01

    During fourth quarter 1991, samples from the PAC monitoring wells at the P-Area Acid/Caustic Basin of Savannah River Plant were analyzed for indicator parameters, turbidity, major ions, volatile organic compounds, radionuclides, and other constituents. Monitoring results that exceeded the US Environmental Protection Agency Primary Drinking Water Standards (PDWS) and the Savannah River Site (SRS) flagging criteria and turbidity standards during the quarter, with summary results for the year, are presented in this report.

  5. The AMTEX Partnership{trademark}. Fourth quarter report, September 1994

    SciTech Connect

    Lemon, D.K.; Quisenberry, R.K.

    1994-06-01

    The AMTEX Partnership{trademark} is a collaborative research and development program among the US Integrated Textile Industry, the Department of Energy (DOE), the DOE laboratories, other federal agencies and laboratories, and universities. The goal of AMTEX is to strengthen the competitiveness of this vital industry, thereby preserving and creating US jobs. The operational and program management of the AMTEX Partnership is provided by the Program Office. This report is produced by the Program Office on a quarterly basis and provides information on the progress, operations, and project management of the partnership.

  6. Shale oil value enhancement research. Fourth quarterly report, 1996

    SciTech Connect

    Bunger, J.W.; Russell, C.P.; Tsai, J.C.H.; Cogswell, D.E.; Wright, A.D.

    1997-09-01

    The main activities during this quarter were: (a) separation and characterization of kerogen oil non-polar fractions, (1) participating in the Dawnbreaker Commercial Assistance Program, (c) continuing the liaison with potential industrial partners, and (d) submitting a Phase II final report. In October, we submitted a draft of the final report for the base program and option Ia activities. In this final report, it was concluded that the industry is showing interest in the concept of producing pyridines from kerogen oil. Our economic analysis showed that with current technologies, pyridines can be effectively and economically manufactured from kerogen oil and is competitive with the synthesis manufacturers. It was also recommended that the Government elect to exercise its option to complete the originally proposed program. Performance of research under Option-I(b) will focus on the alternative scheme for refining the pyridine concentrates into pyridine and lower alkyl pyridines which are more valuable and easier to market to the current consumers. Performance of research under Option-II will focus on assuring the market acceptability of kerogen oil products. At the end of November, the U.S. Department of Energy exercised their option to require JWBA to complete the contract as originally awarded. The work on tasks contained in these options will be initiated in the following quarter.

  7. Parachute Creek Shale Oil Program Environmental Monitoring Program. Quarterly report, fourth quarter, October 1-December 31, 1991

    SciTech Connect

    Not Available

    1992-02-28

    The Energy Security Act of 1980 established a program to provide financial assistance to private industry in the construction and operation of commercial-scale synthetic fuels plants. The Parachute Creek Shale Oil Program is one of four projects awarded financial assistance. The Program agreed to comply with existing environmental monitoring regulations and to develop an Environmental Monitoring Plan (EMP) incorporating supplemental monitoring in the areas of water, air, solid waste, and worker health and safety during the period 1985-1992. These activities are described in a series of quarterly and annual reports. The document contains environmental compliance data collected in the fourth quarter of 1991, contents of reports on compliance data submitted to regulatory agencies, and supplemental analytical results from retorted shale pile runoff water collected following a storm event during the third quarter of 1991.

  8. 78 FR 45283 - Military Reservist Economic Injury Disaster Loans Interest Rate for Fourth Quarter FY 2013

    Federal Register 2010, 2011, 2012, 2013, 2014

    2013-07-26

    ... From the Federal Register Online via the Government Publishing Office SMALL BUSINESS ADMINISTRATION Military Reservist Economic Injury Disaster Loans Interest Rate for Fourth Quarter FY 2013 In... following interest rate is effective for Military Reservist Economic Injury Disaster Loans approved on or...

  9. 77 FR 46550 - Military Reservist Economic Injury Disaster Loans; Interest Rate for Fourth Quarter FY 2012

    Federal Register 2010, 2011, 2012, 2013, 2014

    2012-08-03

    ... From the Federal Register Online via the Government Publishing Office SMALL BUSINESS ADMINISTRATION Military Reservist Economic Injury Disaster Loans; Interest Rate for Fourth Quarter FY 2012 In accordance with the Code of Federal Regulations 13--Business Credit and Assistance Sec. 123.512, the following interest rate is effective for Military...

  10. 76 FR 44976 - Military Reservist Economic Injury Disaster Loans; Interest Rate for Fourth Quarter FY 2011

    Federal Register 2010, 2011, 2012, 2013, 2014

    2011-07-27

    ... [Federal Register Volume 76, Number 144 (Wednesday, July 27, 2011)] [Notices] [Page 44976] [FR Doc No: 2011-18897] SMALL BUSINESS ADMINISTRATION Military Reservist Economic Injury Disaster Loans; Interest Rate for Fourth Quarter FY 2011 In accordance with the Code of Federal Regulations 13--Business Credit and Assistance Sec. 123.512, the...

  11. The Savannah River Site's Groundwater Monitoring Program - Fourth Quarter 1999 (October through December 1999)

    SciTech Connect

    Hutchison, J.B.

    2000-10-12

    This report summarizes the Groundwater Monitoring Program conducted by the Savannah River site during fourth quarter 1999. It includes the analytical data, field data, data review, quality control, and other documentation for this program; provides a record of the program's activities; and serves as an official records of the analytical results.

  12. F-Area Seepage Basins groundwater monitoring report, fourth quarter 1991 and 1991 summary

    SciTech Connect

    Not Available

    1992-03-01

    This progress report for fourth quarter 1991 and 1991 summary fro the Savannah River Plant includes discussion on the following topics: description of facilities; hydrostratigraphic units; monitoring well nomenclature; integrity of the monitoring well network; groundwater monitoring data; analytical results exceeding standards; tritium, nitrate, and pH time-trend data; water levels; groundwater flow rates and directions; upgradient versus downgradient results.

  13. Operation Breakthrough, 1973-1974. Final Evaluation Report. And: Fourth Quarterly Progress Report for Operation Breakthrough.

    ERIC Educational Resources Information Center

    EDCON Associates, Willow Grove, PA.

    The document comprises the final evaluation report and the fourth quarterly progress report of Operation Breakthrough, an experimental demonstration project to upgrade Spanish-speaking workers in entry-level factory jobs. Ten classes at six sites with a total of 133 students were held; 53 attended at least 50 of the total 150 hours. Classes were…

  14. The AMTEX Partnership{trademark}. Fourth quarter FY95 report

    SciTech Connect

    1995-09-01

    The AMTEX Partnership{trademark} is a collaborative research and development program among the US Integrated Textile Industry, the Department of Energy (DOE), the national laboratories, other federal agencies and laboratories, and universities. The goal of AMTEX is to strengthen the competitiveness of this vital industry, thereby preserving and creating US jobs. The operations and program management of the AMTEX Partnership{trademark} is provided by the Program Office. This report is produced by the Program Office on a quarterly basis and provides information on the progress, operations, and project management of the partnership. Progress is reported on the following projects: computer-aided fabric evaluation; cotton biotechnology; demand activated manufacturing architecture; electronic embedded fingerprints; on-line process control for flexible fiber manufacturing; rapid cutting; sensors for agile manufacturing; and textile resource conservation.

  15. Identification of subsurface microorganisms at Yucca Mountain; Fourth quarterly report

    SciTech Connect

    Stetzenbach, L.D.

    1993-08-01

    Bacteria isolated from water samples collected in a series of ground water springs have been isolated, enumerated, and identified from twenty six sites. Ten sites were sampled in Death Valley, California and sixteen sites were sampled in Ash Meadows, Nevada. Replicate samples were collected and tested from four locations. All water samples were collected in conjunction with the HRC chemistry group conducting ground water fingerprinting studies. The protocol for collection of samples, as described in the 3rd quarterly report, specified aseptic collection in sterile screw-capped containers and transportation on ice to the HRC microbiology laboratory. All samples were inoculated by spread plating onto R2A (Difco Laboratories, Detroit, MI) bacterial culture medium. the R2A plates were then incubated at 28{degrees} for 5--7 days and colonies wee counted with the aid of a grid template and magnifying lens.

  16. P-Area Acid/Caustic Basin groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Thompson, C.Y.

    1993-03-01

    During fourth quarter 1992, samples from the six PAC monitoring wells at the P-Area Acid/Caustic Basin were analyzed for indicator parameters, groundwater quality parameters, and parameters characterizing suitability as a drinking water supply. Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS) or the Savannah River Site (SRS) flagging criteria or turbidity standard during the quarter are discussed in this report. During fourth quarter 1992, a sample from well PAC 6 exceeded the SRS turbidity standard. Iron and manganese each exceeded its Flag 2 criterion in wells PAC 2, 5, and 6. No analytes exceeded the final PDWS in wells at the P-Area Acid/Caustic Basin during 1992.

  17. Environmental Surveillance data report for the fourth quarter of 1992

    SciTech Connect

    Goldberg, P.Y.; Cooper, R.C.; Hamilton, L.V.; Hughes, J.F.; Horwedel, B.M.; Loffman, R.S.; Salmons, M.C.; Stevens, M.M.; Valentine, C.K.

    1993-02-01

    The Environmental Surveillance and Protection Section within the Office of Environmental Compliance and Documentation at the Oak Ridge National Laboratory (ORNL) is responsible for the development and implementation of an envirorunental program to (1) ensure compliance with all federal, state, and Department of Energy (DOE) reporting requirements to quantitatively demonstrate prevention, control, and abatement of environmental pollution; (2) monitor the adequacy of containment and effluent controls; and (3) assess impacts of releases from ORNL facilities on the environment. Environmental monitoring, as defined by the Regulatory Guide, consists of two major activities: effluent monitoring and environmental surveillance. Effluent monitoring is the collection and analysis of samples or measurements of liquid and gaseous effluents. Monthly or quarterly summaries are presented in this report for each medium sampled. All data are rounded to two significant digits. The summary tables generally give the number of samples collected during the period and the maximum, minimum, average, and standard error of the mean (SE) values of parameters for which determinations were made.

  18. Environmental surveillance data report for the fourth quarter of 1990

    SciTech Connect

    Goldberg, P.Y.; Horwedel, B.M.; Loffman, R.S.; Osborne-Lee, A.E.; Powell, M.R.; Stevens, M.M.; Tardiff, M.F.; Valentine, C.K.; Wolf, D.A.

    1992-01-01

    The Environmental Surveillance and Protection Section within the Office of Environmental and Health Protection at the Oak Ridge National Laboratory (ORNL) is responsible for the development and implementation of an environmental program to (1) ensure compliance with all federal, state, and Department of Energy (DOE) reporting requirements to quantitatively demonstrate prevention, control, and abatement of environmental pollution; (2) monitor the adequacy of containment and effluent controls; and (3) assess impacts of releases from ORNL facilities on the environment. Environmental monitoring, as defined by Draft DOE Order 5400.6, consists of two major activities: effluent monitoring and environmental surveillance. Effluent monitoring is the collection and analysis of sample or measurements of liquid and gaseous effluents. Environmental surveillance is the collection and analysis of samples, or direct measurements, of air, water, soil, foodstuff, biota, and other media from DOE sites and their environs. Monthly or quarterly summaries are presented in this report for each media sampled. All data are rounded to two significant digits. The summary tables generally give the number of samples collected during the period and the maximum, minimum, average, and standard error of the mean (SE) values of parameters for which determinations were made.

  19. CNA’s Integrated Ship Database, Fourth Quarter 2011 Update

    DTIC Science & Technology

    2012-09-01

    Wlde.fangmg techniCal and analyt.cal ser.tees 11𔃻 cntteal areas of operatiC)(IS and management Education Lendmg cntteal decrs•on-maklng suppol\\ to...pollcymakers educators and stakehOlders through research and analys1s program evaluat100 and tec.hnteal ass1stance Health Research & Policy Combmmg...34’Pod and IS.,..,,...,.., by St Re .. .,... Scoontost ()tog Suoss PhD 703824 m1 andRHearcto Spoc ,.losU lyo>e<te McC!an 703 824 2855 Wyou ba>e any

  20. Z-Area Saltstone Disposal Facility groundwater monitoring report, Fourth quarter 1995 and 1995 summary

    SciTech Connect

    Coward, L.S.

    1996-03-01

    Samples from the ZBG wells at the Z-Area Saltstone Disposal Facility are analyzed quarterly for constituents required by South Carolina Department of Health and Environmental Control Industrial Waster Permit IWP-217 and for other constituents as part of the Savannah River Site Groundwater Monitoring Program. During fourth quarter 1995, no constituents were reported above final Primary Drinking Water Standards or SRS flagging criteria. In the past, tritium has been detected sporadically in the ZBG wells at levels similar to those detected before Z Area began radioactive operations.

  1. Rulison Site groundwater monitoring report. Fourth quarter, October 1997--December 1997

    SciTech Connect

    1998-02-01

    This report summarizes the results of the fourth quarter 1997 groundwater sampling event for the Rulison Site, which is located approximately 65 kilometers (km) (40 miles [mi]) northeast of Grand Junction, Colorado. This is the eighth and final sampling event of a quarterly groundwater monitoring program implemented by the U.S. Department of Energy (DOE). This program monitored the effectiveness of remediation of a drilling effluent pond that had been used to store drilling mud during drilling of the emplacement hole for a 1969 gas stimulation test conducted by the U.S. Atomic Energy Commission (AEC) (the predecessor agency to the DOE) and Austral Oil Company (Austral).

  2. Yucca Mountain Site Characterization Project Technical Data Catalog (quarterly supplement)

    SciTech Connect

    1993-06-30

    The June 1, 1985, Department of Energy (DOE)/Nuclear Regulatory Commission (NRC) Site-Specific Procedural Agreement for Geologic Repository Site Investigation and Characterization Program requires the DOE to develop and maintain a catalog of data which will be updated and provided to the NRC at least quarterly. This catalog is to include a description of the data; the time (date), place, and method of acquisition; and where it may be examined. The Yucca Mountain Site Characterization Project (YMP) Technical Data Catalog is published and distributed in accordance with the requirements of the Site-Specific Agreement. The YMP Technical Data Catalog is a report based on reference information contained in the YMP Automated Technical Data Tracking System (ATDT). The reference information is provided by Participants for data acquired or developed in support of the YMP. The Technical Data Catalog is updated quarterly and published in the month following the end of each quarter. A complete revision to the Catalog is published at the end of each fiscal year. Supplements to the end-of-year edition are published each quarter. These supplements provide information related to new data items not included in previous quarterly updates and data items affected by changes to previously published reference information. The Technical Data Catalog, dated December 31, 1992, should be retained as the baseline document for the supplements until the end-of-year revision is published and distributed in October 1993.

  3. Yucca Mountain Site Characterization Project Technical Data Catalog (Quarterly supplement)

    SciTech Connect

    1993-12-31

    The March 21, 1993, Department of Energy (DOE)/Nuclear Regulatory Commission (NRC) Site-Specific Procedural Agreement for Geologic Repository Site Investigation and Characterization Program requires the DOE to develop and maintain a catalog of data which will be updated and provided to the NRC at least quarterly. This catalog is to include a description of the data; the time (date), place, and method of acquisition; and where it may be examined. The Yucca Mountain Site Characterization Project (YMP) Technical Data Catalog is published and distributed in accordance with the requirements of the Site-Specific Agreement. The YMP Technical Data Catalog is a report based on reference information contained in the YMP Automated Technical Data Tracking System (ATDT). The reference information is provided by Participants for data acquired or developed in support of the YMP. The Technical Data Catalog is updated quarterly and published in the month following the end of each quarter. A complete revision to the Catalog is published at the end of each fiscal year. Supplements to the end-of-year edition are published each quarter. These supplements provide information related to new data items not included in previous quarterly updates and data items affected by changes to previously published reference information. The Technical Data Catalog, dated September 30, 1993, should be retained as the baseline document for the supplements until the end-of-year revision is published and distributed in October 1994.

  4. Yucca Mountain Site Characterization Project technical data catalog quarterly supplement

    SciTech Connect

    1995-03-31

    The Department of Energy (DOE)/Nuclear Regulatory Commission (NRC) Site-Specific Procedural Agreement for Geologic Repository Site Investigation and Characterization Program requires the DOE to develop and maintain a catalog of data which will be updated and provided to the NRC at least quarterly. This catalog is to include a description of the data; the time (date), place, and method of acquisition; and where the data may be examined. The Yucca Mountain Site Characterization Project (YMP) Technical Data Catalog is published and distributed in accordance with t requirements of the Site-Specific Agreement. The YMP Technical Data Catalog is a report based on reference information contained in the YMP Automated Technical Data Tracking System (ATDT). The reference information is provided by Participants for data acquired or developed in support of the YMP. The Technical Data Catalog is updated quarterly and distributed in the month following the end of each quarter. A complete revision to the catalog is published at the end of each fiscal year. Supplements to the end-of-year edition are published each quarter. These supplements provide information related to new data items not included in previous quarterly updates and data items affected by changes to@ previously published reference information. The Technical Data Catalog, dated September 30, 1994, should be retained as the baseline document for the supplements until the end-of-year revision is published and distributed in October 1995.

  5. Yucca Mountain Site Characterization Project technical data catalog: Quarterly supplement

    SciTech Connect

    1994-12-31

    The Department of Energy (DOE)/Nuclear Regulatory Commission (NRC) Site-Specific Procedural Agreement for Geologic Repository Site Investigation and Characterization Program requires the DOE to develop and maintain a catalog of data which will be updated and provided to the NRC at least quarterly. This catalog is to include a description of the data; the time (date), place, and method of acquisition; and where the data may be examined. The Yucca Mountain Site Characterization Project (YMP) Technical Data Catalog is published and distributed-in accordance with the requirements of the Site-Specific Agreement. The YMP Technical Data Catalog is a report based on reference information contained in the YMP Automated Technical Data Tracking System (ATDT). The reference information is provided by Participants for data acquired or developed in support of the YMP. The Technical Data Catalog is updated quarterly and distributed in the month following the end of each quarter. A complete revision to the catalog is published at the end of each fiscal year. Supplements to the end-of-year edition are published each quarter. These supplements provide information related to new data items not included in previous quarterly updates and data items affected by changes to previously published reference information. The Technical Data Catalog, dated September 30, 1994, should be retained as the baseline document for the supplements until the end-of-year revision is published and distributed in October 1995.

  6. Yucca Mountain Site Characterization Project: Technical Data Catalog quarterly supplement

    SciTech Connect

    1994-03-31

    The March 21, 1993, Department of Energy (DOE)/Nuclear Regulatory Commission (NRC) Site-Specific Procedural Agreement for Geologic Repository Site Investigation and Characterization Program requires the DOE to develop and maintain a catalog of data which will be updated and provided to the NRC at least quarterly. This catalog is to include a description of the data; the time (date), place, and method of acquisition; and where it may be examined. The Yucca Mountain Site Characterization Project (YMP) Technical Data Catalog is published and distributed in accordance with the requirements of the Site-Specific Agreement. The YMP Technical Data Catalog is a report based on reference information contained in the YMP Automated Technical Data Tracking System (ATDT). The reference information is provided by Participants for data acquired or developed in support of the YMP. The Technical Data Catalog is updated quarterly and published in the month following the end of each quarter. A complete revision to the Catalog is published at the end of each fiscal year. Supplements to the end-of-year edition are published each quarter. These supplements provide information related to new data items not included in previous quarterly updates and data items affected by changes to previously published reference information. The Technical Data Catalog, dated September 30, 1993, should be retained as the baseline document for the supplements until the end-of-year revision is published and distributed in October 1994.

  7. The Savannah River Site`s Groundwater Monitoring Program: Fourth quarter 1991

    SciTech Connect

    Rogers, C.D.

    1992-06-02

    The Environmental Protection Department/Environmental Monitoring Section (EPD/EMS) administers the Savannah River Site`s (SRS) Groundwater Monitoring Program. During fourth quarter 1991, EPD/EMS conducted extensive sampling of monitoring wells. EPD/EMS established two sets of criteria in 1986 to assist in the management of sample results. The flagging criteria do not define contamination levels; instead, they aid personnel in sample scheduling, interpretation of data, and trend identification. Beginning in 1991, the flagging criteria are based on EPA drinking water standards and method detection limits. A detailed explanation of the current flagging criteria is presented in the Flagging Criteria section of this document. Analytical results from fourth quarter 1991 are listed in this report.

  8. The Savannah River Site`s Groundwater Monitoring Program. Fourth quarter 1988

    SciTech Connect

    Not Available

    1989-12-31

    The Environmental Monitoring Group of the Health Protection Department administers the Savannah River Site`s Groundwater Monitoring Program. During fourth quarter 1988 (October--December), routine sampling of monitoring wells and drinking water locations was performed. The drinking water samples were collected from Savannah River Site (SRS) drinking water systems supplied by wells. Two sets of flagging criteria were established in 1986 to assist in the management of sample results. The flagging criteria do not define contamination levels; instead they aid personnel in sample scheduling, interpretation of data, and trend identification. The flagging criteria are based on detection limits, background levels in SRS groundwater, and drinking water standards. An explanation of flagging criteria for the fourth quarter is presented in the Flagging Criteria section of this document. The drinking water samples were analyzed for radioactive constituents.

  9. K-Area Acid/Caustic Basin Groundwater Monitoring Report. Fourth Quarter 1994

    SciTech Connect

    Chase, J.A.

    1995-03-01

    During fourth quarter 1994, samples from the KAC monitoring wells at the K-Area Acid/Caustic Basin were collected and analyzed for herbicides/pesticides, indicator parameters, metals, nitrate, radionuclide indicators, and other constituents. Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS), other Savannah River Site (SRS) Flag 2 criteria, or the SRS turbidity standard are provided in this report.

  10. The Savannah River Site`s Groundwater Monitoring Program. Fourth quarter 1992

    SciTech Connect

    Not Available

    1993-05-17

    This report summarizes the Savannah River Site (SRS) groundwater monitoring program conducted by the Environmental Protection Department`s Environmental Monitoring Section (EPD/EMS) during the fourth quarter of 1992. It includes the analytical data, field data, data review, quality control, and other documentation for this program, provides a record of the program`s activities; and serves as an official document of the analytical results.

  11. Sanitary Landfill Groundwater Monitoring Report. Fourth Quarter 1997 and 1997 Summary

    SciTech Connect

    Chase, J.

    1998-02-01

    A maximum of forty-eight wells of the LFW series monitor groundwater quality in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill at the Savannah River Site (SRS). These wells are sampled quarterly to comply with the South Carolina Department of Health and Environmental Control Domestic Water Permit DWP-087A and as part of the SRS Groundwater Monitoring Program. Chloroethene (vinyl chloride) and trichloroethylene were the most widespread constituents exceeding standards during 1997. Lead (total recoverable), 1,4-dichlorobenzene, mercury, benzene, dichloromethane (methylene chloride), a common laboratory contaminant, tetrachloroethylene, 1,2-dichloroethane, gross alpha, tritium, and 1.2-dichloropropane also exceeded standards in one or more wells. The groundwater flow direction in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill was to the southeast (universal transverse Mercator coordinates). The flow rate in this unit was approximately 139 ft/year during first quarter 1997 and 132 ft/year during fourth quarter.

  12. Mixed Waste Management Facility (MWMF) groundwater monitoring report. Fourth quarter 1993 and 1993 summary

    SciTech Connect

    Butler, C.T.

    1994-03-01

    During fourth quarter 1993, 10 constituents exceeded final Primary Drinking Water Standards in groundwater samples from downgradient monitoring wells at the Mixed Waste Management Facility, the Old Burial Ground, the E-Area Vaults, and the proposed Hazardous Waste/Mixed Waste Disposal Vaults. As in previous quarters, tritium and trichloroethylene were the most widespread elevated constituents. Carbon tetrachloride, chloroform, chloroethane (vinyl chloride), 1,1-dichloroethylene, dichloromethane (methylene chloride), lead, mercury, or tetrachloroethylene also exceeded standards in one or more wells. Elevated constituents were found in numerous Aquifer Zone 2B{sub 2} (Water Table) and Aquifer Zone 2B{sub 1}, (Barnwell/McBean) wells and in two Aquifer Unit 2A (Congaree) wells. The groundwater flow direction and rates in the three hydrostratigraphic units were similar to those of previous quarters.

  13. Mixed waste management facility groundwater monitoring report. Fourth quarter 1995 and 1995 summary

    SciTech Connect

    1996-03-01

    During fourth quarter 1995, seven constituents exceeded final Primary Drinking Water Standards (PDWS) in groundwater samples from downgradient monitoring wells at the Mixed Waste Management Facility. No constituents exceeded final PDWS in samples from the upgradient monitoring wells. As in previous quarters, tritium and trichloroethylene were the most widespread elevated constituents. Chloroethene, gross alpha, lead, mercury, and tetrachloroethylene also exceeded final PDWS in one or more wells. Elevated constituents were found in numerous Aquifer Zone IIB{sub 2} (Water Table) and Aquifer Zone IIB{sub 1} (Barnwell/McBean) wells and in three Aquifer Unit IIA (Congaree) wells. The groundwater flow directions and rates in the three hydrostratigraphic units were similar to those of previous quarters.

  14. Innovative Clean Coal Technology (ICCT): Demonstration of selective catalytic reduction (SCR) technology for the control of nitrogen oxide (NO{sub x}) emissions from high-sulfur coal-fired boilers. Technical progress report, third and fourth quarters 1994

    SciTech Connect

    1995-11-01

    The objective of this project is to demonstrate and evaluate commercially available selective catalytic reduction (SCR) catalysts from U.S., Japanese, and European catalyst suppliers on a high-sulfur U.S. Coal-fired boiler. SCR is a post-combustion nitrogen oxide (NO{sub x}) control technology that involves injecting ammonia into the flue gas generated from coal combustion in an electric utility boiler. The flue gas containing ammonia is then passed through a reactor that contains a specialized catalyst. In the presence of the catalyst, the ammonia reacts with NO{sub x} to form nitrogen and water vapor. Although SCR is widely practiced in Japan and European gas-, oil-, and low-sulfur coal-fired boilers, there are several technical uncertainties associated with applying SCR to U.S. coals. These uncertainties include: (1) potential catalyst deactivation due to poisoning by trace metal species present in U.S. coals that are not present in other fuels; (2) performance of the technology and effects on the balance-of-plant equipment in the presence of high amounts of SO{sub 2} and SO{sub 3}; performance of a wide variety of SCR catalyst compositions, geometries, and methods of manufacture under typical high-sulfur coal-fired utility operating conditions. These uncertainties are being explored by operating a series of small- scale SCR reactors and simultaneously exposing different SCR catalysts to flue gas derived from the combustion of high sulfur U.S. coal. The demonstration is being performed at Gulf Power Company`s Plant Crist Unit No. 5 (75 MW capacity) near Pensacola, Florida. The project is funded by the U.S. Department of Energy (DOE), Southern Company Services, Inc. (SCS on behalf of the entire Southern electric system), the Electric Power Research Institute (EPRI), and Ontario Hydro. SCS is the participant responsible for managing al aspects of this project. 1 ref., 69 figs., 45 tabs.

  15. Hanford Seismic Annual Report and Fourth Quarter Report for Fiscal Year 1999

    SciTech Connect

    AC Rohay; DC Hartshorn; SP Reidel

    1999-12-07

    Hanford Seismic Monitoring provides an uninterrupted collection of high-quality raw and processed seismic data from the Hanford Seismic Network (HSN) for the U.S. Department of Energy and its contractors. Hanford Seismic Monitoring also locates and identifies sources of seismic activity and monitors changes in the historical pattern of seismic activity at the Hanford Site. The data are compiled, archived, and published for use by the Hanford Site for waste management, Natural Phenomena Hazards assessments, and engineering design and construction. In addition, the seismic monitoring organization works with the Hanford Site Emergency Services Organization to provide assistance in the event of a significant earthquake on the Hanford Site. The HSN and the Eastern Washington Regional Network. (EWRN) consist of 40 individual sensor sites and 15 radio relay sites maintained by the Hanford Seismic Monitoring staff. A major reconfiguration of the HSN was initiated at the end of this quarter and the results will be reported in the first quarter report for next fiscal year (FY2000). For the HSN, there were 390 triggers during the fourth quarter of fiscal year(FY) 1999 on the primary recording system. With the implementation of dual backup systems during the second quarter of the fiscal year and an overall increase observed in sensitivity, a total of 1632 triggers were examined, identified, and processed during this fiscal year. During the fourth quarter, 24 seismic events were located by the HSN within the reporting region of 46 degrees to 47 degrees north latitude and 119 degrees to 120 degrees west longitude 9 were earthquakes in the Columbia River Basalt Group, 2 were earthquakes in the pre-basalt sediments, 10 were earthquakes in the crystalline basement; and 2 were quarry blasts. One earthquake appears to be related to a major geologic structure, 14 earthquakes occurred in known swarm areas, and 7 earthquakes were random occurrences.

  16. RTO Technical Report: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2002-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information from April 1,2002 through June 30, 2002. Topics covered include: intrusion detection and design loads for aircraft.

  17. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2001-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information from Oct 1, 2001 through Dec 31, 2001. This listing includes one citataion titled 'Logistics Test and Evaluation in Flight'.

  18. CCC CAMP WICKIUP – OFFICE BUILDING, CENTER; TECHNICAL SERVICE QUARTERS, ...

    Library of Congress Historic Buildings Survey, Historic Engineering Record, Historic Landscapes Survey

    CCC CAMP WICKIUP – OFFICE BUILDING, CENTER; TECHNICAL SERVICE QUARTERS, RIGHT; EDUCATIONAL BUILDING, LEFT. Photocopy of historic photographs (original photograph on file at National Archives, Rocky Mountain Region, Denver, CO). Unknown USBR Photographer, December 9, 1938 - Wickiup Dam, Deschutes River, La Pine, Deschutes County, OR

  19. Quarterly Technical Progress Report June 2015

    SciTech Connect

    Buchholz, Bruce A.

    2015-06-08

    The project has two main goals: 1) Identify the types of adducts naphthalene (NA) forms with DNA and 2) determine whether adduct formation correlates with site selective tumor formation in defined subcompartments of the respiratory tract (respiratory and olfactory nasal epithelium and airways of mice, rats and rhesus monkeys). Five tasks are associated with the completion of the goals. Task 1: Contracting and Animal Use Approvals. IACUC and ACURO approvals are complete, The subcontract with UC Davis (UCD) was executed in December 2014. Task 2: Perform In Vitro Study for Goal 1. Rat samples exposed and in freezer while adduct standards are being made. Mouse samples need to be exposed in next quarter. Task 3: Perform In Vitro Study for Goal 2. Mouse ex vivo samples completed. Rat and monkey samples need to be completed in the next quarter. Task 4: Sample Preparation and Analysis. Mouse Goal 2 samples completed. Other samples remain to be done. Task 5: Data Interpretation and Reporting. Need rat data to write paper on adduct formation.

  20. H-Area Acid/Caustic Basin Groundwater Monitoring Report. Fourth quarterly report and summary 1993

    SciTech Connect

    Not Available

    1994-03-01

    The four monitoring wells at the H-Area Acid/Caustic Basin are sampled quarterly as part of the Savannah River Site (SRS) Groundwater Monitoring Program and to comply with a consent decree signed May 26, 1988, by the US District Court (District of South Carolina, Aiken Division). During fourth quarter 1993, samples from the monitoring wells received comprehensive analyses. Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS), the SRS flagging criteria, or the SRS turbidity standard are the focus of this report. During fourth quarter 1993, tritium exceeded the final PDWS in all four HAC wells, with activities between 3.8E + 01 and 4.6E + 01 pCi/mL. Aluminum exceeded its Flag 2 criterion in wells HAC 2, 3, and 4. Iron exceeded its Flag 2 criterion in wells HAC 1, 2, and 3. Specific conductance was elevated in well HAC 2, total organic halogens exceeded its Flag 2 criterion in wells HAC 2 and 3, and manganese was elevated in wells HAC 3 and 4. No well samples exceeded the SRS turbidity standard.

  1. Department of Energy quarterly technical report

    SciTech Connect

    Anderson, R.N.

    1995-04-15

    The objective is to test the concept that the growth faults in Eugene Island Block 330 (EI-330 field) are conduits through which producing reservoirs are charged and that enhanced production can be developed by producing directly from the fault zone. The site, operated by Penzoil, is located in 250 feet of water and the productive depth intervals include 4000 to 9000 feet. The field demonstration will be accomplished by drilling and production testing of growth fault systems associated with the EI-330 field. The project utilizes advanced 3-D seismic analysis, geochemical studies, structural and stratigraphic reservoir characterization, reservoir simulation, compact visualization systems. In this quarterly report, progress reports are presented for the following tasks: database management; reservoir characterization; modeling; geochemistry; and data integration.

  2. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2002-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information from Jan 1, 2002 through Mar 31, 2002. Topics covered included information management, ice accretion, digital flight control systems, supercavitation flows, and tactical decision aids.

  3. Metallurgical Laboratory Hazardous Waste Management Facility groundwater monitoring report. Fourth quarter 1993 and 1993 summary

    SciTech Connect

    Not Available

    1994-03-01

    The AMB wells at the Metallurgical Laboratory Hazardous Waste Management Facility (Met Lab HWMF) are monitored for selected constituents to comply with the Natural Resources Defense council et al. Consent Decree of May 1988 that identifies the Met Lab HWMF as subject to the Resource Conservation and Recovery Act. In addition, the wells are monitored, as requested, for other constituents as part of the Savannah River Site (SRS) Groundwater Monitoring Program. During the fourth quarter 1993, samples from AMB groundwater monitoring wells at the Metallurgical Laboratory Hazardous Waste Management Facility were analyzed for selected heavy metals, indicator parameters, radionuclides, volatile organic compounds, and other constituents. Six parameters exceeded standards during the quarter. As in previous quarters, dichloromethane (methylene chloride), tetrachloroethylene, and trichloroethylene exceeded final Primary Drinking Water Standards; pH, specific conductance, and total organic halogens exceeded the Savannah River Site Flag 2 criteria in one or more of the wells. Groundwater flow direction and rate in the water-table unit were similar to previous quarters.

  4. F-Area Acid/Caustic Basin Groundwater Monitoring Report. Fourth quarterly report and summary 1993

    SciTech Connect

    Not Available

    1994-03-01

    During fourth quarter 1993, samples from the six FAC monitoring wells at the F-Area Acid/Caustic Basin were collected and analyzed for indicator parameters, groundwater quality parameters, parameters indicating suitability as drinking water, and other constituents. One of the FAC piezometers was scheduled for these analyses but was dry. Analytical results that exceeded the final Primary Drinking Water Standards (PDWS) or the Savannah River Site (SRS) flagging criteria or turbidity standard during the quarter are the focus of this report. Gross alpha exceeded the final PDWS in two wells. Aluminum exceeded its Flag 2 criterion in five wells. Iron exceeded standards in four wells, manganese exceeded standards in two wells, and total organic halogens exceeded standards in one well. Turbidity exceeded the SRS standard in well FAC 3.

  5. F-Area Acid/Caustic Basin groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Not Available

    1993-03-01

    During fourth quarter 1992, samples from the six FAC monitoring wells at the F-Area Acid/Caustic Basin were analyzed for indicator parameters, groundwater quality parameters, parameters indicating suitability as drinking water, and other constituents. Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS) or the Savannah River Site (SRS) flagging criteria or turbidity standard during the quarter are the focus of this report. Gross alpha exceeded the final PDWS in downgradient well FAC 4. Iron exceeded the Flag 2 criterion in 5 of the 6 wells; a change in sampling procedure accounts for marked increases. Three samples were elevated for each of the following constituents: manganese, total organic carbon, and total organic halogens. Turbidity equaled or exceeded the SRS standard in wells FAC 7 and 8.

  6. K-Area Acid/Caustic Basin groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Not Available

    1993-03-01

    During fourth quarter 1992, samples from the KAC monitoring wells at the K-Area Acid/Caustic Basin were analyzed for indicator parameters, groundwater quality parameters, parameters indicating suitability as drinking water, and other constituents. New wells KAC 8 and 9 also were sampled for GC/MS VOA (gas chromatograph/mass spectrometer volatile organic analyses). Monitoring results that exceeded the final Primary Drinking Water Standards (PDWS) or the Savannah River Site (SRS) flagging criteria or turbidity standard during the quarter are discussed in this report. Iron exceeded the Flag 2 criterion in wells KAC 6 and 7, and specific conductance exceeded the Flag 2 criterion in new well KAC 9. No samples exceeded the SRS turbidity standard.

  7. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2001-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information. Reports may be downloaded for free from the RTO website at http://www.rta.nato.int or they may be purchased from the NASA Center for AeroSpace Information, 7121 Standard Drive, Hanover, MD 21076-1320 USA, phone 301-621-0390, fax 301-621-0134. Prices and order forms are available from the NASA STI website at http://www.sti.nasa.gov. An automatic distribution of unclassified RTO technical publications in CD-ROM is also available within the US through the NASA Standing Order Service from the NASA Center for AeroSpace Information.

  8. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2001-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information. Reports may be downloaded for free from the RTO website at http:/www.rta.nato.int or they may be purchased from the NASA Center for AeroSpace Information, 7121 Standard Drive, Hanover, MID 21076-1320 USA, phone 301-621-0390, fax 301-621-0134. Prices and order forms are available from the NASA STI website at http://www.sti.nasa.gov. An automatic distribution of unclassified RTO technical publications in CD-ROM is also available within the U.S. through the NASA Standing Order Service from the NASA Center for AeroSpace Information.

  9. H-Area Seepage Basin (H-HWMF): Fourth quarterly 1989, groundwater quality assessment report

    SciTech Connect

    Not Available

    1990-03-01

    During the fourth quarter of 1989 the wells which make up the H-Area Seepage Basins (H-HWMF){sup 1} monitoring network were sampled. Laboratory analyses were performed to measure levels of hazardous constituents, indicator parameters, tritium, and gross alpha. A Gas Chromatograph Mass Spectrometer (GCMS) scan was performed on all wells sampled to determine any hazardous organic constituents present in the groundwater. The primary contaminants observed at wells monitoring the H-Area Seepage Basins are tritium, nitrate, mercury, gross alpha, and total radium.

  10. Results For The Fourth Quarter 2014 Tank 50 WAC Slurry Sample: Chemical And Radionuclide Contaminants

    SciTech Connect

    Crawford, C.

    2015-09-30

    This report details the chemical and radionuclide contaminant results for the characterization of the Calendar Year (CY) 2014 Fourth Quarter sampling of Tank 50 for the Saltstone Waste Acceptance Criteria (WAC) in effect at that time. Information from this characterization will be used by DWPF & Saltstone Facility Engineering (DSFE) to support the transfer of low-level aqueous waste from Tank 50 to the Salt Feed Tank in the Saltstone Facility in Z-Area, where the waste will be immobilized. This information is also used to update the Tank 50 Waste Characterization System.

  11. H-Area Seepage Basin (H-HWMF): Fourth quarterly 1989, groundwater quality assessment report

    SciTech Connect

    Not Available

    1990-03-01

    During the fourth quarter of 1989 the wells which make up the H-Area Seepage Basins (H-HWMF){sup 1} monitoring network were sampled. Laboratory analyses were performed to measure levels of hazardous constituents, indicator parameters, tritium, and gross alpha. A Gas Chromatograph Mass Spectrometer (GCMS) scan was performed on all wells sampled to determine any hazardous organic constituents present in the groundwater. The primary contaminants observed at wells monitoring the H-Area Seepage Basins are tritium, nitrate, mercury, gross alpha, and total radium.

  12. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2004-01-01

    This is a listing of recent unclassified RTO technical publications for April 1, 2004 through June 30, 2004, processed by the NASA Center for AeroSpace Information. Topics covered include: heat transfer and cooling in propulsion and power systems; assessment of operator functional state; microwaves; aerodynamics in solid rocket propulsion; command, control, communications and intelligence modeling; personal protective equipment against anti-personnel mine blast; and data fusion and visualization.

  13. RTO Technical Publications: A Quarterly Listing

    NASA Technical Reports Server (NTRS)

    2005-01-01

    This is a listing of recent unclassified RTO technical publications processed by the NASA Center for AeroSpace Information covering the period from July 1, 2005 to September 30, 2005; and available in the NASA Aeronautics and Space Database. Contents include: Aeroelastic Deformation: Adaptation of Wind Tunnel Measurement Concepts to Full-Scale Vehicle Flight Testing; Actively Controlling Buffet-Induced Excitations; Modelling and Simulation to Address NATO's New and Existing Military Requirements; Latency in Visionic Systems: Test Methods and Requirements; Personal Hearing Protection including Active Noise Reduction; Virtual Laboratory Enabling Collaborative Research in Applied Vehicle Technologies; A Method to Analyze Tail Buffet Loads of Aircraft; Particle Image Velocimetry Measurements to Evaluate the Effectiveness of Deck-Edge Columnar Vortex Generators on Aircraft Carriers; Introduction to Flight Test Engineering, Volume 14; Pathological Aspects and Associated Biodynamics in Aircraft Accident Investigation;

  14. H-Area Seepage Basins groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Not Available

    1993-03-01

    During fourth quarter 1992, the groundwater at the H-Area Seepage Basins (HASB) was monitored in compliance with South Carolina Hazardous Waste Management Regulations, R61-79.265, Subpart F. Samples were collected from 130 wells that monitor the three separate hydrostratigraphic units that make up the uppermost aquifer beneath the HASB. A detailed description of the uppermost aquifer is included in the Resource Conservation and Recovery Act Part B Post-Closure Care Permit Application for the H-Area Hazardous Waste Management Facility submitted to the South Carolina Department of Health and Environmental Control in December 1990. Historically, as well as currently, tritium, nitrate, total alpha-emitting radium, gross alpha, and mercury have been the primary constituents observed above final Primary Drinking Water Standards (PDWS) in groundwater at the HASB. Isoconcentration/isoactivity maps included in this report indicate both the concentration/activity and extent of the primary contaminants in each of the three hydrostratigraphic units during first and fourth quarter 1992. Water-level maps indicate that the groundwater flow rates and directions at the HASB have remained relatively constant since the basins ceased to be active in 1988.

  15. Sanitary landfill groundwater monitoring report. Fourth quarter 1996 and 1996 summary

    SciTech Connect

    1997-02-01

    A maximum of eighty-nine wells of the LFW series monitor groundwater quality in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill at the Savannah River Site (SRS). These wells are sampled quarterly to comply with the South Carolina Department of Health and Environmental Control Domestic Waste Permit DWP-087A and as part of the SRS Groundwater Monitoring Program. Dichloromethane, a common laboratory contaminant, and chloroethene (vinyl chloride) were the most widespread constituents exceeding standards during 1996. Benzene, trichloroethylene, 1,4-dichlorobenzene, 1,1-dichloroethylene, lead (total recoverable), gross alpha, mercury (total recoverable), tetrachloroethylene, fluoride, thallium, radium-226, radium-228, and tritium also exceeded standards in one or more wells. The groundwater flow direction in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill was to the southeast (universal transverse Mercator coordinates). The flow rate in this unit was approximately 141 ft/year during first quarter 1996 and 132 ft/year during fourth quarter 1996

  16. Sanitary Landfill Groundwater Monitoring Report, Fourth Quarter 1999 and 1999 Summary

    SciTech Connect

    Chase, J.

    2000-03-13

    A maximum of thirty eight-wells of the LFW series monitor groundwater quality in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill Area at the Savannah River Site (SRS). These wells are sampled quarterly to comply with the South Carolina Department of Health and Environmental Control Domestic Water Permit DWP-087A and as part of the SRS Groundwater Monitoring Program. Iron (Total Recoverable), Chloroethene (Vinyl Chloride) and 1,1-Dichloroethane were the most widespread constituents exceeding the Final Primary Drinking Water Standards during 1999. Trichloroethylene, 1,1-Dichloroethylene, 1,2-Dichloroethane, 1,4-Dichlorobenzene, Aluminum (Total Recoverable), Benzene, cis-1,2-Dichloroethylene, Dichlorodifluoromethane, Dichloromethane (Methylene Chloride), Gross Alpha, Mercury (Total Recoverable), Nonvolatile Beta, Tetrachloroethylene, Total Organic Halogens, Trichlorofluoromethane, Tritium also exceeded standards in one or more wells. The groundwater flow direction in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill is to the southeast (universal transverse Mercator coordinates). The flow rate in this unit was approximately 144.175 ft/year during first quarter 1999 and 145.27 ft/year during fourth quarter 1999.

  17. Sanitary Landfill Groundwater Monitoring Report - Third and Fourth Quarters 2000 and 2000 Summary

    SciTech Connect

    Chase, J.A.

    2001-03-07

    A maximum of forty wells of the LFW series monitor groundwater quality in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill Area at the Savannah River Site (SRS). These wells are sampled quarterly to comply with the South Carolina Department of Health and Environmental Control Domestic Waste Permit DWP-087A and as part of the Sanitary Landfill Groundwater Quality Assessment Plan. Chloroethene (vinyl chloride) and trichloroethylene were the most widespread constituent exceeding the Final Primary Drinking Water Standards during the calendar year 2000. 1,4-Dichlorobenzene, benzene, dichloromethane (methylene chloride), gross alpha, lead (total recoverable) mercury (total recoverable), thallium (total recoverable), and tritium also exceeded standards in one or more wells. The groundwater flow direction in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill is to the southeast (universal transverse Mercator coordinates). The flow rate at this unit was approximately 122.64 ft/year during first quarter 2000 and 132.28 ft/year during fourth quarter 2000.

  18. RESULTS FOR THE FOURTH QUARTER 2011 TANK 50 WAC SLURRY SAMPLE: CHEMICAL AND RADIONUCLIDE CONTAMINANT RESULTS

    SciTech Connect

    Bannochie, C.

    2012-01-31

    The Saltstone Facility is designed and permitted to immobilize and dispose of low-level radioactive and hazardous liquid waste (salt solution) remaining from the processing of radioactive material at the Savannah River Site. Low-level waste (LLW) streams from the Effluent Treatment Project (ETP), H-Canyon, and the decontaminated salt solution product from the Actinide Removal Process/Modular Caustic Side Solvent Extraction (CSSX) Unit (ARP/MCU) process are stored in Tank 50 until the LLW can be transferred to the Saltstone Facility for treatment and disposal. The LLW must meet the specified waste acceptance criteria (WAC) before it is processed into saltstone. The specific chemical and radionuclide contaminants and their respective WAC limits are in the current Saltstone WAC. Waste Solidification Engineering (WSE) requested that Savannah River National Laboratory (SRNL) perform quarterly analysis on saltstone samples. The concentrations of chemical and radionuclide contaminants are measured to ensure the saltstone produced during each quarter is in compliance with the current WAC. This report documents the concentrations of chemical and radionuclide contaminants for the 2011 Fourth Quarter samples collected from Tank 50 on October 12, 2011 and discusses those results in further detail than the previously issued results report.

  19. K-Area Acid/Caustic Basin groundwater monitoring report. Fourth quarter 1991 and 1991 summary

    SciTech Connect

    Not Available

    1992-03-01

    During fourth quarter 1991, samples from the KAC monitoring wells at the K-Area Acid/Caustic Basin of Savannah River Plant were analyzed for indicator parameters, turbidity, major ions, volatile organic compounds, radionuclides, and other constituents. Monitoring results that exceeded the US Environmental Protection Agency Primary Drinking Water Standards (PDWS) and the Savannah River Site (SRS) flagging criteria and turbidity standards during the quarter, with summary results for the year, are presented in this report. No constituents exceeded the PDWS at the K-Area Acid/Caustic Basin. Iron and total organic halogens exceeded Flag 2 criteria in sidegradient-to-downgradient well KAC 7 but not in other KAC wells. No priority pollutants (EPA, 1990) exceeded the PDWS or the Flag 2 criteria in wells KAC 1 and 3. None of the KAC wells exceeded the SRS turbidity standard. Lead exceeded the PDWS in well KAC 7 during first quarter. No other constituent exceeded the PDWS at the K-Area Acid/Caustic Basin during the year.

  20. Air Force Office of Scientific Research, Air Force Systems Command Technical Report Summaries. First Quarter 1986.

    DTIC Science & Technology

    1986-03-01

    The AFOSR Technical Report Summaries are published quarterly by the Air Force Office of Scientific Research (AFOSR) of each calendar year. They...consist of a brief summary of each AFOSR technical report received in the Technical Information Division and submitted to the Defense Technical Information Center for that quarter.

  1. K-Area and Par Pond Sewage Sludge Application Sites Groundwater Monitoring Report. Fourth quarter 1993 and summary 1993

    SciTech Connect

    Not Available

    1994-04-01

    Samples from the three wells at the K-Area Sewage Sludge Application Site (KSS wells) and the three wells at the Par Pond Sewage Sludge Application Site (PSS wells) are analyzed quarterly for constituents required by South Carolina Department of Health and Environmental Control Construction Permit 13,173 and, as requested, for other constituents as part of the Savannah River Site (SRS) Groundwater Monitoring Program. Annual analyses for other constituents, primarily metals, also are required by the permit. Dichloromethane (methylene chloride) exceeded the final Primary Drinking Water Standard in a single well of the K-Area Sewage Sludge Application Site during fourth quarter 1993. Aluminum, iron, and lead, reported in excess of the SRS Flag 2 criteria at both the K-Area and Par Pond Sewage Sludge Application Sites during third quarter 1993, were not analyzed fourth quarter.

  2. Results of the fourth quarter tritium survey of the F- and H-Area seeplines: March--April 1993

    SciTech Connect

    Dixon, K.L.; Rogers, V.A.

    1993-07-01

    The Environmental Sciences Section (ESS) established a quarterly monitoring program of the Four Mile Creek seepline down gradient from the F- and H-Area seepage basins. The program surveys and tracks changes in tritium, specific conductivity, and pH for the seepline water. Measurements from the fourth quarter survey (March/April 1993) showed lower tritium and conductivity measurements and higher pH values (pH 5--6) than measurements from previous studies. The results of the first four quarterly surveys suggest that infiltration of rainfall may be diluting and flushing the contaminants from the groundwater system. More measurements are needed to confirm these trends.

  3. F- and H-Area Sewage Sludge Application Sites groundwater monitoring report, fourth quarter 1991

    SciTech Connect

    Thompson, C.Y.

    1992-03-01

    Eleven sewage sludge application sites at the Savannah River Site (SRS) were originally the subject of a research program, begun in 1980, using domestic sewage sludge to reclaim borrow pits and to enhance forest productivity at SRS. Currently, the F- and H-Area Sewage Sludge Application Sites are the only remaining active sludge application sites. During fourth quarter 1991, samples from the four monitoring wells at the F-Area site (FSS series) and three monitoring wells at the H-Area site (HSS series) were analyzed for specific conductance, pH, and certain pesticides, herbicides, toxic metals, water quality indicators, and radionuclides. This report describes monitoring results that exceeded the US Environmental Protection Agency primary drinking water standards (PDWS) and the SRS flagging criteria.

  4. The Savannah River Site`s Groundwater Monitoring Program. Fourth quarter, 1990

    SciTech Connect

    Not Available

    1991-06-18

    This report summarizes the Savannah River Site (SRS) groundwater monitoring program conducted in the fourth quarter of 1990. It includes the analytical data, field data, well activity data, and other documentation for this program, provides a record of the program`s activities and rationale, and serves as an official document of the analytical results. The groundwater monitoring program includes the following activities: installation, maintenance, and abandonment of monitoring wells, environmental soil borings, development of the sampling and analytical schedule, collection and analyses of groundwater samples, review of analytical and other data, maintenance of the databases containing groundwater monitoring data, quality assurance (QA) evaluations of laboratory performance, and reports of results to waste-site facility custodians and to the Environmental Protection Section (EPS) of EPD.

  5. F-Area Seepage Basins groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Not Available

    1993-03-01

    During fourth quarter 1992, the groundwater at the F-Area Seepage Basins (FASB) was monitored in compliance with South Carolina Hazardous Waste Management Regulations, R61-79.265, Subpart F. Eighty-five wells provided samples from the three hydrostratigraphic units that make up the uppermost aquifer beneath the FASB. A detailed description of the uppermost aquifer is included in the Resource Conservation and Recovery Act Part B Post-Closure Care Permit Application for the F-Area Hazardous Waste Management Facility submitted to the South Carolina Department of Health and Environmental Control in December 1990. Historically, as well as currently, tritium, nitrate, gross alpha, total alpha-emitting radium, cadmium, and lead are the primary constituents observed above final Primary Drinking Water Standards (PDWS) in groundwater at the FASB. Nonvolatile beta has consistently exceeded its drinking water screening level. Other radionuclides and hazardous constituents also have exceeded the final PDWS in the groundwater at the FASB. The elevated constituents are found primarily in Aquifer Zone IIB{sub 2} (Water Table) and Aquifer Zone IIB{sub 1}, (Barnwell/McBean) wells. However, several Aquifer Unit IIA (Congaree) wells also contain elevated levels of constituents, primarily tritium. Isoconcentration/isoactivity maps included in this report indicate both the concentration/ activity and extent of the primary contaminants in each of the three hydrostratigraphic units for first and fourth quarters 1992. Water-level maps indicate that the groundwater flow rates and directions at the FASB have remained relatively constant since the basins ceased to be active in 1988.

  6. Mixed Waste Management Facility (MWMF) groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Not Available

    1993-03-01

    During fourth quarter 1992, nine constituents exceeded final Primary Drinking Water Standards (PDWS) in one or more groundwater samples from monitoring wells at the Mixed Waste Management Facility (MWMF) and adjacent facilities. As in previous quarters, tritium and trichloroethylene were the most widespread constituents. Fifty-seven (48%) of the 120 monitoring wells, contained elevated tritium activities, and 23 (19%) contained elevated trichloroethylene concentrations. Total alpha-emitting radium, tetrachloroethylene, chloroethene, cadmium, 1,1-dichloroethylene, lead, or nonvolatile beta levels exceeded standards in one or more wells. During 1992, elevated levels of 13 constituents were found in one or more of 80 of the 120 groundwater monitoring wells (67%) at the MWMF and adjacent facilities. Tritium and trichloroethylene exceeded their final PDWS more frequently and more consistently than did other constituents. Tritium activity exceeded its final PDWS m 67 wells and trichloroethylene was. elevated in 28 wells. Lead, tetrachloroethylene, total alpha-emitting radium, gross alpha, cadmium, chloroethene, 1,1-dichloroethylene 1,2-dichloroethane, mercury, or nitrate exceeded standards in one or more wells during the year. Nonvolatile beta exceeded its drinking water screening level in 3 wells during the year.

  7. Idaho National Engineering and Environmental Laboratory Offsite Environmental Surveillance Program Report: Fourth Quarter 1998

    SciTech Connect

    T. Saffle; R. Evans

    1999-08-01

    The Environmental Science and Research Foundation conducts the Offsite Environmental Surveillance Program at the US Department of Energy's Idaho National Engineering and Environmental Laboratory (INEEL). The Foundation's environmental surveillance program monitors the effects, if any, of US Department of Energy (DOE) activities on the offsite environment, collects data to confirm compliance with applicable environmental laws and regulations, and observes any trends in the environmental levels of radioactivity. This report for the fourth quarter 1998 is based on 622 samples collected of air, fine particulates, atmospheric moisture, precipitation, water, milk, potatoes, and game animals. All concentrations of radioactivity found in these samples were consistent with concentrations which have been found in sampling during recent quarters and which have been attributed in the past to natural background radioactivity, worldwide fallout from past nuclear weapons testing, an! d nuclear operations around the world. No measured concentrations could be directly attributed to operations at the INEEL, although statistical differences did exist between on-site and distant gross beta concentrations. No evidence could be found to link these differences with a specific INEEL source. Concentrations in all samples were below the guidelines set by both the DOE and the US Environmental Protection Agency (EPA) for protection of the public.

  8. Renewable Energy Finance Tracking Initiative (REFTI): Snapshot of Recent Geothermal Financing Terms, Fourth Quarter 2009 - Second Half 2011

    SciTech Connect

    Lowder, T.; Hubbell, R.; Mendelsohn, M.; Cory, K.

    2012-09-01

    This report is a review of geothermal project financial terms as reported in the National Renewable Energy Laboratory's Renewable Energy Finance Tracking Initiative (REFTI). The data were collected over seven analysis periods from the fourth quarter (Q4) of 2009 to the second half (2H) of 2011.

  9. F-Area Acid/Caustic Basin groundwater monitoring report. 1991 Annual report, fourth quarter 1991 and 1991 summary report

    SciTech Connect

    Thompson, C.Y.

    1992-03-01

    This progress report for fourth quarter 1991 and 1992 summary from the Savannah River Plant includes discussion on the following topics: groundwater monitoring data; analytical results exceeding standards; upgradient versus downgradient results; turbidity results exceeding standards; water elevations, flow directions, and flow rates.

  10. PFBC HGCU Test Facility. Technical progress report No. 24, Third quarter, CY 1995

    SciTech Connect

    1995-10-01

    This is the twenty-fourth and final Technical Progress Report submitted to the Department of Energy (DOE) in connection with the cooperative agreement between the DOE and Ohio Power Company for the Tidd PFBC Hot Gas Clean Up Test Facility. This report covers the work completed during the Third Quarter of CY 1995. All activity this quarter was directed toward the completion of the program final report. A draft copy of the final report was forwarded to DOE during this quarter, and DOE submitted their comments on the report to AEPSC. DOE requested that Westinghouse write an appendix to the report covering the performance of the fail-safe regenerator devices during Tad operation, and Westinghouse subsequently prepared the appendix. Additional DOE comments were incorporated into the report, and it will be issued in camera-ready form by the end of October, 1995, which is the program end date. Appendix 1 presents the results of filter candle posttest examination by Westinghouse performed on selected filter candles following final shutdown of the system.

  11. F- and H-Area Sewage Sludge Application Sites groundwater monitoring report. Fourth quarter 1993 and 1993 summary

    SciTech Connect

    Not Available

    1994-04-01

    Samples from the four wells at the F-Area Sewage Sludge Application Site (FSS wells) and the three wells at the H-Area Sewage Sludge Application Site (HSS wells) are analyzed quarterly for constituents as required by South Carolina Department of Health and Environmental Control Construction Permit 12,076 and, as requested, for other constituents as part of the Savannah River Site (SRS) Groundwater Monitoring Program. Annual analyses for other constituents, primarily metals, also are required by the permit. No constituent exceeded either the final Primary Drinking Water Standards or the SRS Flag 2 criteria during fourth quarter 1993. Iron, lead, and manganese were the only permit- required analytes that exceeded standards at the F- and H-Area Sewage Sludge Application Sites in 1993. Tritium, aluminum, and other constituents not included in the permit have exceeded standards at this site previously, but only sporadically. These constituents were not analyzed fourth quarter 1993.

  12. Phase II - photovoltaics for utility scale applications (PVUSA). Quarterly technical report, First quarter 1996

    SciTech Connect

    1996-07-01

    This is the first of three planned quarterly Technical Reports of 1996 system performance and major project activities. The final quarter will be discussed in the 1996 Progress Report. Activity for the PVUSA project was curtailed considerably, pending resolution of the transfer of management to the California Energy Commission (CEC) and the Sacramento Municipal Utility District (SMUD). Principal activities during the first quarter of 1996 included: (1) Continued negotiations regarding the transfer of project management from PG&E to the joint CEC/SMUD team. Primary remaining hurdle is obtaining approval from the California Public Utilities Commission. (2) Provided training to CEC and SMUD project team members on January 8, 9, and 11. Training covered site operations including data acquisition. (3) Completed the draft of the 1995 Progress Report. (4) Supported the contractor in their efforts for enhancing the performance and reliability of the Amonix EMT-3 array at Davis. (5) Reviewed the PSCo installation drawings, and started activities to provide the PVUSA DAS equipment, (6) Operation and maintenance of existing systems, including data collection and reporting. Data were collected for 19 completed systems with a combined capacity of 1,800 kW. Combined, these systems generated nearly 1.1 million kWh during January through March. The project`s cumulative generation now stands at 8.2 million kWh. Key cumulative 1996 results are listed in the following table. The locations of systems other than Davis are noted alongside the supplier`s name.

  13. Development of vanadium-phosphate catalysts for methanol production by selective oxidation of methane. Quarterly technical progress report 4, July--September 1993

    SciTech Connect

    McCormick, R.L.; Jha, M.C.; Streuber, R.D.

    1993-12-07

    This document is the fourth quarterly technical progress report under Contract No. DE-AC22-92PC92110, {open_quotes}Development of Vanadium-Phosphate Catalysts for Methanol Production by Selective Oxidation of Methane.{close_quotes} During this quarter, the authors focused primarily on catalyst activity testing in the microreactor. Additional blank runs using methane and methanol were performed. Initial attempts at preparing a silica supported catalyst are described. These results are discussed in detail and plans for the coming quarter are outlined.

  14. RESULTS FOR THE FOURTH QUARTER TANK 50 WAC SLURRY SAMPLE: CHEMICAL AND RADIONUCLIDE CONTAMINANT RESULTS

    SciTech Connect

    Reigel, M.; Bibler, N.

    2010-01-27

    The Saltstone Facility is designed and permitted to immobilize and dispose of low-level radioactive and hazardous liquid waste (salt solution) remaining from the processing of radioactive material at the Savannah River Site. Low-level waste (LLW) streams from the Effluent Treatment Project (ETP), H-Canyon, the DDA (Deliquification, Dissolution, and Adjustment) process, and the decontaminated salt solution product from the Actinide Removal Process/Modular Caustic Side Solvent Extraction (CSSX) Unit (ARP/MCU) process are stored in Tank 50 until the LLW can be transferred to the Saltstone Facility for treatment and disposal. The LLW must meet the specified waste acceptance criteria (WAC) before it is processed into saltstone. The specific chemical and radionuclide contaminants and their respective WAC limits are listed in the current Saltstone WAC. SRS Liquid Waste Operations (LWO) requested that Savannah River National Laboratory (SRNL) perform quarterly analysis on saltstone samples. The concentrations of chemical and radionuclide contaminants are measured to ensure the saltstone produced during each quarter is in compliance with the current WAC. This report documents the concentrations of chemical and radionuclide contaminants for the 2009 Fourth Quarter samples collected from Tank 50 on October 2, 2009 and discusses those results in further detail than the previously issued results report. This report details the chemical and radionuclide contaminant results for the characterization of the 2009 Fourth Quarter sampling of Tank 50 for the Saltstone Waste Acceptance Criteria (WAC). Information from this characterization will be used by Liquid Waste Operations (LWO) to support the transfer of low-level aqueous waste from Tank 50 to the Salt Feed Tank in the Saltstone Facility in Z-Area, where the waste will be immobilized. This information is also used to update the Tank 50 Waste Characterization System. The following conclusions are drawn from the analytical results

  15. RESULTS FOR THE FOURTH QUARTER 2013 TANK 50 WAC SLURRY SAMPLE CHEMICAL AND RADIONUCLIDE CONTAMINANTS

    SciTech Connect

    Bannochie, C.

    2014-04-01

    This report details the chemical and radionuclide contaminant results for the characterization of the 2013 Fourth Quarter sampling of Tank 50 for the Saltstone Waste Acceptance Criteria (WAC) in effect at that time. Information from this characterization will be used by DWPF & Saltstone Facility Engineering (DSFE) to support the transfer of low-level aqueous waste from Tank 50 to the Salt Feed Tank in the Saltstone Facility in Z-Area, where the waste will be immobilized. This information is also used to update the Tank 50 Waste Characterization System. The following conclusions are drawn from the analytical results provided in this report: SRR WAC targets or limits were met for all analyzed chemical and radioactive contaminants unless noted in this section. {sup 59}Ni, {sup 94}Nb, {sup 247}Cm, {sup 249}Cf, and {sup 251}Cf are above the requested SRR target concentrations. However, they are below the detection limits established by SRNL. Norpar 13 and Isopar L have higher detection limits compared with the Saltstone WAC. The data provided in this report is based upon the concentrations in the sub-sample, and due to the limited solubility of these materials in aqueous solution, may not represent the concentrations of the analytes in Tank 50. The low insoluble solids content increases the measurement uncertainty for insoluble species. The semivolatile organic analysis (SVOA) method employed in the measurement of Norpar 13 and tributyl phosphate (TBP) has resulted in the erroneous reporting of a variety of small chain alcohols, including 4-methyl-3-hexanol and 5-methyl-3-hexanol, in previous quarterly sample reports. It has now been determined that these alcohols are an artifact of the sample preparation. Further work is being conducted in SRNL to delineate the conditions that produce these alcohols, and these findings will be reported separately.

  16. RESULTS FOR THE FOURTH QUARTER 2010 TANK 50 WAC SLURRY SAMPLE: CHEMICAL AND RADIONUCLIDE CONTAMINANT RESULTS

    SciTech Connect

    Reigel, M

    2011-02-22

    This report details the chemical and radionuclide contaminant results for the characterization of the 2010 Fourth Quarter sampling of Tank 50 for the Saltstone Waste Acceptance Criteria (WAC). Information from this characterization will be used by Liquid Waste Operations (LWO) to support the transfer of low-level aqueous waste from Tank 50 to the Salt Feed Tank in the Saltstone Facility in Z-Area, where the waste will be immobilized. This information is also used to update the Tank 50 Waste Characterization System. The following conclusions are drawn from the analytical results provided in this report: (1) The concentrations of the reported chemical and radioactive contaminants were less than their respective WAC targets or limits unless noted in this section. (2) The reported detection limits for {sup 94}Nb, {sup 247}Cm and {sup 249}Cf are above the requested limits from Reference 2. However, they are below the limits established in Reference 3. (3) There is an estimated concentration of trimethylbenzene (2.25 mg/L). This is not a WAC analyte, but it is the first time this organic compound has been detected in a quarterly WAC sample from Tank 50. (4) The reported detection limit for Norpar 13 is greater than the limit from Table 4 and Attachment 8.2 of the WAC. (5) The reported detection limit for Isopar L is greater than the limit from Table 3 of the WAC. (6) Isopar L and Norpar 13 have limited solubility in aqueous solutions making it difficult to obtain consistent and reliable sub-samples. The values reported in this memo are the concentrations in the sub-sample as detected by the GC/MS; however, the results may not accurately represent the concentrations of the analytes in Tank 50.

  17. Mixed Waste Management Facility (MWMF) Groundwater Monitoring Report: Fourth quarter 1991 and 1991 summary

    SciTech Connect

    Thompson, C.Y.

    1992-03-01

    During fourth quarter 1991, tritium, trichloroethylene, tetrachloroethylene, chloroethene (vinyl chloride), total radium, mercury, and lead exceeded the US Environmental Protection Agency primary drinking water standards (PDWS) in groundwater samples from monitoring wells at the Mixed Waste Management Facility (MWMF) and adjacent facilities. Tritium and trichloroethylene were the most widespread contaminants; 55 (49%) wells exhibited elevated tritium activities, and 24 (21%) wells exhibited elevated trichloroethylene concentrations. Tritium and trichloroethylene levels exceeding the PDWS also occurred in several wells in Aquifer Unit IIA (Congaree). Levels of manganese, total organic halogens, nickel, iron, 1,1-dichloroethane, aluminum, nonvolatile beta, and trichlorofluoromethane that exceeded Flag 2 criteria were found in one or more wells beneath the MWMF. Downgradient wells in the three hydrostratigraphic units at the MWMF contained elevated levels of tritium, trichloroethylene, tetrachloroethylene, total radium, chloroethene (vinyl chloride), lead, mercury, manganese, total organic halogens, nickel, iron, 1,1-dichloroethane, aluminum, nonvolatile beta, or trichlorofluoromethane. Groundwater samples from 81 (72%) of the monitoring wells at the MWMF and adjacent facilities contained elevated levels of several contaminants.

  18. Results for the Fourth Quarter 2012 Tank 50 WAC Slurry Sample: Chemical and Radionuclide Contaminants

    SciTech Connect

    Bannochie, Christopher J.

    2014-09-30

    This report details the chemical and radionuclide contaminant results for the characterization of the 2012 Fourth Quarter sampling of Tank 50 for the Saltstone Waste Acceptance Criteria (WAC).1 Information from this characterization will be used by Waste Solidification Engineering (WSE) to support the transfer of low-level aqueous waste from Tank 50 to the Salt Feed Tank in the Saltstone Facility in Z-Area, where the waste will be immobilized. This information is also used to update the Tank 50 Waste Characterization System. The following conclusions are drawn from the analytical results provided in this report: The concentration of the reported chemical and radioactive contaminants were less than their respective WAC Limits and Targets, unless noted in this section. Norpar 13 and Isopar L have higher detection limits5 compared with the Saltstone WAC1. The data provided in this report is based upon the concentrations in the sub-sample, and due to the limited solubility in aqueous solution, may not represent the concentrations of the analytes in Tank 50. Diisooctyl adipate (or diisooctyl hexanedioate) was measured at 1.30E+00 mg/L in one of two replicate measurements conducted on an at-depth sample.a The organic analysis of the at-depth sample was conducted at the request of SRR.4 This analyte was below the detection limit in the surface sample. The low insoluble solids content increases the measurement uncertainty for insoluble species.

  19. Technical Data Catalog: Yucca Mountain Site Characterization Project. Quarterly supplement

    SciTech Connect

    1995-06-30

    This report presents reference information contained in the Yucca Mountain Project Automated Technical Data Tracking System. The Department of Energy is seeking to design and maintain a geologic repository for the disposal of high-level radioactive wastes. However, before this repository can be built, the DOE must first do a comprehensive site evaluation. This evaluation is subject to many regulations. This report fulfills the reporting requirements of the Site-Specific Procedural Agreement for Geologic Repository to develop and maintain a catalog of data which will be updated and provided to the Nuclear Regulatory Commission on a quarterly basis. This catalog contains: description of data; time, place, and method of acquisition; and where data may be examined.

  20. Phase 2 -- Photovoltaics for utility scale applications (PVUSA). Quarterly technical report, third quarter 1996

    SciTech Connect

    1996-12-01

    PVUSA is now monitoring 20 systems at nine locations with a combined capacity of 1,800 kW. This is the first quarter that performance data are being reported on the Amonix EMT-3 array. One additional 375-kW system is under construction in Yuma, AZ and is scheduled to start up in December 1996. Combined, these systems generated 0.8 million kWh during July through September, increasing the project cumulative total to 9.2 million kWh since 1989. The report discusses project management including schedule analysis, cost analysis and funding activities, and technology transfer activities. A section of the report gives a technical analysis of the Davis site describing performance data for the 11 systems, weather data, operation and maintenance. Performance of the other 9 PVUSA sites is briefly discussed.

  1. High Energy Density Physics technical quarterly, October--December 1994. Volume 3

    SciTech Connect

    1995-09-01

    The High Energy Density Physics Technical Quarterly (formerly the AGEX 2 Technical Quarterly) publishes short technical contributions on above ground experiments that use pulsed power and laser drivers. The Quarterly is intended to provide rapid exposure of timely technical ideas and results as well as a means for documenting High Energy Density Physics progress and scientific quality for the High Energy Density Physics community. Two articles are included in this volume. They are ``Simulation and Analysis of PEGII-25`` and ``Resistor Developments for Atlas Marx Modules``.

  2. Results For The Fourth Quarter 2012 Tank 50 WAC Slurry Sample: Chemical And Radionuclide Contaminants

    SciTech Connect

    Bannochie, C. J.

    2013-02-05

    This report details the chemical and radionuclide contaminant results for the characterization of the 2012 Fourth Quarter sampling of Tank 50 for the Saltstone Waste Acceptance Criteria (WAC).Information from this characterization will be used by Waste Solidification Engineering (WSE) to support the transfer of low-level aqueous waste from Tank 50 to the Salt Feed Tank in the Saltstone Facility in Z-Area, where the waste will be immobilized. This information is also used to update the Tank 50 Waste Characterization System. The following conclusions are drawn from the analytical results provided in this report: The concentration of the reported chemical and radioactive contaminants were less than their respective WAC Limits and Targets, unless noted in this section; Norpar 13 and Isopar L have higher detection limits compared with the Saltstone WAC. The data provided in this report is based upon the concentrations in the sub-sample, and due to the limited solubility in aqueous solution, may not represent the concentrations of the analytes in Tank 50; Diisooctyl adipate (or diisooctyl hexanedioate) and 5-methyl-3-hexanol, plasticizers, were measured at 1.30E+00 mg/L and 3.00E+00 mg/L, respectively, in one of two replicate measurements conducted on an at-depth sample. The organic analysis of the at-depth sample was conducted at the request of SRR. These analytes were below the detection limits for the surface sample; and, The low insoluble solids content increases the measurement uncertainty for insoluble species.

  3. F- and H-Area Sewage Sludge Application Sites groundwater monitoring report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Not Available

    1993-04-01

    Samples from the four wells at the F-Area Sewage Sludge Application Site (FSS wells) and the three wells at the H-Area Sewage Sludge Application Site (HSS wells) are analyzed quarterly for constituents as required by South Carolina Department of Health and Environmental Control Construction Permit 12,076 and, as requested, for other constituents as part of the Savannah River Site Groundwater Monitoring Program. Annual analyses for other constituents, primarily metals, also are required by the permit. During fourth quarter 1992, the FSS wells also were analyzed for a number of other constituents not required by the permit. Historically and currently, no permit-required analytes exceed standards at the F- and H-Area Sewage Sludge Application Sites except iron, lead, and manganese, which occur in elevated concentrations frequently in FSS wells. Lead concentrations exceeded the final Primary Drinking Water Standards during fourth quarter 1992, an event that is concurrent with a change in sampling procedures. Tritium is the primary nonpermit constituent that exceeds standards at the F-Area Sewage Sludge Application Site. Other constituents also exceed standards at this site but only sporadically.

  4. Regulatory and technical reports (abstract index journal). Compilation for third quarter 1997, July--September

    SciTech Connect

    Stevenson, L.L.

    1998-01-01

    This compilation consists of bibliographic data and abstracts for the formal regulatory and technical reports issued by the US Nuclear Regulatory Commission (NRC) Staff and its contractors. It is NRC`s intention to publish this compilation quarterly and to cumulate it annually. This report contains the third quarter 1997 abstracts.

  5. SERI biofuels program. Quarterly technical report, second and third quarters, FY 1985

    SciTech Connect

    Bull, S.R.; Lowenstein, M.Z.; McIntosh, R.P.

    1985-07-01

    Highlights of progress accomplished during the second and third quarters of FY 1985 in the areas of aquatic species, anaerobic digestion and photobiological hydrogen production research are summarized. The following accomplishments were attained in aquatic species research: evaluation of the growth of marine species in desert saline waters; preliminary evaluation of potential gains in productivity from utilization of light modulation; determined the relationship between the initial carbohydrate accumulation and subsequent lipid synthesis in Ankistrodesmus; completed designs and analysis of three outdoor systems; completed evaluations on the use of immobilized systems for the production of fuels; completed economic and technical evaluation of two harvesting schemes for microalgae; and completed evaluation of macroalgal production concepts and submit research plan. In the area of anaerobic digestion research, the following tasks were accomplished: received final report on autohydrolysis; received final report on genetic engineering of methanogens; completed computerized data based on commercial anaerobic digesters; completed analysis of anaerobic digestion for energy and submitted draft white paper to DOE program managers; and made presentations on ''Anaerobic Digestion for Energy'' and ''Potential for Improvement of Anaerobic Digestion Technology'' to DOE program managers. In photobiological hydrogen production, program wrap-up was completed and a final draft of the program report was submitted.

  6. Atmospheric Properties from the 2006 Niamey Deployment and Climate Simulation with a Geodesic Grid Coupled Climate Model Fourth Quarter 2008

    SciTech Connect

    JH Mather; DA Randall; CJ Flynn

    2008-09-30

    In 2008, the Atmospheric Radiation Measurement (ARM) Program and the Climate Change Prediction Program (CCPP) have been asked to produce joint science metrics. For CCPP, the metrics will deal with a decade-long control simulation using geodesic grid-coupled climate model. For ARM, the metrics will deal with observations associated with the 2006 deployment of the ARM Mobile Facility (AMF) to Niamey, Niger. Specifically, ARM has been asked to deliver data products for Niamey that describe cloud, aerosol, and dust properties. The first quarter milestone was the initial formulation of the algorithm for retrieval of these properties. The second quarter milestone included the time series of ARM-retrieved cloud properties and a year-long CCPP control simulation. The third quarter milestone included the time series of ARM-retrieved aerosol optical depth and a three-year CCPP control simulation. This final fourth quarter milestone includes the time-series of aerosol and dust properties and a decade-long CCPP control simulation.

  7. FY 1991 environmental research programs for the DOE Field Office, Nevada: Work plan and quarterly reports, fourth quarter report

    SciTech Connect

    1991-10-01

    This research includes a wide range of research and support activities associated with the Weapons Testing Program conducted at the Nevada Test Site (NTS). Ongoing and new environmental research programs to be conducted by DRI over the period of this contract include archaeological studies, site mitigation plans, compliance activities, and historical research; offsite community radiation monitoring support; environmental compliance activities related to state and federal regulations; hydrologic assessment of containment of underground nuclear detonations; hydrology/radionuclide investigations designed to better understand and predict the possible subsurface movement of radionuclides at the NTS; and support of various statistical and data management and design, laboratory, field, and administrative activities. In addition to these, archaeological site characterization, flood hazards for rail transportation, and paleofaunal investigations will be carried out in support of the Yucca Mountain Project. Other areas of the overall program which required DRI support are classified security activities, radiation safety and training, quality assurance and control, computer protection and historical data management, review and classification of DRI documents, and preparation of any special reports, e.g., quarterly reports, not included in the requirements of the individual projects. A new set of programs funded by the Office of Technology Development will be in place by the third quarter of FY 1991. These projects will address environmental restoration and waste management concerns, among other related topics. In accordance with specific contract requirements for each activity, DRI will produce summary, status and final reports and, in some cases, journal articles which will present the results of specific research efforts. This document contains the work plan, including project descriptions, tasks, deliverables and quarterly progress reports on each project for FY 1991.

  8. BX in situ oil shale project. Quarterly technical progress report, September 1-November 30, 1981

    SciTech Connect

    Dougan, P.M.

    1981-12-20

    September 1, 1981-November 30, 1981, was the fourth consecutive quarter of superheated steam injection at the BX In Situ Oil Shale Project. During the quarter, 117,520 barrels of water as steam were injected into project injection wells at an average wellhead temperature of 715/sup 0/F and an average wellhead pressure of 1378 PSIG. During the same period, 148,516 barrels of fluid were produced from the project production wells for a produced-to-injected fluid ratio of 1.26 to 1.0. Net oil production for the quarter was 169 barrels.

  9. K-Area and Par Pond Sewage Sludge Application Sites Groundwater Monitoring Report. Fourth quarter 1992 and 1992 summary

    SciTech Connect

    Thompson, C.Y.

    1993-04-01

    During fourth quarter 1992, samples from the three monitoring wells at the K-Area site (KSS series) and the three monitoring wells at the Par Pond site (PSS series) were analyzed for constituents required by South Carolina Department of Health and Environmental Control Construction Permit 13, 173 and for other constituents as part of the Savannah River Site (SRS) Groundwater Monitoring Program. This report describes monitoring results that exceeded the final Primary Drinking Water Standards (PDWS) or the SRS flagging criteria. During fourth quarter 1992, no constituents analyzed exceeded the PDWS or the SRS Flag 2 criteria at the K-Area and Par Pond Sewage Sludge Application Sites. In the KSS well series, the field measurement for alkalinity ranged as high as 26 mg/L in well KSS 1D. Alkalinity measurements were zero in the PSS wells. Historical and current water-level elevations at the K-Area and Par Pond Sewage Sludge Application Site indicate that the groundwater flow directions are south to southwest (SRS grid coordinates).

  10. HAMS (Hypoxia, Monitoring, and Mitigation System) II Quarterly Progress Report (Technical and Financial)

    DTIC Science & Technology

    2015-04-10

    percent VO2max and heart rate). VO2max represents the functional limit of their respiratory and circulatory systems to deliver O2 to active muscles...Report (Technical and Financial) Quarterly Progress Report Technical and Financial Hypoxia, Monitoring, and Mitigation System Contract...Transmitter: options ......................................................................... 10 Figure 5: HAMS II System Block diagram

  11. UNOCAL: Parachute Creek Shale Oil Program. Environmental Monitoring Plan quarterly report. Fourth quarter 1987. Report for 1 October-31 December 1987

    SciTech Connect

    Not Available

    1988-02-29

    The Energy Security Act of 1980 established a program to provide financial assistance to private industry in the construction and operation of commercial-scale synthetic-fuels plants. The Parachute Creek Shale Oil Program is one of four projects awarded financial assistance. The support agreement included development of an Environmental Monitoring Plan, incorporating existing compliance monitoring and supplemental monitoring on water, air, solid waste, worker health and safety, and socio-economic impacts during the period 1986-1993. Phase I of this project is to produce 10,000 barrels per day of syncrude from oil shale, using the Unishale B process. During the fourth quarter, detailed analytical procedures and computer-data-management software were developed, sampling analytical and data-management standards were completed, and supplemental quality assurance and control programs were finalized. All of these activities are summarized in the report.

  12. Sanitary Landfill Groundwater Monitoring Report - Fourth Quarter 1998 and 1998 Summary

    SciTech Connect

    Chase, J.

    1999-04-09

    A maximum of fifty-three wells of the LFW series monitor groundwater quality in the Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill at the Savannah River Site (SRS). These wells are sampled quarterly to comply with the South Carolina Department of Health and Environmental Control Domestic Water permit and as part of the SRS Groundwater Monitoring Program.

  13. Radioactivity in gaseous waste discharged from the separations facilities during fourth quarter of 1979

    SciTech Connect

    Sliger, G. J.

    1980-02-22

    This document is issued quarterly for the purpose of summarizing the radioactive gaseous wastes that are discharged from the facilities of the Rockwell Hanford Operations (Rockwell). Data on alpha and beta emissions during 1979 are presented where relevant to the gaseous effluent. Emission data are not included on gaseous wastes produced within the 200 areas by other Hanford contractors.

  14. Electric and Hybrid Vehicle Program, Site Operator Program. Quarterly progress report for July through September 1994 (Fourth quarter of fiscal year 1994)

    SciTech Connect

    Kiser, D.M.; Brown, H.L.

    1995-03-01

    The Site Operator Program was initially established by the Department of Energy (DOE) to incorporate the electric vehicle activities dictated by the Electric and Hybrid Vehicle Research, Development and Demonstration Act of 1976. In the ensuing years, the Program has evolved in response to new legislation and interests. The Program currently includes twelve sites located in diverse geographic, metrologic, and metropolitan areas across the US. Information is shared reciprocally with a thirteenth site, not under Program contract. The vehicles are operator-owned, except for two Griffon vans. The Mission Statement of the Site Operator Program includes three major activities: advancement of electric vehicle technologies; development of infrastructure elements necessary to support significant electric vehicle use; and increasing the awareness and acceptance of electric vehicles (EVs) by the public. The current participants in the Site Operator Program are shown. The ultimate thrust of program activities varies among sites, reflecting not only the Operator`s business interests but also geographic and climate-related operating conditions. This fourth quarter report (FY-94) includes a summary of activities from the previous three quarters. The report section sequence has been revised to provide a more easily seen program overview, and specific operator activities are now found in Appendix A.

  15. OTEC support services. Quarterly technical progress report No. 7, 15 November 1979-14 February 1980

    SciTech Connect

    1980-02-01

    The technical engineering and management support services provided by VSE corporation for the Ocean Thermal Energy Conversion Program of the Ocean Systems Branch, Division of Central Solar Technology during this quarter are described. The seven tasks include (1) survey, analysis evaluation, and recommendation concerning program performance, (2) program technical monitoring, (3) development and implementation of methodology to identify and evaluate program alternatives, (4) technical assessments, (5) OTEC system integration, (6) environment and siting considerations; and (7) transmission subsystem considerations. (WHK)

  16. DOE KSU EV Site Operator Program. Year 1, fourth quarter report, April 1--June 30, 1992

    SciTech Connect

    Hague, J.R.; Steinert, R.A.; Nissen-Pfrang, T.

    1992-08-01

    Kansas State University, with funding from federal, state, public, and private companies, is participating in the DOE Electric Vehicle Site Operator Program. Kansas State is demonstrating, testing, and evaluating electric of hybrid vehicle technology. This will provide organizations the opportunity to examine the latest EHV prototypes under actual operating conditions. KSU proposes to purchase one (1) electric or hybrid van and four(4) electric cars during the first two years of this five-year program. KSU has purchased one G-Van built by Conceptor Industries, Toronto, Canada and has initiated a procurement order to purchase two (2) Soleq 1992 Ford EVcort station wagons. This quarter`s report describes ongoing public relations activities and meetings as well as presenting performance data for the electric vehicles. (GHH)

  17. FY 2010 Fourth Quarter Report: Evaluation of the Dependency of Drizzle Formation on Aerosol Properties

    SciTech Connect

    Lin, W; McGraw, R; Liu, Y; Wang, J; Vogelmann, A; Daum, PH

    2010-10-01

    Metric for Quarter 4: Report results of implementation of composite parameterization in single-column model (SCM) to explore the dependency of drizzle formation on aerosol properties. To better represent VOCALS conditions during a test flight, the Liu-Duam-McGraw (LDM) drizzle parameterization is implemented in the high-resolution Weather Research and Forecasting (WRF) model, as well as in the single-column Community Atmosphere Model (CAM), to explore this dependency.

  18. A Comparison of Model Short-Range Forecasts and the ARM Microbase Data Fourth Quarter ARM Science Metric

    SciTech Connect

    Hnilo, J.

    2006-09-19

    For the fourth quarter ARM metric we will make use of new liquid water data that has become available, and called the “Microbase” value added product (referred to as OBS, within the text) at three sites: the North Slope of Alaska (NSA), Tropical West Pacific (TWP) and the Southern Great Plains (SGP) and compare these observations to model forecast data. Two time periods will be analyzed March 2000 for the SGP and October 2004 for both TWP and NSA. The Microbase data have been averaged to 35 pressure levels (e.g., from 1000hPa to 100hPa at 25hPa increments) and time averaged to 3hourly data for direct comparison to our model output.

  19. CHRONICLE: Fourth Scientific and Technical Conference on Optical Methods for Flow Diagnostics

    NASA Astrophysics Data System (ADS)

    Zubov, Vladimir A.; Rinkevichius, Bronyus S.

    1997-12-01

    A review is given of the papers presented at the Fourth Scientific and Technical Conference on Optical Methods for Flow Diagnostics. This conference was concerned with research and applications in the field of flow diagnostics and with related physical and technical topics, such as determination and visualisation of optical and dynamic characteristics of media, creation and monitoring of local directional precision displacements, local measurements and determination of the spatial distribution of optical inhomogeneities in transparent media, as well as a number of practical applications of new methods and techniques.

  20. High temperature packing test program. First quarterly technical progress report, October 1-December 26, 1981

    SciTech Connect

    Not Available

    1982-02-12

    The program was undertaken to improve the technical understanding of the performance of plunger packings in coal liquefaction pilot plant feed pumps. During the first quarter of FY 1982, visits were made to the H-Coal, EDS and SRC-I pilot plants, where technical discussions were held with maintenance and engineering personnel, and the maintenance records and work orders for the plunger pumps were reviewed. Technical discussions were held with engineering personnel at the manufacturing facilities of three plunger pump manufacturers' companies. Contracts and technical discussions with packing vendors were initiated. Design of the laboratory tests was started.

  1. Study of Education Satellite Communication Demonstration. Fourth Quarterly Progress Report. Report of Activities and Accomplishments, April 11, 1975 to July 10, 1975.

    ERIC Educational Resources Information Center

    Syracuse Univ. Research Corp., NY. Educational Policy Research Center.

    A fourth quarterly report completes one year of the Educational Policy Research Center's (EPRC) analysis and assessment of the Education Satellite Communication demonstration. Activities and accomplishments during the period April 11, 1975-July 10, 1975 are listed and described. The report also includes cost data from the Appalachian Educational…

  2. Sanitary Landfill groundwater monitoring report. Fourth quarterly report and summary 1993

    SciTech Connect

    Not Available

    1994-02-01

    Fifty-seven wells of the LFW series monitor groundwater quality in Steed Pond Aquifer (Water Table) beneath the Sanitary Landfill at the Savannah River Site (SRS). These wells are sampled quarterly to comply with the South Carolina Department of Health and Environmental Control Domestic Waste Permit DWP-087A and as part of the SRS Groundwater Monitoring Program. Dichloromethane a common laboratory contaminant, and trichloroethylene were the most widespread constituents exceeding standards during 1993. Benzene, chlorobenzene, chloroethene 1,2 dichloroethane, 1,1-dichloroethylene, 1,2-dichloropropane, gross alpha, lindane, mercury, tetrachloroethylene, and tritium also exceeded standards in one or more wells. No groundwater contaminants were observed in wells screened in the lower section of Steed Pond Aquifer.

  3. High efficiency shale oil recovery. Fourth quarterly report, October 1, 1992--December 31, 1992

    SciTech Connect

    Adams, D.C.

    1992-12-31

    The overall project objective is to demonstrate the high efficiency of the Adams Counter-Current shale oil recovery process. The efficiency will first be demonstrated on a small scale, in the current phase, after which the demonstration will be extended to the operation of a small pilot plant. Thus the immediate project objective is to obtain data on oil shale retorting operations in a small batch rotary kiln that will be representative of operations in the proposed continuous process pilot plant. Although an oil shale batch sample is sealed in the batch kiln from the start until the end of the run, the process conditions for the batch are the same as the conditions that an element of oil shale would encounter in a continuous process kiln. Similar chemical and physical (heating, mixing) conditions exist in both systems. The two most important data objectives in this phase of the project are to demonstrate (1) that the heat recovery projected for this project is reasonable and (2) that an oil shale kiln will run well and not plug up due to sticking and agglomeration. The following was completed and is reported on this quarter: (1) A software routine was written to eliminate intermittently inaccurate temperature readings. (2) We completed the quartz sand calibration runs, resolving calibration questions from the 3rd quarter. (3) We also made low temperature retorting runs to identify the need for certain kiln modifications and kiln modifications were completed. (4) Heat Conductance data on two Pyrolysis runs were completed on two samples of Occidental oil shale.

  4. PFBC HGCU Test Facility. Technical progress report: Third Quarter, CY 1993

    SciTech Connect

    Not Available

    1993-10-01

    This is the sixteenth Technical Progress Report submitted to the Department of Energy (DOE) in connection with the cooperative agreement between the DOE and Ohio Power Company for the Tidd PFBC (pressurized fluidized-bed combustion) Hot Gas Clean Up Test Facility (HGCU). This report covers the period of work completed during the Third Quarter of CY 1993. During this quarter, the Advanced Particle Filter (APF) was operated for a total of 1295 hours. This represents 58% availability during July, August, September, and including June 30 of the previous quarter. The operating dates and times since initial operation are summarized. The APF operating temperatures and differential pressures are provided. Details of the APF runs during this quarter are included in this report.

  5. SRC-1 Quarterly technical report, April-June 1980

    SciTech Connect

    Not Available

    1980-01-01

    The SRC-1 quarterly report has chapters on: an evaluation of current technologies for deashing coal liquids; domestic vendors of thick-wall pressure vessels; a comparative evaluation of GKT, Texaco and Shell-Koppers gasification processes (GKT is a modification of Koppers-Totzek and is recommended for reasons given); disposal or gasification of residues; evaluation of one or two slurry feed tanks; evaluation of one or two critical solvent deashing trains; analysis of causes of corrosion in the fractionating tower (chlorides and phenols); identifying and planning for pollution control in the demonstration plant; and characterizing waste center and monitoring its treatment. (LTN)

  6. Responsive copolymers for enhanced petroleum recovery. Quarterly technical progress report, March 22, 1993--June 22, 1993

    SciTech Connect

    McCormick, C.; Hester, R.

    1993-08-01

    The overall goal of this research is the development of advanced water-soluble copolymers for use in enhanced oil recovery which rely on reversible microheterogeneous associations for mobility control and reservoir conformance. Technical progress for the quarter is summarized for the following tasks: advanced copolymer syntheses; characterization of molecular structure of copolymers; and polymer solution rheology.

  7. Regulatory and technical reports: (Abstract index journal). Compilation for first quarter 1997, January--March

    SciTech Connect

    Sheehan, M.A.

    1997-06-01

    This compilation consists of bibliographic data and abstracts for the formal regulatory and technical reports issued by the U.S. Nuclear Regulatory Commission (NRC) Staff and its contractors. This compilation is published quarterly and cummulated annually. Reports consist of staff-originated reports, NRC-sponsored conference reports, NRC contractor-prepared reports, and international agreement reports.

  8. Offshore scientific and technical publications, February-July, Spring 1989. Quarterly report

    SciTech Connect

    Not Available

    1989-01-01

    The catalog lists all current (1987-1989) scientific and technical publications of the Offshore Minerals Management Program. The catalog is updated and released on a quarterly basis in winter, spring, summer, and fall. Publications available after July 21, 1989, will be listed in the next issue.

  9. [Kelastic variable wall mining machine]. Ninth quarterly technical report, October 1, 1995--December 31, 1995

    SciTech Connect

    1995-12-31

    This is the Ninth Quarterly Technical Report of Grant Number DE-FG01-93CE15394 entitled Kelastic Variable Wall Mining Machine. This reporting period comprised a time extension which was requested and authorized by correspondence from the Department of Energy on August 9, 1995. The work described in this report was completed on the modified termination date.

  10. Mechanism for Clastogenic Activity of Naphthalene. Quarterly Technical Progress Report

    SciTech Connect

    Buchholz, B. A.

    2016-02-05

    The project has two main goals: 1) Identify the types of adducts naphthalene (NA) forms with DNA and 2) determine whether adduct formation correlates with site selective tumor formation in defined subcompartments of the respiratory tract (respiratory and olfactory nasal epithelium and airways of mice, rats and rhesus monkeys). Five tasks are associated with the completion of the goals. Task 1: Contracting and Animal Use Approvals. IACUC and ACURO approvals are complete. The subcontract with UC Davis (UCD) was executed in December 2014. Task 2: Perform In Vitro Study for Goal 1. Rat and mouse samples exposures completed. Monkey samples need to be exposed in next quarter. Task 3: Perform In Vitro Study for Goal 2. Mouse and rat ex vivo exposures completed. Monkey samples need to be completed in the next quarter. Task 4: Sample Preparation and Analysis. Mouse and Rat Goal 2 samples completed. Monkey samples remain to be done for Goal 2. Rat samples completed for Goal 1. Mouse and Monkey samples for Goal 1 need to be completed. Task 5: Data Interpretation and Reporting. Poster will be presented at 2016 Society of Toxicology Meeting. Outline for paper on adduct formation complete and similar to poster for SOT meeting.

  11. Commercialization of atom interferometers for borehole gravity gradiometry. Fourth quarterly report, July--September 1993

    SciTech Connect

    Clauser, J.F.

    1993-11-01

    The present status of tasks is: Task 1- Solution of tomography problem (completed qtrs. 1 and 2), Task 2- Study influence of vibrations (completed qtr. 3), Task 3- List of borehole imposed constraints (completed qtr.3 with update this qtr.), Task 4- Evaluate merits of various cooling schemes (completed this qtr.), Task 5- Specify magnet system requirements (completed qtr. 3), Task 6-Specify laser system (in progress), and Task 7- a. specify detector, b. specify gratings and layout, c. specify gratings and magnet spacers, d. specify vacuum system (all in progress). During this quarter, we report an update to Task 3, as well as the completion of Task 4. Work on Tasks 6 and 7 is in progress. The use of a magneto-optic trap (MOT), the choice of atomic species, state of the art for lithium MOT`s, use of lenses to increase the intensity, computerized simulation of system throughtput, and magnetic lens design are the topics addressed concerning Task 4.

  12. F-Area Seepage Basins groundwater monitoring report -- third and fourth quarters 1993. Volume 1

    SciTech Connect

    Butler, C.T.

    1994-03-01

    During the second half of 1993, the groundwater at the F-Area Seepage Basins (FASB) was monitored in compliance with Module 3, Section C, of South Carolina Hazardous Waste Permit SC1-890-008-989, effective November 2, 1992. The monitoring well network is composed of 87 FSB wells screened in the three hydrostratigraphic units that make up the uppermost aquifer beneath the FASB. A detailed description of the uppermost aquifer is included in the Resource Conservation and Recovery Act Part B post-closure care permit application for the F-Area Hazardous Waste Management Facility submitted to the South Carolina Department of Health and Environmental Control (SCDHEC) in December 1990. Beginning in the first quarter of 1993, the standard for comparison became the SCDHEC Groundwater Protection Standard (GWPS) specified in the approved F-Area Seepage Basins Part B permit. Currently and historically, gross alpha, nitrate, nonvolatile beta, and tritium are among the primary constituents to exceed standards. Numerous other radionuclides and hazardous constituents also exceeded the GWPS in the groundwater at the FASB during the second half of 1993, notably aluminum, iodine-129, and zinc. The elevated constituents are found primarily in Aquifer Zone 2B{sub 2} and Aquifer Zone 2B{sub 1} wells. However, several Aquifer Unit 2A wells also contain elevated levels of constituents. Isoconcentration/isoactivity maps included in this report indicate both the concentration/activity and extent of the primary contaminants in each of the three hydrostratigraphic units. Water-level maps indicate that the groundwater flow rates and directions at the FASB have remained relatively constant since the basins ceased to be active in 1988.

  13. H-Area Seepage Basins groundwater monitoring report -- third and fourth quarters 1993. Volume 1

    SciTech Connect

    Butler, C.T.

    1994-03-01

    During the second half of 1993, the groundwater at the H-Area Seepage Basins (HASB) was monitored in compliance with the September 30, 1992, modification of South Carolina Hazardous Waste Permit SC1-890-008-989. A detailed description of the uppermost aquifer is included in the Resource Conservation and Recovery Act Part B post-closure care permit application for the H-Area Hazardous Waste Management Facility submitted to the South Carolina Department of Health and Environmental Control (SCDHEC) in December 1990. Beginning first quarter 1993, the HASB`s Groundwater Protection Standard (GWPS), established in Appendix 3D-A of the cited permit, became the standard for comparison. Historically as well as currently, nitrate, nonvolatile beta, and tritium have been among the primary constituents to exceed standards. Other radionuclides and hazardous constitutents also exceeded the GWPS in the groundwater at the HASB (notably aluminum, iodine-129, strontium-90, technetium-99, and zinc) during the second half of 1993. Elevated constituents were found primarily in Aquifer Zone 2B{sub 2} and in the upper portion of Aquifer Zone 2B{sub 1}. However, constituents exceeding standards also occurred in several wells screened in the lower portion of Aquifer Zone 2B{sub 1} and Aquifer Unit 2A. Isoconcentration/isoactivity maps include in this report indicate both the concentration/activity and extent of the primary contaminants in each of the three hydrostratigraphic units during the second half of 1993. Water-level maps indicate that the groundwater flow rates and directions at the HASB have remained relatively constant since the basins ceased to be active in 1988.

  14. Oil Bypass Filter Technology Evaluation, Fourth Quarterly Report, July--September 2003

    SciTech Connect

    James E. Francfort; Larry Zirker

    2003-11-01

    This fourth Oil Bypass Filter Technology Evaluation report details the ongoing fleet evaluation of an oil bypass filter technology by the Idaho National Engineering and Environmental Laboratory (INEEL) for the U.S. Department of Energy’s FreedomCAR & Vehicle Technologies Program. Eight four-cycle diesel-engine buses used to transport INEEL employees on various routes have been equipped with oil bypass filter systems from the puraDYN Corporation. The bypass filters are reported to have engine oil filtering capability of <1 micron and a built-in additive package to facilitate extended oil-drain intervals. To date, the eight buses have accumulated 259,398 test miles. This represents an avoidance of 21 oil changes, which equates to 740 quarts (185 gallons) of oil not used or disposed of. To validate the extended oil-drain intervals, an oil-analysis regime evaluates the fitness of the oil for continued service by monitoring the presence of necessary additives, undesirable contaminants, and engine-wear metals. For bus 73450, higher values of iron have been reported, but the wear rate ratio (parts per million of iron per thousand miles driven) has remained consistent. In anticipation of also evaluating oil bypass systems on six Chevrolet Tahoe sport utility vehicles, the oil is being sampled on each of the Tahoes to develop a characterization history or baseline for each engine.

  15. Los Alamos National Laboratory Environmental Restoration Project quarterly technical report, April--June 1994

    SciTech Connect

    Not Available

    1994-08-18

    This quarterly report describes the technical status of activities in the Los Alamos National Laboratory Environmental Restoration (ER) Project. Each activity is identified by an activity data sheet number, a brief title describing the activity or the technical area where the activity is located, and the name of the project leader. The Hazardous and Solid Waste Amendments (HSWA) portion of the facility operating permit requires the submission of a technical progress report on a quarterly basis. This report, submitted to fulfill the permit`s requirement, summarizes the work performed and the results of sampling and analysis in the ER Project. Suspect waste found include: Radionuclides, high explosives, metals, solvents and organics. The data provided in this report have not been validated. These data are considered ``reviewed data.``

  16. Northeast Regional Biomass Program. Ninth year, Fourth quarterly report, July--September 1992

    SciTech Connect

    Lusk, P.D.

    1992-12-01

    The Northeast Regional Biomass Program has been in operation for a period of nine years. During this time, state managed programs and technical programs have been conducted covering a wide range of activities primarily aim at the use and applications of wood as a fuel. These activities include: assessments of available biomass resources; surveys to determine what industries, businesses, institutions, and utility companies use wood and wood waste for fuel; and workshops, seminars, and demonstrations to provide technical assistance. In the Northeast, an estimated 6.2 million tons of wood are used in the commercial and industrial sector, where 12.5 million cords are used for residential heating annually. Of this useage, 1504.7 mw of power has been generated from biomass. The use of wood energy products has had substantial employment and income benefits in the region. Although wood and woodwaste have received primary emphasis in the regional program, the use of municipal solid waste has received increased emphasis as an energy source. The energy contribution of biomass will increase as potentia users become more familiar with existing feedstocks, technologies, and applications. The Northeast Regional Biomass Program is designed to support region-specific to overcome near-term barriers to biomass energy use.

  17. Advanced direct liquefaction concepts for PETC generic units. Quarterly technical progress report, July 1992--September 1992

    SciTech Connect

    Not Available

    1992-11-01

    Preparation of the baseline economic assessment, based on Wilsonville Run {number_sign}263J, continued. This baseline study will serve as the reference against which the results of this program will be compared. During the quarter calculation of the material and energy balances for the conceptual commercial plant were completed and estimation of the investment for the main process units was begun (Wyoming plant site basis). A presentation on the technical results of the baseline study was prepared and delivered at the Quarterly Project Review Meeting in Pittsburgh.

  18. Project DEEP STEAM: fourth meeting of the technical advisory panel, Albuquerque, NM, November 1980

    SciTech Connect

    Fox, R.L.; Donaldson, A.B.; Eisenhawer, S.W.; Hart, C.M.; Johnson, D.R.; Mulac, A.J.; Wayland, J.R.; Weirick, L.J.

    1981-07-01

    The Fourth Project DEEP STEAM Technical Advisory Panel Meeting was held on 5 and 6 November 1980 in Albuquerque, New Mexico, to review the status of project DEEP STEAM. This Proceedings, following the order of the meeting, is divided into five main sections: the injection string modification program, the downhole steam generator program, supporting activities, field testing, and the Advisory Panel recommendations and discussion. Each of the 17 presentations is summarized, and a final Discussion section has been added, when needed, for inclusion of comments and replies related to specific presentations. Finally, the Advisory Panel recommendations and the ensuing discussion are summarized in the closing section.

  19. Large-area silicon sheet by EFG. Fourth quarterly report, October 1-December 31, 1980

    SciTech Connect

    Not Available

    1981-02-17

    Extensive characterization of the multiple ribbon Furnace 3A main zone temperature profile has been performed and the information used to improve uniformity of heating. Irregularities in the main zone heater have been associated with growth difficulties at specific cartridge locations, and growth conditions subsequently improved by profiling the main zone heater. This work has resulted in good growth conditions being established in all three cartridge positions. These improvements have allowed multiple growth of three 10 cm wide ribbons to be demonstrated for periods of an hour on several occasions. A full eight-hour technical features demonstration run has not been achieved due to malfunctions in auxiliary equipment. A new gas distribution system for the 10 cm cartridge has been introduced and demonstrated to lead to improved ambient control during growth. Growth without and with CO/sub 2/ has shown that quality improvement in 10 cm ribbon grown with cold shoes results from ambient manipulation. Optimization of this process is continuing with studies of different means by which to vary oxygen levels in the ribbon.

  20. Yucca Mountain Site Characterization Project: Technical data catalog,(quarterly supplement)

    SciTech Connect

    1993-03-31

    The June 1, 1985, Department of Energy (DOE)/Nuclear Regulatory Commission (NRC) Site-Specific Procedural Agreement for Geologic Repository Site Investigation and Characterization Program requires the DOE to develop and maintain a catalog of data which will be updated and provided to the NRC at least quarterly. This catalog is to include a description of the data; the time (date), place, and method of acquisition; and where it may be examined. The Yucca Mountain Site Characterization Project (YMP) Technical Data Catalog is published and distributed in accordance with the requirements of the Site-Specific Agreement. The YMP Technical Data Catalog is a report based on reference information contained in the YMP Automated Technical Data Tracking System (ATDT). The reference information is provided by Participants for data acquired or developed in support of the YMP. The Technical Data Catalog is updated quarterly and published in the month following the end of each quarter. A complete revision to the Catalog is published at the end of each fiscal year.

  1. Quarterly technical progress report, February 1, 1996--April 30, 1996

    SciTech Connect

    1996-05-28

    This report from the Amarillo National REsource Center for PLutonium provides research highlights and provides information regarding the public dissemination of information. The center is a a scientific resource for information regarding the issues of the storage, disposition, potential utilization and transport of plutonium, high explosives, and other hazardous materials generated from nuclear weapons dismantlement. The center responds to informational needs and interpretation of technical and scientific data raised by interested parties and advisory groups. Also, research efforts are carried out on remedial action programs and biological/agricultural studies.

  2. DOE Safety Metrics Indicator Program (SMIP) Fiscal Year 2001 Fourth Quarter Report of Packaging- and Transportation-related Occurrences

    SciTech Connect

    Dickerson, L.S.

    2001-11-30

    The Safety Metrics Indicator Program (SMIP) retrieved 44 packaging- or transportation-related occurrences from the Occurrence Reporting and Processing System (ORPS) during the period from July 1 through September 30, 2001. Only those incidents that occur in preparation for transport, during transport, and during unloading of hazardous material are considered as packaging- or transportation-related occurrences. Other incidents with packaging and transportation (P and T) significance but not involving hazardous material (such as vehicle accidents or empty packagings) are not rated to the SMIP criteria, but are archived in the SMIP Subsidiary Database of occurrences, a sub-database of the main SMIP P and T Occurrence Database. Thirty-two of the originally-selected 44 occurrences were appropriate for classification to the SMIP criteria, only 7 of which have offsite applicability. Eight of the original 44 reports are archived in a subsidiary database because they either do not involve the transport of hazardous material or do not involve transport by vehicle, plane, boat, or rail. The others either were deleted because more thorough review revealed that they were not strictly related to P and T or were canceled by the reporting site and removed from the ORPS. These occurrences have not been normalized as in the Annual Report of Occurrences because the necessary information is not yet available. The number and severity of the selected occurrence reports (ORs) are consistent with historical reporting. Contamination events continue to be among the most common type of occurrences; however, ''Shipping Preparation'' events decreased this quarter to only 4 events from the 21 reported last quarter. None of the 32 ORs that were rated had event consequence measures (W{sub EC}) greater than 2; 14 of them were categorized as having a W{sub EC} of 1. This means that all of the fourth-quarter FY 2001 ORs had only slight consequences at worst (i.e., resulting in minimal safety

  3. Quarter-sweep Gauss-Seidel method with quadratic spline scheme applied to fourth order two-point boundary value problems

    NASA Astrophysics Data System (ADS)

    Mohd Fauzi, Norizyan Izzati; Sulaiman, Jumat

    2013-04-01

    The aim of this paper is to describe the application of Quarter-Sweep Gauss-Seidel (QSGS) iterative method using quadratic spline scheme for solving fourth order two-point linear boundary value problems. In the line to derive approximation equations, firstly the fourth order problems need to be reduced onto a system of second-order two-point boundary value problems. Then two linear systems have been constructed via discretization process by using the corresponding quarter-sweep quadratic spline approximation equations. The generated linear systems have been solved using the proposed QSGS iterative method to show the superiority over Full-Sweep Gauss-Seidel (FSGS) and Half-Sweep Gauss-Seidel (HSGS) methods. Computational results are provided to illustrate that the effectiveness of the proposed QSGS method is more superior in terms of computational time and number of iterations as compared to other tested methods.

  4. FETC/EPRI Biomass Cofiring Cooperative Agreement. Quarterly technical report, July 1-September 30, 1997

    SciTech Connect

    Hughes, E.; Tillman, D.

    1997-12-01

    The FETC/EPRI Biomass Cofiring Program has completed one year of activity, accelerating the pace of cofiring development. Cofiring tests were completed at the Seward Generating Station of GPU Genco and at the Michigan City Generating Station of NIPSCO. The NYSEG work at Greenidge Station resulted in a workable, low cost method for injecting biofuels into coal-fired PC boilers. Support studies and modeling continued to provide analytics for the cofiring program. This report summarizes the activities during the fourth quarter of the FETC/EPRI Biomass Cofiring Cooperative Agreement. It focuses upon the results of testing in order to highlight the progress at utilities.

  5. Nucla circulating atmospheric fluidized bed demonstration project. Quarterly technical progress report, October--December 1990

    SciTech Connect

    Not Available

    1991-01-31

    During the fourth quarter of 1990, steady-state performance testing at the Nucla Circulating Fluidized Bed (CFB) resumed under sponsorship of the US Department of Energy. Co-sponsorship of the Demonstration Test Program by the Electric Power Research Institute (EPRI) was completed on June 15, 1990. From October through December, 1990, Colorado-Ute Electric Association (CUEA) completed a total of 23 steady-state performance tests, 4 dynamic tests, and set operating records during November and December as the result of improved unit operating reliability. Highlight events and achievements during this period of operation are presented.

  6. Nuclear magnetic resonance studies of granular flows: Technical progress report, quarter ending 09/30/93

    SciTech Connect

    Not Available

    1993-10-27

    This Technical Progress Report for the quarter ending 09/30/93 describes work on two tasks which are part of nuclear magnetic resonance studies of granular flows. (1) Research has been directed toward improving concentration measurements under reasonably fast conditions. (2) The process continues of obtaining comprehensive velocity, concentration, and diffusion information at several angular velocities of the cylinder for seeds (mustard, sesame, and sunflower seeds) flowing in a half-filled cylinder.

  7. Technical data base quarterly report, April--June 1992; Yucca Mountain Site Characterization Project

    SciTech Connect

    1992-09-01

    The acquisition and development of technical data are activities that provide the information base from which the Yucca mountain Site will be characterized and may P-ventually be licensed as a high-level waste repository. The Project Technical Data Base (TDB) is the repository for the regional and site-specific technical data required in intermediate and license application analyses and models. The TDB Quarterly Report provides the mechanism for identifying technical data currently available from the Project TDB. Due to the variety of scientific information generated by YMP activities, the Project TDB consists of three components, each designed to store specific types of data. The Site and Engineering Properties Data Base (SEPDB) maintains technical data best stored in a tabular format. The Geographic Nodal Information Study and Evaluation System (GENISES), which is the Geographic Information System (GIS) component of the Project TDB, maintains spatial or map-like data. The Geologic and Engineering Materials Bibliography of Chemical Species (GEMBOCHS) data base maintains thermodynamic/geochemical data needed to support geochemical reaction models involving the waste package and repository geochemical environment. Each of these data bases are addressed independently within the TDB Quarterly Report.

  8. Objective structured assessment of technical skills for repair of fourth-degree perineal lacerations.

    PubMed

    Siddiqui, Nazema Y; Stepp, Kevin J; Lasch, Susan J; Mangel, Jeffrey M; Wu, Jennifer M

    2008-12-01

    The objective of this study was to assess the reliability and validity of an objective structured assessment of technical skills (OSATS) for repair of fourth-degree obstetric lacerations on a surgical model. Three blinded judges reviewed recordings of 20 junior and 20 senior obstetrics-gynecology residents performing simulated perineal repairs using a beef tongue model. Judges completed task-specific OSATS and global rating scales for each repair. Six recordings were rereviewed after 2 weeks. Inter- and intrarater reliability and construct validity were assessed. Interrater reliability was 0.80 for task-specific OSATS and 0.59 for the global rating scale. Intrarater reliability was poor. Construct validity was demonstrated, with senior residents scoring higher than junior residents on task-specific OSATS (13.0 vs 10.5; P = .007) and the global rating scale (24.0 vs 19.3; P = .001). We found good interrater reliability and construct validity using a task-specific OSATS for fourth-degree perineal laceration repair. This instrument shows promise as a tool for competency-based evaluations.

  9. West Hackberry Tertiary Project. Quarterly technical progress report, January 1, 1996--March 31, 1996

    SciTech Connect

    Gillham, T.; Cerveny, B.; Turek, E.

    1996-04-10

    The goal of the West Hackberry Tertiary Project is to demonstrate the technical and economic feasibility of combining air injection with the Double Displacement Process for tertiary oil recovery. The Double Displacement Process is the gas displacement of a water invaded oil column for the purpose of recovering oil through gravity drainage. The novel aspect of this project is the use of air as the injection fluid. The target reservoir for the project is the Camerina C-1,2,3 sand located on the West Flank of West Hackberry Field in Cameron Parish, Louisiana. If successful, this project will demonstrate that the use of air injection in the Double Displacement Process can economically recover oil in reservoirs where tertiary oil recovery is presently uneconomic. The first quarter of 1996 was outstanding both in terms of volume of air injected and low cost operations. More air was injected during this quarter than in any preceding quarter. The compressors experienced much improved run time with minimal repairs. Low operating costs resulted from no repairs required for injection or production wells. A discussion of the following topics are contained herein: (1) performance summary for the injection and production wells, (2) air compressor operations, (3) updated bottom hole pressure data, (4) technology transfer activities and (5) plans for the upcoming quarter.

  10. Great Plains Coal Gasification Project: Quarterly technical progress report, April-June 1988 (Fourth fiscal quarter, 1987-1988)

    SciTech Connect

    Not Available

    1988-07-29

    This progress report describes the operation of the Great Plains Gasification Plant, including lignite coal production, SNG production, gas quality, by-products, and certain problems encountered. (LTN)

  11. Great Basin paleoenvironmental studies project; Technical progress report: Fourth quarter, March--May, 1994

    SciTech Connect

    1994-07-01

    Examination of the paleoenvironmental and geomorphic records to determine the local and regional impact of past climates will advance the assessment of Yucca Mountain`s suitability as a high-level nuclear waste repository. Paleobotanical studies will reconstruct the response of vegetation to climate change at the community and the organismal levels in order to identify periods of mesic climate at Yucca Mountain and the adjacent region during the last 20,000 to 50,000 years. Constructing a history of Great Basin vertebrates, particularly mammals, will provide empirical evidence of past environmental and climatic conditions within the Great Basin. The objective of the geomorphology component of the program is to document the responses of surficial processes and landforms to the climatic changes documented by studies of packrat middens, pollens, and faunal distributions. The goal of the transportation component is to compare the results from three models (FESWMS-2DH, DAMBRK, and FLO-2D) that have been suggested as appropriate for evaluating flood flows on alluvial fans with the results obtained from the traditional one-dimensional, stochastic model used in previous research for the Yucca Mountain Project. Progress on all these tasks is described.

  12. Air Force Office of Scientific Research (AFOSR). Technical Report Summaries. Fourth Quarter (CY).

    DTIC Science & Technology

    1985-01-01

    CLSI U Sli l I ., , l. - u ,-..,eU,- LS -W* , t . L- L -C Ub-S4i L-* - SE 4m c IL. a~ c.xr aui 4. - 61L hI. ,. O -0 O • ini inI. #1. 7t . 4 . U in .4 I...4o aUa . 0 In I I. L a C24 4’ L. a.I hi v. 0. 2 0 v O= r 0- 0 lz 0 02S - AL) ul I.- ow- ffv ;- 65 low L. U. W * Lb.U4. 4.IL -4 m C 2 4 ant bo an NA 4

  13. Heber geothermal binary demonstration project quarterly technical progress report, July 1, 1981--September 30, 1981

    SciTech Connect

    Lacy, R.G.; Allen, R.F.; Alsup, R.A.; Liparidis, G.S.; Van De Mark, G.D.

    1983-08-01

    The purpose of this quarterly technical progress report is to document work completed on the nominal 65 Megawatt (Mwe gross) Heber Geothermal Binary Demonstration Project, located at Heber, California, during the period of July 1, 1981, through September 30, 1981. The work was performed by San Diego Gas and Electric Company under the support and cooperation of the US Department of Energy, the Electric Power Research Institute, the Imperial Irrigation District, the California Department of Water Resources, and the Southern California Edison Company. Topics covered in this quarterly report include progress made in the areas of Wells and Fluid production and Injection Systems, Power Plant Design and Construction, Power Plant Demonstration, and Data Acquisition and Dissemination.

  14. Power systems development facility. Quarterly technical progress report, January 1, 1994--March 31, 1994

    SciTech Connect

    Not Available

    1994-07-01

    This quarterly technical progress report summarizes work completed during the last quarter of the Second Budget Period, January 1 through March 31, 1994, entitled {open_quotes}Hot Gas Cleanup Test Facility for Gasification and Pressurized Combustion.{close_quotes} The objective of this project is to evaluate hot gas particulate control technologies using coal-derived gas streams. This will entail the design, construction, installation, and use of a flexible test facility which can operate under realistic gasification and combustion conditions. The major particulate control device issues to be addressed include the integration of the particulate control devices into coal utilization systems, on-line cleaning techniques, chemical and thermal degradation of components, fatigue or structural failures, blinding, collection efficiency as a function of particle size, and scale-up of particulate control systems to commercial size.

  15. Heber geothermal binary demonstration project quarterly technical progress report, October 1, 1982--December 31, 1982

    SciTech Connect

    Lacy, R.G.; Allen, R.F.; Dixon, J.R.; Hsiao, W.P.; Liparidis, G.S.; Lombard, G.L.; Nelson, T.T.; Van De Mark, G.D.

    1983-05-01

    The purpose of this quarterly technical progress report is to document work completed on the nominal 65 Megawatt (Mwe gross) Heber Geothermal Binary Demonstration Project, located at Heber, California, during the period of October 1, 1982--December 31, 1982. The work was performed by San Diego Gas and Electric Company under the support and cooperation of the U.S. Department of Energy, the Electric Power Research Institute, the Imperial Irrigation District, the California Department of Water Resources, and the Southern California Edison Company. Topics covered in this quarterly report include progress made in the areas of Wells and Fluid Production and Injection Systems, Power Plant Design and Construction, Power Plant Demonstration, and Data Acquisition and Dissemination.

  16. PFBC HGCU test facility technical progress report. First Quarter, CY 1994

    SciTech Connect

    Not Available

    1994-04-01

    This is the eighteenth Technical Progress Report submitted in connection with the cooperative agreement between the DOE and Ohio Power Company for the Tidd PFBC Hot Gas Clean Up Test Facility. During this quarter, the Tidd Hot Gas Clean Up System operated for 835 hours during six separate test runs. The system was starting into a seventh run at the end of the quarter. Highlights of this period are summarized below: the longest run during the quarter was approximately 333 hours; filter pressure drop was stable during all test runs this quarter using spoiling air to the primary cyclone upstream of the Advanced Particle Filter (APF); the tempering air system was commissioned this quarter which enabled the unit to operate at full load conditions while limiting the gas temperature in the APF to 1,400 F; during a portion of the one run, the tempering air was removed and the filter operated without problems up to 1,450 F; ash sampling was performed by Battelle personnel upstream and downstream of the APF and ash loading and particle size distribution data were obtained, a summary report is included; a hot area on the APF head was successfully repaired in service; a hot spot on the top of an expansion joint was successfully repaired by drilling holes from the inside of the pipe and pumping in refractory insulation; a corrosion inspection program for the HGCU system was issued giving recommendations for points to inspect; filter internal inspections following test runs 13 and 17 revealed a light coating (up to 1/4 inch thick) of residual ash on the candles and some ash bridging between the dust sheds and inner rows of candles. Data from these inspections are included with this report.

  17. Decontamination Systems Information and Research Program. Quarterly technical progress report, January 1--March 31, 1994

    SciTech Connect

    Not Available

    1994-05-01

    West Virginia University (WVU) and the US DOE Morgantown Energy Technology Center (METC) entered into a Cooperative Agreement on August 29, 1992 entitled ``Decontamination Systems Information and Research Programs.`` Stipulated within the Agreement is the requirement that WVU submit to METC a series of Technical Progress Reports on a quarterly basis. This report comprises the first Quarterly Technical Progress Report for Year 2 of the Agreement. This report reflects the progress and/or efforts performed on the sixteen (16) technical projects encompassed by the Year 2 Agreement for the period of January 1 through March 31, 1994. In situ bioremediation of chlorinated organic solvents; Microbial enrichment for enhancing in-situ biodegradation of hazardous organic wastes; Treatment of volatile organic compounds (VOCs) using biofilters; Drain-enhanced soil flushing (DESF) for organic contaminants removal; Chemical destruction of chlorinated organic compounds; Remediation of hazardous sites with steam reforming; Soil decontamination with a packed flotation column; Use of granular activated carbon columns for the simultaneous removal of organics, heavy metals, and radionuclides; Monolayer and multilayer self-assembled polyion films for gas-phase chemical sensors; Compact mercuric iodide detector technology development; Evaluation of IR and mass spectrometric techniques for on-site monitoring of volatile organic compounds; A systematic database of the state of hazardous waste clean-up technologies; Dust control methods for insitu nuclear and hazardous waste handling; Winfield Lock and Dam remediation; and Socio-economic assessment of alternative environmental restoration technologies.

  18. Instructor's Manual for Electrical Apprentice Technical Training. Series No. D (Fourth Year). Revised to Meet 1978 Electrical Code.

    ERIC Educational Resources Information Center

    North Carolina State Dept. of Community Colleges, Raleigh.

    Twenty-seven lesson plans for a fourth-year electrical apprentice technical training program are presented in this instructor's manual. Also included are student worksheets and information sheets for each lesson, and copies of unit tests. (Answers to the worksheets and tests are provided.) The lesson plans are generally organized into four steps:…

  19. Related Instructional Material for Electrical Apprentice Technical Training. Student Worksheets. Series D (Fourth Year). Revised to Meet 1978 Electrical Code.

    ERIC Educational Resources Information Center

    North Carolina State Dept. of Community Colleges, Raleigh.

    Information sheets and student worksheets for twenty-seven lesson plans designed for a fourth-year electrical apprentice technical training program are presented in this workbook. The information sheets provide summary information about the lesson topics and the worksheets contain problems to be solved and questions to be answered relating to each…

  20. Related Instructional Material for Electrical Apprentice Technical Training. Student Worksheets. Series D (Fourth Year). Revised to Meet 1978 Electrical Code.

    ERIC Educational Resources Information Center

    North Carolina State Dept. of Community Colleges, Raleigh.

    Information sheets and student worksheets for twenty-seven lesson plans designed for a fourth-year electrical apprentice technical training program are presented in this workbook. The information sheets provide summary information about the lesson topics and the worksheets contain problems to be solved and questions to be answered relating to each…

  1. Instructor's Manual for Electrical Apprentice Technical Training. Series No. D (Fourth Year). Revised to Meet 1978 Electrical Code.

    ERIC Educational Resources Information Center

    North Carolina State Dept. of Community Colleges, Raleigh.

    Twenty-seven lesson plans for a fourth-year electrical apprentice technical training program are presented in this instructor's manual. Also included are student worksheets and information sheets for each lesson, and copies of unit tests. (Answers to the worksheets and tests are provided.) The lesson plans are generally organized into four steps:…

  2. MHD Integrated Topping Cycle Project. Eighteenth quarterly technical progress report, November 1, 1991--January 31, 1992

    SciTech Connect

    Not Available

    1992-07-01

    This eighteenth quarterly technical progress report of the MHD Integrated Topping cycle Project presents the accomplishments during the period November 1, 1991 to January 31, 1992. The precombustor is fully assembled. Manufacturing of all slagging stage components has been completed. All cooling panels were welded in place and the panel/shell gap was filled with RTV. Final combustor assembly is in progress. The low pressure cooling subsystem (LPCS) was delivered to the CDIF. Second stage brazing issues were resolved. The construction of the two anode power cabinets was completed.

  3. Mild coal pretreatment to improve liquefaction reactivity. Quarterly technical progress report, June--August 1991

    SciTech Connect

    Miller, R.L.

    1991-12-31

    This report describes work completed during the fourth quarter of a three year project to study the effects of mild chemical pretreatment on coal dissolution reactivity during low severity liquefaction or coal/oil coprocessing. The overall objective of this research is to elucidate changes in the chemical and physical structure of coal by pretreating with methanol or other simple organic solvent and a trace amount of hydrochloric acid and measure the influence of these changes on coal dissolution reactivity. This work is part of a larger effort to develop a new coal liquefaction or coal/oil coprocessing scheme consisting of three main process steps: (1) mile pretreatment of the feed coal to enhance dissolution reactivity and dry the coal, (2) low severity thermal dissolution of the pretreated coal to obtain a very reactive coal-derived residual material amenable to upgrading, and (3) catalytic upgrading of the residual products to distillate liquids.

  4. PFBC HGCU Test Facility technical progress report second quarter, CY 1994

    SciTech Connect

    Mudd, M.J.

    1994-07-01

    This is the nineteenth Technical Progress Report submitted to the Department of Energy (DOE) in connection with the cooperative agreement between the DOE and Ohio Power Company for the Tidd PFBC Hot Gas Clean Up Test Facility. During this quarter, the Tidd Hot Gas Clean Up System operated for 444 continuous hours (including 15 hours at the end of the first quarter) during Test Run 18. The system was shut down on April 18, 1994, and remained out of service for the remainder of the quarter. Highlights of this period are summarized below: operated HGCU for 444 continuous hours which was the longest run so far in 1994; completed Hazardous Air Pollutant testing; inspected Advanced Particle Filter (APF) following testing and found 28 broken filter candles; cleaned and reassembled the APF without the inner rows of candles in the upper and middle plenums since ash bridging between these candles and the center support pipe caused the candle failures; installed 30 new filter candles of different materials for testing in the APF; and installed additional air piping and valves to permit the primary cyclone to be totally spoiled in service and thereby direct all of the ash into the filter.

  5. 76 FR 17951 - Notice of Regulatory Waiver Requests Granted for the Fourth Quarter of Calendar Year 2010

    Federal Register 2010, 2011, 2012, 2013, 2014

    2011-03-31

    ...Section 106 of the Department of Housing and Urban Development Reform Act of 1989 (the HUD Reform Act) requires HUD to publish quarterly Federal Register notices of all regulatory waivers that HUD has approved. Each notice covers the quarterly period since the previous Federal Register notice. The purpose of this notice is to comply with the requirements of section 106 of the HUD Reform Act.......

  6. Projects at the Component Development and Integration Facility. Quarterly technical progress report, July 1--September 30, 1993

    SciTech Connect

    Not Available

    1993-12-31

    This quarterly technical progress report presents progress on the projects at the Component Development and Integration Facility (CDIF) during the first quarter of FY94. The CDIF is a major US Department of Energy test facility in Butte, Montana, operated by MSE, Inc. Projects in progress include: MHD Proof-of-Concept project; mine waste technology pilot program; plasma projects; resource recovery project; sodium sulfide/ferrous sulfate project; soil washing project; and spray casting project.

  7. Projects at the Component Development and Integration Facility. Quarterly technical progress report, April 1--June 30, 1993

    SciTech Connect

    Not Available

    1993-12-01

    This quarterly technical progress report presents progress on the projects at the Component Development and Integration Facility (CDIF) during the third quarter of FY93. The CDIF is a major US Department of Energy test facility in Butte, Montana, operated by MSE, Inc. Projects in progress include: MHD Proof-of-Concept Project; Mine Waste Technology Program; Plasma Projects; Resource Recovery Project; Sodium Sulfide/Ferrous Sulfate Project; Soil Washing Project; and Spray Casting Project.

  8. Projects at the Component Development and Integration Facility. Quarterly technical progress report, January 1, 1994--March 31, 1994

    SciTech Connect

    Not Available

    1994-08-01

    This quarterly technical progress report presents progress on the projects at the Component Development and Integration Facility (CDIF) during the second quarter of FY94. The CDIF is a major US Department of Energy test facility in Butte, Montana, operated by MSE, Inc. Projects in progress include: Biomass Remediation Project; Heavy Metal-Contaminated Soil Project; MHD Shutdown; Mine Waste Technology Pilot Program; Plasma Projects; Resource Recovery Project; Sodium Sulfide/Ferrous Sulfate Project; and Spray Casting Project.

  9. Projects at the Component Development and Integration Facility. Quarterly technical progress report, October 1--December 31, 1992

    SciTech Connect

    Not Available

    1992-12-31

    This quarterly technical progress report presents progress on the projects at the component Development and Integration Facility (CDIF) during the first quarter of FY93. The CDIF is a major US Department of Energy (DOE) test facility in Butte, Montana, operated by MSE, Inc. Projects in progress include: MHD proof-of-concept project; mine waste pilot program; plasma projects; resource recovery project; sodium sulfide/ferrous sulfate project; soil washing project; and spray casting project.

  10. Predictive Engineering Tools for Injection-Molded Long-Carbon-Fiber Thermoplastic Composites - Fourth FY 2015 Quarterly Report

    SciTech Connect

    Nguyen, Ba Nghiep; Fifield, Leonard S.; Wollan, Eric J.; Roland, Dale; Gandhi, Umesh N.; Mori, Steven; Lambert, Gregory; Baird, Donald G.; Wang, Jin; Costa, Franco; Tucker III, Charles L.

    2015-11-13

    During the last quarter of FY 2015, the following technical progress has been made toward project milestones: 1) PlastiComp used the PlastiComp direct in-line (D-LFT) Pushtrusion system to injection mold 40 30wt% LCF/PP parts with ribs, 40 30wt% LCF/PP parts without ribs, 10 30wt% LCF/PA66 parts with ribs, and 35 30wt% LCF/PA66 parts without ribs. In addition, purge materials from the injection molding nozzle were obtained for fiber length analysis, and molding parameters were sent to PNNL for process modeling. 2) Magna cut samples at four selected locations (named A, B, C and D) from the non-ribbed Magna-molded parts based on a plan discussed with PNNL and the team and shipped these samples to Virginia Tech for fiber orientation and length measurements. 3) Virginia Tech started fiber orientation and length measurements for the samples taken from the complex parts using Virginia Tech’s established procedure. 4) PNNL and Autodesk built ASMI models for the complex parts with and without ribs, reviewed process datasheets and performed preliminary analyses of these complex parts using the actual molding parameters received from Magna and PlastiComp to compare predicted to experimental mold filling patterns. 5) Autodesk assisted PNNL in developing the workflow to use Moldflow fiber orientation and length results in ABAQUS® simulations. 6) Autodesk advised the team on the practicality and difficulty of material viscosity characterization from the D-LFT process. 7) PNNL developed a procedure to import fiber orientation and length results from a 3D ASMI analysis to a 3D ABAQUS® model for structural analyses of the complex part for later weight reduction study. 8) In discussion with PNNL and Magna, Toyota developed mechanical test setups and built fixtures for three-point bending and torsion tests of the complex parts. 9) Toyota built a finite element model for the complex parts subjected to torsion loading. 10) PNNL built the 3D ABAQUS® model of the complex ribbed

  11. Predictive Engineering Tools for Injection-Molded Long-Carbon-Fiber Thermoplastic Composites - FY 2014 Fourth Quarterly Report

    SciTech Connect

    Nguyen, Ba Nghiep; Fifield, Leonard S.; Mathur, Raj N.; Kijewski, Seth A.; Sangid, Michael D.; Wang, Jin; Jin, Xiaoshi; Costa, Franco; Gandhi, Umesh N.; Mori, Steven; Tucker, III, Charles L.

    2014-09-30

    During the last quarter of FY 2014, the following technical progress has been made toward project milestones: 1) Autodesk, Inc. (Autodesk) has implemented a new fiber length distribution (FLD) model based on an unbreakable length assumption with Reduced Order Modeling (ROM) by the Proper Orthogonal Decomposition (POD) approach in the mid-plane, dual-domain and 3D solvers. 2) Autodesk improved the ASMI 3D solver for fiber orientation prediction using the anisotropic rotary diffusion (ARD) – reduced strain closure (RSC) model. 3) Autodesk received consultant services from Prof. C.L. Tucker at the University of Illinois on numerical simulation of fiber orientation and fiber length. 4) PlastiComp, Inc. (PlastiComp) suggested to Purdue University a procedure for fiber separation using an inert-gas atmosphere in the burn-off furnace. 5) Purdue University (Purdue) hosted a face-to-face project review meeting at Purdue University on August 6-7, 2014. 6) Purdue conducted fiber orientation measurements for 3 PlastiComp plaques: fast-fill 30wt% LCF/PP edged-gated, slow-fill 50wt% LCF/PP edge-gated, and slow-fill 50wt% LCF/PP center-gated plaques, and delivered the orientation data for these plaques at the selected locations (named A, B, and C) to PNNL. 7) PNNL conducted ASMI mid-plane analyses for the above PlastiComp plaques and compared the predicted fiber orientations with the measured data provided by Purdue at Locations A, B, and C on these plaques. 8) PNNL planned the project review meeting (August 6-7, 2014) with Purdue. 9) PNNL performed ASMI analyses for the Toyota complex parts with and without ribs, having different wall thicknesses, and using the PlastiComp 50wt% LCF/PP, 50wt% LCF/PA66, 30wt% LCF/PP, and 30wt% LCF/PA66 materials to provide guidance for tool design and modifications needed for molding these parts. 10) Magna Exteriors and Interiors Corp. (Magna) molded plaques from the 50% LCF/PP and 50% LCF/PA66 materials received from Plasticomp in order to

  12. Unocal Parachute Creek Shale Oil Program. Environmental Monitoring Plan quarterly report. Fourth quarter, 1989. Rept. for 1 Oct-31 Dec 89

    SciTech Connect

    Not Available

    1990-02-28

    The Energy Security Act of 1980 established a program to provide financial assistance to private industry in the construction and operation of commerical-scale synthetic fuels plants. The Parachute Creek Shale Oil Program is one of four projects awarded financial assistance. The Program agreed to comply with existing environmental monitoring regulations and to develop an Environmental Monitoring Plan incorporating supplemental monitoring in the areas of water, air, solid waste, and worker health and safety during the period 1985-1992. These activities are described in a series of quarterly and annual reports. The report contains environmental compliance data reports, results of industrial hygiene compliance monitoring, and independent audits. Table 2-1 shows 14 of the 20 supplemental monitoring sites sampled during the quarter.

  13. Predictive Engineering Tools for Injection-Molded Long-Carbon-Fiber Thermoplastic Composites - FY13 Fourth Quarterly Report

    SciTech Connect

    Nguyen, Ba Nghiep; Simmons, Kevin L.

    2013-12-02

    This quarterly report summarizes the status of the project planning to obtain all the approvals required for a Cooperative Research and Development Agreement (CRADA) with Autodesk, Inc., Toyota Motor Engineering and Manufacturing North America (Toyota), and Magna Exterior and Interiors Corporation (Magna). The final CRADA documents processed by PNNL’s Legal Services were submitted to all the parties for signatures.

  14. PFBC HGCU Test Facility. Second quarterly technical progress report, CY 1992

    SciTech Connect

    Not Available

    1992-07-01

    This is the eleventh technical progress report submitted to the Department of Energy (DOE) in connection with the Cooperative Agreement between DOE and Ohio Power company for the Tidd Pressurized Fluidized Bed Combustion (PFBC) Hot Gas Clean Up Test Facility. This report covers the period of work completed during the Second Quarter of CY 1992. Activities included: The Tidd combustor internals were modified to connect the hot gas system for slipstream operation; Various pre-operational activities were completed, including pneumatic leak testing of the HGCU system, operation of the closed cycle cooling water system, operation of the back pulse compressor and air preheater, and checkout of the back pulse skid. Initial operation of the system using the bypass cyclone occurred during May 21--23, 1992; On May 23, 1992, an expansion joint ruptured, forcing the unit to be shut down. The failure was later determined to be due to stress corrosion. Following the expansion joint failure, a complete engineering review of the system was undertaken and is continuing; Contract Modification No. 6 was issued to Westinghouse during this quarter. This modification is for APF surveillance testing services; A purchase order was issued to Battelle for ash sampling hardware and testing services.

  15. Coal liquefaction process streams characterization and evaluation. Quarterly technical progress report, July 1--September 30, 1992

    SciTech Connect

    Brandes, S.D.; Winschel, R.A.; Burke, F.P.

    1992-11-01

    This is the twelfth Quarterly Technical Progress Report under DOE Contract DE-AC22-89PC89883. Major topics reported are: Summaries of the final reports produced by Lehigh University, West Virginia University, and Vander Sande Associates under the Participants Program are presented. Analytical data produced by CONSOL are provided in Appendix I for all samples employed in the Participants Program and issued with the samples to research groups in the Participants Program. A paper was presented at the 1992 US Department of Energy Pittsburgh Energy Technology Center Liquefaction Contractors` Review Conference, held in Pittsburgh September 23--24, 1992, entitled ``The Chemical Nature of Coal Liquid Resids and the Implications for Process Development``. It appears as Appendix 2 in this report.

  16. Quarterly technical progress report, October-December 1982 on Energy Conversion Research and Development Programs

    SciTech Connect

    Not Available

    1983-10-01

    In this quarterly technical progress report, UTSI reports on the continued design work for the low mass flow train superheater. The detailed design of this component continued and the overall arrangement drawing for the superheater and air heater was finalized. The air heater procurement reached the point of contract award, but the actual purchase order award was held up pending receipt of additional funding from the Department of Energy. Testing activity reported includes two additional tests in the LMF1C series, which concludes this test series. Test data are presented, along with preliminary analyses for the combustor, nozzle, diagnostic channel, diffuser, radiant furnace/secondary combustor and Materials Test Module. In addition to the nitrogen oxide test measurements, corrosion and erosion rates for the boiler tube specimens and the materials test module are reported.

  17. MHD Integrated Topping Cycle Project. Seventeenth quarterly technical progress report, August 1, 1991--October 31, 1991

    SciTech Connect

    Not Available

    1992-07-01

    This seventeenth quarterly technical progress report of the MHD Integrated Topping Cycle Project presents the accomplishments during the period August 1, 1991 to October 31, 1991. Manufacturing of the prototypical combustor pressure shell has been completed including leak, proof, and assembly fit checking. Manufacturing of forty-five cooling panels was also completed including leak, proof, and flow testing. All precombustor internal components (combustion can baffle and swirl box) were received and checked, and integration of the components was initiated. A decision was made regarding the primary and backup designs for the 1A4 channel. The assembly of the channel related prototypical hardware continued. The cathode wall electrical wiring is now complete. The mechanical design of the diffuser has been completed.

  18. Solvent refined coal (SRC) process. Quarterly technical progress report, January 1980-March 1980. [In process streams

    SciTech Connect

    Not Available

    1981-01-01

    This report summarizes the progress of the Solvent Refined Coal (SRC) project at the SRC Pilot Plant in Fort Lewis, Wahsington, and the Process Development Unit (P-99) in Harmarville, Pennsylvania. After the remaining runs of the slurry preheater survey test program were completed January 14, the Fort Lewis Pilot Plant was shut down to inspect Slurry Preheater B and to insulate the coil for future testing at higher rates of heat flux. Radiographic inspection of the coil showed that the welds at the pressure taps and the immersion thermowells did not meet design specifications. Slurry Preheater A was used during the first 12 days of February while weld repairs and modifications to Slurry Preheater B were completed. Two attempts to complete a material balance run on Powhatan No. 6 Mine coal were attempted but neither was successful. Slurry Preheater B was in service the remainder of the quarter. The start of a series of runs at higher heat flux was delayed because of plugging in both the slurry and the hydrogen flow metering systems. Three baseline runs and three slurry runs of the high heat flux program were completed before the plant was shut down March 12 for repair of the Inert Gas Unit. Attempts to complete a fourth slurry run at high heat flux were unsuccessful because of problems with the coal feed handling and the vortex mix systems. Process Development Unit (P-99) completed three of the four runs designed to study the effect of dissolver L/D ratio. The fourth was under way at the end of the period. SRC yield correlations have been developed that include coal properties as independent variables. A preliminary ranking of coals according to their reactivity in PDU P-99 has been made. Techniques for studying coking phenomenona are now in place.

  19. Project LIFE--Language Improvement to Facilitate Education. (Technical Progress Report; Third Quarter; March 1, 1974-May 31, 1974).

    ERIC Educational Resources Information Center

    National Foundation for the Improvement of Education, Washington, DC.

    Reported is the third quarter, fiscal year 1974 (March 1, 1974-May 31, 1974) technical progress of Project LIFE (Language Improvement to Facilitate Education), toward developing an instructional system in which filmstrips in the areas of perceptual training, perceptual thinking, and language/reading are used to assist hearing impaired children in…

  20. Regulatory and technical reports (abstract index journal). Volume 20, No. 2: Compilation for second quarter April--June 1995

    SciTech Connect

    1995-09-01

    This compilation consists of bibliographic data and abstracts for the formal regulatory and technical reports issued by the U.S. Nuclear Regulatory Commission (NRC) Staff and its contractors. It is NRC`s intention to publish this compilation quarterly and to cumulate it annually.

  1. Projects at the Component Development and Integration Facility. Quarterly technical progress report, January 1--March 31, 1993

    SciTech Connect

    Not Available

    1993-09-01

    This quarterly technical progress report presents progress on several different projects at the Component Development and Integration Facility (CDIF) during the second quarter of FY93. The CDIF is a major US Department of Energy test facility in Butte, Montana, operated by MSE, Inc. Projects in progress include: MHD Proof-of-Concept Project; Mine Waste Technology Pilot Program; Plasma Furnace Projects for waste destruction; Resource Recovery Project; Sodium Sulfide/Ferrous Sulfate Project; Soil Washing Project for removal of radioactive materials; and Spray Casting Project.

  2. Advancement of flash hydrogasification. Quarterly technical progress report, January-March 1984

    SciTech Connect

    Falk, A.Y.

    1984-06-25

    This first quarterly report documents technical progress during the period 31 December 1983 through 30 March 1984. The technical effort is 17 months in duration and is divided into two major technical tasks: Task VII, Hardware Fabrication and PDU Modifications, and Task VIII, Performance Testing. The design of test hardware and process development unit modifications had been previously completed as part of Task VI of the current contract. Task VII involves the fabrication of test hardware and modification of an existing 1-ton/h hydroliquefaction PDU at Rockwell's facilities for use as a hydrogasifier test facility. During this report period, fabrication of the test hardware and modifications to the PDU were initiated. Test hardware fabrication is now approximately 80% complete and should be completed by the end of May 1984. PDU modifications are progressing well and should be completed by the end of June 1984. The completed test hardware fabrication and PDU modifications will allow the conduct of short duration (1 to 2 h) hydrogasification tests along with preburner assembly performance evaluation tests in order to fulfill the test program objectives. Separate supplies of hydrogen, oxygen, methane, carbon monoxide, and water (for steam generation) are provided for this purpose. The modified facility is designed to accommodate both 10- and 20-ft-long hydrogasifier reactors so that residence times will be in the range of 2 to 6 s when coal is fed at a nominal 1/2 ton/h into reactors at 1000 psia pressure. Provisions are being made for real-time analysis of the product gases using an on-line gas chromatograph system. Test planning was the only Task VIII effort active during this report period. An initial (preliminary) test matrix has been defined. Preparation of a data analysis plan is underway, and data reduction programs are being programmed. 17 references, 25 figures, 6 tables.

  3. Methyl chloride via oxyhydrochlorination of methane. Quarterly technical progress report No. 13, October--December 1994

    SciTech Connect

    1995-02-01

    The purpose of this contract is to develop a process for converting light alkane gases to methyl chloride via oxyhydrochlorination using highly selective, stable catalysts in fixed-bed reactors designed to remove the large amount of heat generated, so as to control the reaction temperature. Further, the objective is to obtain the engineering data base necessary for developing a commercially feasible process and to evaluate t economics of the process. Significant progress was made in six different technical areas during this quarter. These key highlights are: (1) Evaluation of catalyst samples from UCI led to the ordering of the OHC PDU catalyst batch. This catalyst batch arrived, was screened and found to be defective, and was reordered. (2) Natural gas containing higher hydrocarbons was used as a methane source. The reactant mixture formed oxygenates at temperatures lower than observed in the past. Burning at such low temperatures seems to create a product stream containing very little CH{sub 2}Cl{sub 2}. (3) Although it has not been decided if the PDU will use natural gas from the plant or methane or natural gas from cylinders as a methane feed source, it was concluded that an adsorption unit to remove sulfur and higher hydrocarbons is not necessary at this time. (4) PDU construction was completed in December. The bulk of insulation work was completed at the end of November. Much effort has been put into pressure testing the PDU`s systems. The startup team has become adept at finding and correcting such leaks. (5) SOP writing for the PDU was completed this quarter with communication with the software programmer to insure agreement between the software and SOP.

  4. Power systems development facility. Quarterly technical progress report, July 1--September 30, 1993

    SciTech Connect

    Not Available

    1993-12-31

    This quarterly technical progress report summarizes work completed during the Second Quarter of the Second Budget Period, July 1 through September 30, 1993, under the Department of Energy (DOE) Cooperative Agreement No. DE-FC21-90MC25140 entitled ``Hot Gas Cleanup Test Facility for Gasification and Pressurized Combustion.`` The objective of this project is to evaluate hot gas particle control technologies using coal-derived gas streams. This will entail the design, construction, installation, and use of a flexible test facility which can operate under realistic gasification and combustion conditions. The major particulate control device issues to be addressed include the integration of the particulate control devices into coal utilization systems, on-line cleaning techniques, chemical and thermal degradation of components, fatigue or structural failures, blinding, collection efficiency as a function of particle size, and scaleup of particulate control systems to commercial size. The conceptual design of the facility was extended to include a within scope, phased expansion of the existing Hot Gas Cleanup Test Facility Cooperative Agreement to also address systems integration issues of hot particulate removal in advanced coal-based power generation systems. This expansion included the consideration of the following modules at the test facility in addition to the existing Transport Reactor gas source and Hot Gas Cleanup Units: Carbonizer/Pressurized Circulating Fluidized Bed Gas Source. Hot Gas Cleanup Units to mate to all gas streams; Combustion Gas Turbine; and Fuel Cell and associated gas treatment. This expansion to the Hot Gas Cleanup Test Facility is herein referred to as the Power Systems Development Facility (PSDF). The major emphasis during this reporting period was continuing the detailed design of the facility.

  5. Development of a $10/kW bipolar separator plate. Technical quarterly progress report, July 1--September 30, 1998

    SciTech Connect

    1998-12-31

    The authors have identified a moldable graphite blend separator plate material, have molded complex shape bipolar separator plates, have tested the molded plate properties and function in single fuel cells, and have designed a conceptual rapid manufacturing line. In this quarter, the project received a three-month interim funding period to continue progress while the proposal is in DOE review. Thus, this fourth quarterly report is submitted in place of the originally scheduled final report for this project. All of the objectives of this project have been accomplished. Specifically, the electrical, chemical, and physical properties of the molded separator plates have met or exceeded the DOE specifications. Performance and endurance tests of the molded plates in single cells have shown comparable performance to the state-of-art machined graphite separator plates. The DOE cost target of $10 per kW appears to be achievable with the low cost composite materials.

  6. EDS coal liquefaction process development: Phase V. Quarterly technical progress report, January 1-March 31, 1984

    SciTech Connect

    1984-07-01

    This report is the twenty-first Quarterly Technical Progress Report for US Department of Energy Cooperative Agreement No. DE-FC05-77ET10069 for EDS Coal Liquefaction Process Development Phase V. A detailed comparison of RCLU, CLPP, and ECLP yields has been initiated. This study builds off previous yield modeling results, which found that RCLU, CLPP, and ECLP yields were generally consistent given the scatter of the data, although some differences were noted. These pilot unit yield differences have now been quantified, and operating/configurational differences which account for some of them have been identified. Preliminary yield comparison results after correcting for these known process differences between the pilot plants indicate that: RCLU and CLPP yields are generally consistent; ECLP's conversion is about 5 lb/100 lb DAF coal lower than RCLU/CLPP at comparable operating conditions; and work has been initiated to define the EDS slurry preheater feed system design (based on slurry distributor manifold guidelines and coking correlation predictions, which influence furnace pass control issues such as slurry flow measurement). EDS hydrotreated naphtha showed a low level of systemic toxicity to rats exposed to the vapor six hours per day, five days per week for thirteen weeks.

  7. MHD Integrated Topping Cycle Project. Sixteenth quarterly technical progress report, May 1991--July 1991

    SciTech Connect

    Not Available

    1992-03-01

    The Magnetohydrodynamics (MHD) Integrated Topping Cycle (ITC) Project represents the culmination of the proof-of-concept (POC) development stage in the US Department of Energy (DOE) program to advance MHD technology to early commercial development stage utility power applications. The project is a joint effort, combining the skills of three topping cycle component developers: TRW, Avco/TDS, and Westinghouse. TRW, the prime contractor and system integrator, is responsible for the 50 thermal megawatt (50 MW{sub t}) slagging coal combustion subsystem. Avco/TDS is responsible for the MHD channel subsystem (nozzle, channel, diffuser, and power conditioning circuits), and Westinghouse is responsible for the current consolidation subsystem. The ITC Project will advance the state-of-the-art in MHD power systems with the design, construction, and integrated testing of 50 MW{sub t} power train components which are prototypical of the equipment that will be used in an early commercial scale MHD utility retrofit. Long duration testing of the integrated power train at the Component Development and Integration Facility (CDIF) in Butte, Montana will be performed, so that by the early 1990`s, an engineering data base on the reliability, availability, maintainability and performance of the system will be available to allow scaleup of the prototypical designs to the next development level. This Sixteenth Quarterly Technical Progress Report covers the period May 1, 1991 to July 31, 1991.

  8. Heterogeneous kinetics of coal gasification. Quarterly technical progress report, 1 April 1983-30 June 1983

    SciTech Connect

    Calo, J.M.; Ganapathi, R.

    1983-01-01

    In the current quarterly technical progress report we present data and results on transient kinetic studies of the steam-char reaction system for activated coconut and lignite chars. These experiments were conducted in a fashion similar to the previous char-CO/sub 2/ studies, under approximately the same experimental conditions. The two principal product species, H/sub 2/ and CO, were monitored using the automatic mass programming system developed especially for this project. In order to perform the steam-char experiments, the original apparatus was modified by the addition of a steam generation/condensate removal system. The steam-char reaction system, being somewhat more complex than the CO/sub 2/-char reaction system, was modeled with a six-parameter, elementary kinetic scheme. The ''effective'' active site concentrations determined from the steam gasification data were of the same order of magnitude, and behaved in a similar fashion, to those obtained for the CO/sub 2/ gasification studies. The implications of this result are briefly discussed. 21 refs., 23 figs., 2 tabs.

  9. Pipeline gas demonstration plant, Phase I. Quarterly technical progress report for June 1980-August 1980

    SciTech Connect

    Eby, R.J.

    1980-09-01

    Work was performed in the following tasks in Phase I of the Pipeline Gas Demonstration Plant Program: Demonstration Plant Process Design; Site Evaluation and Selection; Demonstration Plant Environmental Analysis; Feedstock Plans, Licenses, Permits and Easements; Demonstration Plant Definitive Design; Economic Reassessment; Technical Support; Long Lead Procurement List; and Project Management. The following Major Contract Deliverables were submitted to the Government: Process Evaluation Report - TIC Version; Conceptual Commercial Plant Design Report - TIC Version; Demonstration Plant Design Analysis Report - TIC Version; Demonstration Plant Process Design Report; Site Master Plan; and Prevention of Significant Deterioration Documentation. The major work activity has been the effort in Demonstration Plant Definitive Design which commenced following the completion of the Process Design Baseline Packages for the fourteen Demonstration Plant process areas. Task VIII, Economic Reassessment was opened in this quarter. Completion of the TIC copies of the ICGG major deliverables constituted a significant effort in this period. Work has progressed satisfactorily in the other Tasks in support of the Demonstration Plant Program.

  10. TIDD PFBC Demonstration Project: Third quarterly technical progress report 1992, CY 1992

    SciTech Connect

    Not Available

    1992-10-01

    This is the 22nd Technical Progress Report submitted to the Department of Energy in connection with the Cooperative Agreement between the DOE and the Ohio Power Company for the Tidd PFBC Demonstration Plant. This report covers the period from July 1, 1992 to September 30, 1992. The unit was operated for a total of 903 hours (including gas turbine air prewarming). There were 9 gas turbine starts, 11 preheating starts, and 8 operating periods with coal fire. The peak gross output of 59 MWH was achieved for the period of 1600 to 1700 hours on September 23, 1992. The longest coal fire was 422 hourb beginning at 1349 hours on August 9, 1992. Total gross generation was 32,418 MWH, and coal consumption was 15,846 tons. Testing was completed on the gas turbine blade resonance frequency problem. The report showed that a resonant frequency problem existing at high LPT speeds and at a mostly closed guide vane position. An operating curve was developed by ABBC to avoid the points of blade resonance. Monitoring of solid, liquid and gaseous waste streams, as detailed in the operations phase monitoring requirements in the EMP, were performed throughout the quarter.

  11. Coal liquefaction process streams characterization and evaluation. Quarterly technical progress report, July 1--September 30, 1993

    SciTech Connect

    Robbins, G.A.; Brandes, S.D.; Winschel, R.A.; Burke, F.P.

    1994-03-01

    This is the Sixteenth Quarterly Technical Progress Report under DOE Contract DE-AC22-89PC89883. Major topics reported are: Fifty-eight process samples from HRI CTSL Bench Unit Run CC-15 (227-75) were analyzed to provide information on process performance. Run CC-15 was operated for 14 periods (days) from October 21 through November 3, 1992 in the thermal/catalytic configuration with Black Thunder Mine (Wyodak and Anderson seams) coal and Shell S-317 Ni/Mo supported extrudate catalyst. The run was made to test performance with and without a dispersed hydrous iron hydroxide catalyst precursor impregnated in the coal. Results are compared with those of previous HRI CTSL bench unit Run CC-1, which was operated in the catalytic/catalytic configuration, also with Shell S-317 catalyst. Several HRI Run CC-15 product distillate fractions prepared by the National Institute for Petroleum and Energy Research (NIPER) for petroleum inspection tests were further characterized by CONSOL. These characterization data are presented. MicroAutoclave tests and chemical analyses were performed to evaluate the solvent quality of two potential solvents for Alberta Research Council ARC. Eight product samples from catalytic dehydrogenation experiments were characterized for the University of Pittsburgh. A description is presented of the thermogravimetric analysis (TGA) method for determination of resid concentration/resid conversion, which was adapted for use in-house from HRI`s standard method. A brief summary of the status of the Participants Program is given.

  12. MHD Integrated Topping Cycle Project. Fourteenth quarterly technical progress report, November 1, 1990-- January 31, 1991

    SciTech Connect

    Not Available

    1992-02-01

    This fourteenth quarterly technical progress report of the MHD Integrated Topping Cycle Project presents the accomplishments during the period November 1, 1990 to January 31, 1991. Testing of the High Pressure Cooling Subsystem electrical isolator was completed. The PEEK material successfully passed the high temperature, high pressure duration tests (50 hours). The Combustion Subsystem drawings were CADAM released. The procurement process is in progress. An equipment specification and RFP were prepared for the new Low Pressure Cooling System (LPCS) and released for quotation. Work has been conducted on confirmation tests leading to final gas-side designs and studies to assist in channel fabrication.The final cathode gas-side design and the proposed gas-side designs of the anode and sidewall are presented. Anode confirmation tests and related analyses of anode wear mechanisms used in the selection of the proposed anode design are presented. Sidewall confirmation tests, which were used to select the proposed gas-side design, were conducted. The design for the full scale CDIF system was completed. A test program was initiated to investigate the practicality of using Avco current controls for current consolidation in the power takeoff (PTO) regions and to determine the cause of past current consolidation failures. Another important activity was the installation of 1A4-style coupons in the 1A1 channel. A description of the coupons and their location with 1A1 channel is presented herein.

  13. PFBC HGCU Test Facility. Second quarterly technical progress report, CY 1993

    SciTech Connect

    Not Available

    1993-07-01

    This is the fifteenth Technical Progress Report submitted to the Department of Energy (DOE) in connection with the cooperative agreement between the DOE and Ohio Power Company for the Tidd Pressurized Fluidized Bed Combustion (PFBC) Hot Gas Clean Up Test Facility. This report covers the period of work completed during the Second Quarter of CY 1993.Work accomplished during the reporting period includes: the expansion joint heaters and control system were installed and tested. The system consists of 8 bellows heaters and 14 heaters on the adjacent piping. During initial testing, 11 of the 14 pipe and heaters failed due to overheating caused by control and installation problems; A pneumatically powered vibrator was installed in the APF manway nozzle to vibrate the hopper liner during back pulsing. This should eliminate any build-up on the pipes of the hopper; Two half capacity diesel driven back-up pulse air compressors were rented and installed; Installation of an emergency ash removal system was completed. The system enables ash to be removed via a line connected to the pipe between the outlet of the screw cooler and the inlet of the lockhopper system; Installation of the spoiling air line, valves, and metering orifice to the primary cyclone was completed; Numerous revisions were made to the Net 90 instrumentation and control system and the POPS data trending system to enhance system control and performance monitoring capability.

  14. EDS coal liquefaction process development. Phase V. Quarterly technical progress report, July 1-September 30, 1980

    SciTech Connect

    1981-02-01

    This report is the tenth Quarterly Technical Progress Report for US Department of Energy Cooperative Agreement No. DE-FC01-77ET10069 (formerly EF-77-A-01-2893) for Exxon Donor Solvent (EDS) Coal Liquefaction Process Development - Phase V. The Laboratory Process Research and Development studies were conducted at various Exxon Research and Engineering Co. (ER and E) facilities: Research and Development Division at Baytown, Texas; Products Research Division at Linden, New Jersey; and the Exxon Research and Development Laboratories at Baton Rouge, Louisiana. The Engineering Research and Development studies were performed at the Synthetic Fuels Engineering and Exxon Engineering Technology Departments of ER and E at Florham Park, New Jersey. The information dealing with the Management, Detailed Engineering, and Procurement activities related to revamp of the FLEXICOKING Prototype Unit was generated at Exxon Company, USA, Houston, Texas, and Exxon Engineering - Project Management Department of ER and E, Florham Park, New Jersey. The information dealing with operation of the 250 T/D Exxon Coal Liquefaction Pilot Plant (ECLP) was generated at Exxon Company, USA, Houston, Texas.

  15. Coal liquefaction process streams characterization and evaluation. Quarterly technical progress report, January 1--March 31, 1992

    SciTech Connect

    Robbins, G.A.; Brandes, S.D.; Winschel, R.A.; Burke, F.P.

    1992-08-01

    This is the tenth Quarterly Technical Progress Report under DOE Contract DE-AC22-89PC89883. Process oils from Wilsonville Run 262 were analyzed to provide information on process performance. Run 262 was operated from July 10 through September 30, 1991, in the thermal/catalytic Close-Coupled Integrated Two-Stage Liquefaction (CC-ITSL) configuration with ash recycle. The feed coal was Black Thunder Mine subbituminous coal. The high/low temperature sequence was used. Each reactor was operated at 50% of the available reactor volume. The interstage separator was in use throughout the run. The second-stage reactor was charged with aged Criterion 324 catalyst (Ni/Mo on 1/16 inch alumina extrudate support). Slurry catalysts and sulfiding agent were fed to the first-stage reactor. Molyvan L is an organometallic compound which contains 8.1% Mo, and is commercially available as an oil-soluble lubricant additive. It was used in Run 262 as a dispersed hydrogenation catalyst precursor, primarily to alleviate deposition problems which plagued past runs with Black Thunder coal. One test was made with little supported catalyst in the second stage. The role of phenolic groups in donor solvent properties was examined. In this study, four samples from direct liquefaction process oils were subjected to O-methylation of the phenolic groups, followed by chemical analysis and solvent quality testing.

  16. Coal liquefaction process streams characterization and evaluation. Quarterly technical progress report, April 1--June 30, 1992

    SciTech Connect

    Brandes, S.D.; Lancet, M.S.; Robbins, G.A.; Winschel, R.A.; Burke, F.P.

    1992-11-01

    This is the eleventh Quarterly Technical Progress Report under DOE Contract DE-AC22-89PC89883. Major topics reported are: (1) The results of a study designed to determine the effects of the conditions employed at the Wilsonville slurry preheater vessel on coal conversion is described. (2) Stable carbon isotope ratios were determined and used to source the carbon of three product samples from Period 49 of UOP bench-scale coprocessing Run 37. The results from this coprocessing run agree with the general trends observed in other coprocessing runs that we have studied. (3) Microautoclave tests and chemical analyses were performed to ``calibrate`` the reactivity of the standard coal used for determining donor solvent quality of process oils in this contract. (4) Several aspects of Wilsonville Close-Coupled Integrated Two-Stage Liquefaction (CC-ITSL) resid conversion kinetics were investigated; results are presented. Error limits associated with calculations of deactivation rate constants previously reported for Runs 258 and 261 are revised and discussed. A new procedure is described that relates the conversions of 850{degrees}F{sup +} , 1050{degrees}F{sup +}, and 850 {times} 1050{degrees}F material. Resid conversions and kinetic constants previously reported for Run 260 were incorrect; corrected data and discussion are found in Appendix I of this report.

  17. Production and screening of carbon products precursors from coal. Quarterly technical report, October 1, 1996--December 31, 1996

    SciTech Connect

    Irwin, C.L.

    1997-02-01

    The technical work during this past quarter has focused on enhancing equipment and instrumentation in the WVU Carbon Products Laboratory. Development work on coal-based precursors for carbon foams, pitches, cokes, and fibers continues. The effects of carbon powders and chopped fibers as additives to the foam precursor are being evaluated. Extensive coordination and technology transfer activities have been undertaken and are described in Section 5 of this report.

  18. Objective Structured Assessment of Technical Skills to Teach and Study Retention of Fourth-Degree Laceration Repair Skills

    PubMed Central

    Martinez, Anjali; Cassling, Caroline; Keller, Jennifer

    2015-01-01

    Background Fourth-degree perineal lacerations are a serious but infrequent complication of childbirth. Objective We studied the long-term effect of an educational workshop on the knowledge and ability of obstetrics and gynecology residents to repair fourth-degree lacerations. Methods We assessed obstetrics and gynecology residents' baseline knowledge and skill of fourth-degree laceration repair by using a written examination and the Objective Structured Assessment of Technical Skills (OSATS). After the educational intervention (a lecture, a demonstrational video, and practice on a model), residents completed a written and OSATS posttest. Six months later, residents took the same posttests to determine their level of retention. Another group of residents who had not attended the workshop also took the tests at the 6-month mark and served as a control group. Results A total of 17 residents were in the intervention group and 11 residents in the control group. The pretest written examination mean was 6.1/10 and the OSATS mean was 10.9/18. After the workshop, the written mean increased to 9.1/10 and the OSATS to 16.6/18. This improvement was statistically significant (P < .01). Compared to the pretest, the 6-month follow-up scores had a statistically significant increase (written mean, 8.0/10, P < .01, and OSATS mean 15.5/18, P < .01). Conclusions Residents improved on the written examination and OSATS after the educational workshop and maintained this improvement for 6 months. This intervention may prepare graduating residents for repairing future fourth-degree lacerations they may not have encountered during training. PMID:26217419

  19. Objective Structured Assessment of Technical Skills to Teach and Study Retention of Fourth-Degree Laceration Repair Skills.

    PubMed

    Martinez, Anjali; Cassling, Caroline; Keller, Jennifer

    2015-03-01

    Fourth-degree perineal lacerations are a serious but infrequent complication of childbirth. We studied the long-term effect of an educational workshop on the knowledge and ability of obstetrics and gynecology residents to repair fourth-degree lacerations. We assessed obstetrics and gynecology residents' baseline knowledge and skill of fourth-degree laceration repair by using a written examination and the Objective Structured Assessment of Technical Skills (OSATS). After the educational intervention (a lecture, a demonstrational video, and practice on a model), residents completed a written and OSATS posttest. Six months later, residents took the same posttests to determine their level of retention. Another group of residents who had not attended the workshop also took the tests at the 6-month mark and served as a control group. A total of 17 residents were in the intervention group and 11 residents in the control group. The pretest written examination mean was 6.1/10 and the OSATS mean was 10.9/18. After the workshop, the written mean increased to 9.1/10 and the OSATS to 16.6/18. This improvement was statistically significant (P < .01). Compared to the pretest, the 6-month follow-up scores had a statistically significant increase (written mean, 8.0/10, P < .01, and OSATS mean 15.5/18, P < .01). Residents improved on the written examination and OSATS after the educational workshop and maintained this improvement for 6 months. This intervention may prepare graduating residents for repairing future fourth-degree lacerations they may not have encountered during training.

  20. Nickel Based Superalloy with Improved Weldability and Oxidation Resistance. Fourth quarterly report for the period July 1999 to October 1999

    SciTech Connect

    George Simkovich; Eric Whitney

    1999-11-01

    The aim of this project is to determine and provide technical and economic data to a commercial end user of the alloy so that a full-scale alloy qualification program can be defined and implemented. The object of this project is to define the compositional range for a new alloy that is suitable for evaluation and qualification by a commercial enterprise. Alloy properties that will need to be determined include weldability, oxidation resistance, creep strength, resistance to thermo-mechanical fatigue, microstructure stability, and cost. Test results will be used to finalize the compositional range of an alloy that will undergo a rigorous qualification process.

  1. Applications of advanced petroleum production technology and water alternating gas injection for enhanced oil recovery: Mattoon Oil Field, Illinois. Fourth quarterly report, [October 1, 1993--December 31, 1993

    SciTech Connect

    Baroni, M.

    1994-01-25

    The objectives of this project are to continue reservoir characterization of the Cypress Sandstone; to identify and map fades-defined waterflood units (FDWS); and to design and Implement water-alternating-gas (WAG) oil recovery utilizing carbon dioxide (CO{sub 2}). The producibility problems are permeability variation and poor sweep efficiency. Phase 1 of the project focuses on the development of computer-generated geological and reservoir simulation models that will be used to select sites for the demonstration and implementation of CO{sub 2} displacement programs in Phase 2. Included in Phase 1 is the site selection and drilling of an infill well, coring of the Cypress interval, and injectivity testing to gather information used to update the reservoir simulation model. Phase 2 involves field implementation of WAG. Technology Transfer includes outreach activity such as seminars, workshops, and field trips. Technical progress for this quarter is described.

  2. Hybrid 320 Ton Off Highway Haul Truck: Quarterly Technical Status Report 9

    SciTech Connect

    Tim Richter

    2005-03-02

    This ninth quarterly status report for the Hybrid Off Highway Vehicle (OHV) project, DOE Award DEFC04- 2002AL68080 presents the project status at the end of December 2004, and covers activities in the ninth project quarter, October - December 2004.

  3. Quarterly Reporting of Government-Funded Activity to the 2015 National VET Provider Collection. Technical Paper

    ERIC Educational Resources Information Center

    Foley, Paul

    2016-01-01

    The topic of more frequent and timely vocational education and training (VET) data has been an issue of interest for a number of years. Since 2015, the National Centre for Vocational Education Research (NCVER) has collected and reported data on government-funded students and courses on a quarterly basis. These quarterly data submissions are…

  4. Stanford Geothermal Program (quarterly technical progress reports, July--September 1990 and October--December 1990)

    SciTech Connect

    Not Available

    1991-02-18

    For the summer quarter, progress is summarized and data are presented on the following: well test analysis of finite-conductivity fractures, theoretical investigation of adsorption phenomena, and optimization of reinjection strategy. For the fall quarter, activity focused on the adsorption and well testing projects. A new project investigating reinjection at the Geysers was initiated. (MHR)

  5. Caldwell Community College and Technical Institute 1982-1983 Fact Book. Fourth Edition.

    ERIC Educational Resources Information Center

    Tippett, Candace, Comp.; Clegg, Margarette, Comp.

    Statistical data are provided on the enrollments, programs, faculty and staff, finances, facilities, and future students of Caldwell Community College and Technical Institute (CCC&TI). First, general information is provided on the history and mission of CCC&TI, the characteristics of its service area, its administrative organization, and its board…

  6. Kansas State University: DOE/KEURP Site Operator Program. Year 4, fourth quarterly report, April 1, 1995--June 30, 1995

    SciTech Connect

    1995-08-01

    Kansas State University, in support of a DOE and Kansas Electric Utilities Research Program subject contract, continues to test, evaluate, demonstrate, and develop electric vehicle and infrastructure technology. K-State is operating two Soleq EVcort vehicles. During this reporting period both vehicles were brought back to full operational status after warranty service was completed by Soleq. Vehicle failures occurred due to three unrelated battery cable failures in addition to the replacement of one battery. Both vehicles are being operated on a routine basis. K-State, along with York Technical College, has established a relationship with Troy Design and Manufacturing (TDM) Redford, Michigan. K-State has ordered no less than four Ford Ranger electric trucks from TDM. K-State is involved in the steering committee that is monitoring and refining information to direct the design and testing of these new technology vehicles. TDM should become the first automotive manufacturer certified by one of the Big Three under their Quality Vehicle Manufacturer program. Kansas State University and the Kansas Electric Utility Research Program look forward to working with TDM on their new EV program.

  7. Identification and Evaluation of Fluvial-Dominated Deltaic Reservoirs. Quarterly technical report, April 1 -June 30, 1997

    SciTech Connect

    Banken, M.K.; Andrews, R.

    1997-09-12

    This document is provided as a Quarterly Technical Progress Report for the program entitled `Identification and Evaluation of Fluvial- Dominated Deltaic (Class 1 Oil) Reservoirs in Oklahoma`, covering the reporting period of April 1 - June 30, 1997. Work is progressing as expected for the project. The FDD computer facility is fully operational. During this quarter, there were 27 industry individuals who used the facility. The Tonkawa Play workshop is scheduled for July 9, 1997 in Norman. The Tonkawa publication and presentation graphics are nearly completed. The Bartlesville workshop is scheduled for October and November, 1997, in three different sites. Text and illustrations for that play are in progress. This project is serving an extremely valuable role in the technology transfer activities for the Oklahoma petroleum industry, with very positive industry feedback.

  8. [National Institute for Petroleum and Energy Research] quarterly technical report, October 1--December 31, 1992

    SciTech Connect

    Not Available

    1993-04-01

    Accomplishments for the past quarter are described for the following tasks: chemical flooding--supporting research; gas displacement--supporting research; thermal recovery--supporting research; geoscience technology; resource assessment technology; and microbial technology.

  9. Fischer Tropsch synthesis in supercritical fluids. Quarterly technical progress report, July 1, 1995--September 30, 1995

    SciTech Connect

    Akgerman, A.; Bukur, D.B.

    1996-05-01

    Our objective for this quarter was to compare performance of the Ruhrchemie catalyst in different modes of operation: fixed bed reactor (conventional and supercritical mode of operation), and stirred tank slurry reactor. Diffusion coefficients are discussed.

  10. Short-term energy outlook: Quarterly projections. Second quarter 1995

    SciTech Connect

    1995-05-02

    The Energy Information Administration (EIA) prepares quarterly, short-term energy supply, demand, and price projections for publication in February, May, August, and November in the Short-Term Energy Outlook (Outlook). An annual supplement analyzes the performance of previous forecasts, compares recent projections with those of other forecasting services, and discusses current topics related to the short-term energy markets. (See Short-Term Energy Outlook Annual Supplement, DOE/EIA-0202.) The forecast period for this issue of the Outlook extends from the second quarter of 1995 through the fourth quarter of 1996. Values for the first quarter of 1995, however, are preliminary EIA estimates (for example, some monthly values for petroleum supply and disposition are derived in part from weekly data reported in the Weekly Petroleum Status Report) or are calculated from model simulations using the latest exogenous information available (for example, electricity sales and generation are simulated using actual weather data). The historical energy data, compiled into the second quarter 1995 version of the Short-Term Integrated Forecasting System (STIFS) database, are mostly EIA data regularly published in the Monthly Energy Review, Petroleum Supply Monthly, and other EIA publications. Minor discrepancies between the data in these publications and the historical data in this Outlook are due to independent rounding. The STIFS database is archived quarterly and is available from the National Technical Information Service.

  11. Short-term energy outlook. Quarterly projections, third quarter 1996

    SciTech Connect

    1996-07-01

    The Energy Information Administration (EIA) prepares quarterly, short-term energy supply, demand, and price projections for publication in January, April, July, and October in the Outlook. The forecast period for this issue of the Outlook extends from the third quarter of 1996 through the fourth quarter of 1997. Values for the second quarter of 1996, however, are preliminary EIA estimates (for example, some monthly values for petroleum supply and disposition are derived in part from weekly data reported in the Weekly Petroleum Status Report) or are calculated from model simulations using the latest exogenous information available (for example, electricity sales and generation are simulated using actual weather data). The historical energy data, compiled in the third quarter 1996 version of the Short-Term Integrated Forecasting System (STIFS) database, are mostly EIA data regularly published in the Monthly energy Review, Petroleum Supply Monthly, and other EIA publications. Minor discrepancies between the data in these publications and the historical data in this Outlook are due to independent rounding. The STIFS database is archived quarterly and is available from the National Technical Information Service.

  12. LFCM vitrification technology: Quarterly progress report, July-September 1987

    SciTech Connect

    Brouns, R.A.; Allen, C.R.; Powell, J.A.; Bates, S.O.; Bray, L.A.; Budden, M.J.; Dierks, R.D.; Elliott, M.L.; Elmore, M.R.; Faletti, D.W.; Farnsworth, R.K.; Holton, L.K. Jr.; Kuhn, W.L.; Mellinger, G.B.; Nakaoka, R.K.; Peterson, M.E.; Piepel, G.F.; Powell, J.A.; Pulsipher, B.A.; Reimus, M.A.H.; Surma, J.E.; Wiemers, K.D.

    1988-09-01

    This report describes the progress in developing, testing, applying and documenting liquid-fed ceramic melter vitrification technology. Progress in the following technical subject areas during the fourth quarter of FY 1987 is discussed: melting process chemistry and glass development, feed preparation and transfer systems, canister filling and handling systems, and process/product modeling and control.

  13. Toms Creek Integrated Gasification Combined Cycle Demonstration Project. Final quarterly technical progress report for the period ending March 31, 1993

    SciTech Connect

    Feher, G.

    1993-05-24

    This Quarterly Technical Progress Report for the period ending March 31, 1993 summarizes the work done to data by Tampella Power Corporation and Enviropower, Inc. on the integrated combined-cycle power plant project. Efforts were concentrated on the Toms Creek PDS (Preliminary Design and Studies). Tampella Power Corporation`s efforts were concentrated on the Toms Creek Preliminary Process Flow Diagram (PFD) and Piping and Instrument Diagrams (P&IDs). Tampella Power Corporation also prepared Heat and Material Balances (H&MBs) for different site-specific cases.

  14. Bench-scale testing of the micronized magnetite process. Second quarterly technical progress report, October 1994--December 1994

    SciTech Connect

    1995-01-19

    This document contains the Quarterly Technical Progress Report for the Micronized Magnetite Testing Project being performed at PETC`s Process Research Facility (PRF). This second quarterly report covers the period from October, 1994 through December, 1994. The main accomplishments of Custom Coals and the project subcontractors, during this period, included: (1) Submitted all overdue project documents and kept up with routine reporting requirements; (2) Worked with CLI Corporation, the design subcontractor, and completed the circuit design and finalized all design drawings; (3) Specified and procured all of the process equipment for the circuit, as well as a number of ancillary equipment, instruments, and supplies; (4) Assisted Vangura Iron Inc. in detailing and constructing the structural and platework steel; (5) Subcontracted Rizzo & Sons to perform the circuit mechanical and electrical installation, and prepared for January 23rd installation start date; (6) Organized and prepared for coal and magnetite procurement; (7) Specified and organized an operating personnel plan for the commissioning and testing tasks in the project; (8) Assessed analytical challenges for project, and began to research problem areas. This report contains a short discussion of the project description, objectives, budget, schedule, and teaming arrangement. It also includes a detailed discussion of the abovementioned project accomplishments and plans, organized by the various task series within the project work plan. The final section contains an outline of the specific project goals for the next quarterly reporting period.

  15. Excimer laser annealing to fabricate low cost solar cells. Quarterly technical report No. 1, 26 March-30 June 1984

    SciTech Connect

    Not Available

    1984-07-01

    The objective of this research is to show whether or not pulsed excimer laser annealing (PELA) of ion-implanted junctions is a cost effective replacement for diffused junctions in fabricating crystalline silicon solar cells. The preliminary economic analysis completed during the first quarter of this program shows that the use of PELA to fabricate both the front junction and back surface field (BSF) would cost approximately 35 cents per peak watt (Wp), compared to a cost of 15 cents/Wp for diffusion, aluminum BSF and an extra cleaning step in the baseline process described by JPL. The cost advantage of the PELA process depends on improving the average cell efficiency from 14% to 16%, which would lower the overall cost of the module by about 15 cents/Wp. The technical goal of this research is to develop an optimized PELA process compatible with commercial production, and to demonstrate increased cell efficiency with sufficient product for adequate statistical analysis. During the first quarter of this program an excimer laser annealing station was set-up and made operational. The first experiment used 248 nm radiation to anneal phosphorus implants in polished and texture-etched silicon. Preliminary results showed that the PELA processed cells had overall efficiencies comparable to furnace annealed ion implanted controls, and that texture-etched material requires lower fluence for annealing than polished silicon. Process optimization will be carried out in the second quarter.

  16. Advanced liquefaction using coal swelling and catalyst dispersion techniques. Quarterly technical progress report, April--June 1992

    SciTech Connect

    Curtis, C.W.; Gutterman, C.; Chander, S.

    1992-08-26

    Research in this project centers upon developing a new approach to the direct liquefaction of coal to produce an all-distillate product slate at a sizable cost reduction over current technology. The approach integrates all aspects of the coal liquefaction process including coal selection, pretreatment, coal swelling with catalyst impregnation, coal liquefaction experimentation, product recovery with characterization, alternate bottoms processing, and a technical assessment including an economic evaluation. The project is being carried out under contract to the United States Department of Energy. On May 28, 1992, the Department of Energy authorized starting the experimental aspects of this projects; therefore, experimentation at Amoco started late in this quarterly report period. Research contracts with Auburn University, Pennsylvania State University, and Foster Wheeler Development Corporation were signed during June, 1992, so their work was just getting underway. Their work will be summarized in future quarterly reports. A set of coal samples were sent to Hazen Research for beneficiation. The samples were received and have been analyzed. The literature search covering coal swelling has been up-dated, and preliminary coal swelling experiments were carried out. Further swelling experimentation is underway. An up-date of the literature on the liquefaction of coal using dispersed catalysts is nearing completion; it will be included in the next quarterly report.

  17. AFRRI Reports, Fourth Quarter 1991

    DTIC Science & Technology

    1992-01-01

    combination therapy in prevention of bacterial translocation and animal mortality after irradiation. SR91-43: Brook, I., and Ledney, G. D. Oral aminoglycoside...and ofloxacin therapy in the prevention of gram-negative sepsis after irradiation. SR91-44: Bruley des Varannes, S., Mizrahi, M.. and Dubois, A...syndrome in the canine: Effect of therapy on survival. SR91-50: Pellmar, T. C. Fatty acids modulate excitability in guinea-pig hippocampal slices. SR91

  18. AFRRI Reports, Fourth Quarter 1992

    DTIC Science & Technology

    1993-01-01

    contrast, ion channel activ- (Kc.) potassium channels on the apical and basal surfaces of ity has not been recorded on the exposed basal mem- bovine ...monolayers provides indi- rect evidence about channel distribution in polarized Isolation and Identification of Bovine Aortic Endothelial CellS cells...direct observation of ion channel activity is re- Endothelial cells were dislodged from the vessel wall of bovine quired to conclusively demonstrate

  19. Plasma separation process: Quarterly technical report for period 1 October 1987 through 31 December 1987

    SciTech Connect

    Not Available

    1988-01-01

    The closeout plan was modified during the quarter to reflect a no cost extension of the Phase II period of performance from 15 November 1987 through 15 January 1988 and a delay of the PPM magnet warmup to the first quarter of CY 1988. The magnet warmup delay was instituted to allow the possible use of the PPM for an application demonstration. To maintain the overall closeout schedule, the resources associated with the magnet warmup are being used to accelerate the PPM process hardware decontamination. 8 figs., 4 tabs.

  20. Liquid fossil-fuel technology. Quarterly technical progress report, January-March 1983

    SciTech Connect

    Linville, B.

    1983-07-01

    Accomplishments for the quarter ending March 1983 are presented under the following headings: liquid fossil fuel cycle, processing, utilization, and project integration and technology transfer. Feature articles for this quarter are: (1) abandoned oil field reports issued; (2) oilfield water data bank report published; (3) microbial enhanced recovery report issued; (4) polymer-augmented project could be economic today; (5) carbon dioxide EOR estimates given; (6) BETC passes 65th milestone; and (7) fifty achievements for fifty years (1918-1968). BETC publications are also listed. (ATT)

  1. International Project on Technical and Vocational Education (UNEVOC). International Advisory Committee, Fourth Session (Paris, France, March 10-12, 1997). Final Report.

    ERIC Educational Resources Information Center

    United Nations Educational, Scientific, and Cultural Organization, Berlin (Germany). International Project on Technical and Vocational Education (UNEVOC).

    The fourth session of the UNEVOC International Advisory Committee was opened by Colin N. Power, whose welcoming address emphasized the importance of technical and vocational education (TVE) for socioeconomic development of UNESCO's member states. He pointed out that this sector of education is facing serious challenges posed by the recent trends…

  2. OTEC support services. Quarterly technical progress report No. 17, 15 May 1982-14 August 1982

    SciTech Connect

    1982-08-01

    Progress relative to accomplishments and relative to meetings, conferences, etc. are reported in the areas of OTEC commercialization support, program technical engineering and instrumentation analysis, technical and management services, OTEC system integration, and transmission subsystem considerations. (LEW)

  3. OTEC support services. Quarterly technical progress report No. 19, November 15, 1982-February 14, 1983

    SciTech Connect

    Not Available

    1983-03-01

    Activities relative to accomplishments and to meetings, conferences, etc. are reported in the areas of: OTEC commercialization support, program technical engineering and instrumentation analysis, technical and management services, OTEC systems integration, and transmission subsystem considerations. (LEW)

  4. OTEC support services. Quarterly technical progress report No. 11, 15 November 1980-14 February 1981

    SciTech Connect

    1981-02-01

    Technical engineering and management support services for the Ocean Thermal Energy Conversion Program are listed along with their objectives. Progress is reported on the following: technical assessments, OTEC system integration, environment and siting considerations, and transmission subsystem considerations. (MHR)

  5. Management of dry flue gas desulfurization by-products in underground mines. Quarterly technical progress report, April 1995--June 1995

    SciTech Connect

    Chugh, Y.P.; Dutta, D.; Esling, S.

    1995-07-01

    On September 30, 1993, the U.S. Department of Energy-Morgantown Energy Technology Center and Southern Illinois University at Carbondale (SIUC) entered into a cooperative research agreement entitled {open_quotes}Management of Dry Flue Gas Desulfurization By-Products in Underground Mines{close_quotes} (DE-FC21-93MC30252). Under the agreement Southern Illinois University at Carbondale will develop and demonstrate several technologies for the placement of coal combustion residues in abandoned coal mines, and will assess the environmental impact of such underground residues placement. Previous quarterly Technical Progress Reports have set forth the specific objectives of the program, and a discussion of these is not repeated here. Rather, this report discusses the technical progress made during the period April 1 - June 30, 1995. A final topical report on the SEEC, Inc. demonstration of its technology for the transporting of coal combustion residues was completed during the quarter, although final printing of the report was accomplished early in July, 1995. The SEEC technology involves the use of Collapsible Intermodal Containers (CIC`s) developed by SEEC, and the transportation of such containers - filled with fly ash or other coal combustion residues - on rail coal cars or other transportation means. Copies of the final topical report, entitled {open_quotes}The Development and Testing of Collapsible Intermodal Containers for the Handling and Transport of Coal Combustion Residues{close_quotes} were furnished to the Morgantown Energy Technology Center. The Rapid Aging Test colums were placed in operation during the quarter. This test is to determine the long-term reaction of both the pneumatic and hydraulic mixtures to brine as a leaching material, and simulates the conditions that will be encountered in the actual underground placement of the coal combustion residues mixtures. The tests will continue for about one year.

  6. OTEC support services. Quarterly technical progress report No. 16, 15 February 1982-14 May 1982

    SciTech Connect

    Not Available

    1982-05-01

    Technical progress is reported in the area of OTEC program survey, analysis, evaluation, and recommendation concerning program performance, including OTEC commercialization support and program technical engineering and instrumentation analysis. Progress is also reported in the areas of program technical monitoring, OTEC system integration, and transmission subsystem considerations. Participation in meetings, conferences, etc. is also reported. (LEW)

  7. OTEC support services. Quarterly technical progress report No. 18, 15 August 1982-14 November 1982

    SciTech Connect

    Not Available

    1982-11-01

    After a brief description of the technical engineering and management support services for the OTEC Program and of the task objectives, technical progress is reported in the areas of: survey, analysis, and evaluation; program technical monitoring; and transmission subsystem subsytem considerations. (LEW)

  8. OTEC support services quarterly technical progress report No. 14, 15 August 1981-14 November 1981

    SciTech Connect

    1981-11-01

    The progress in the areas of system integration, system engineering, and management services is reported. The effort is divided into seven tasks: survey, analysis, and evaluation of technical program status; program technical monitoring; development and implementation of methodology for identification, evaluation, and trade-off for major subsystem configurations; technical assessments; OTEC system integration; environment and siting considerations; and transmission subsystem considerations. (LEW)

  9. Amarillo National Resource Center for Plutonium quarterly technical progress report, August 1, 1997--October 31, 1997

    SciTech Connect

    1997-12-31

    This report summarizes activities of the Amarillo National Resource Center for Plutonium during the quarter. The report describes the Electronic Resource Library; DOE support activities; current and future environmental health and safety programs; pollution prevention and pollution avoidance; communication, education, training, and community involvement programs; and nuclear and other material studies, including plutonium storage and disposition studies.

  10. Electrostatic beneficiation of coal. Quarterly technical progress report, July 1--September 30, 1995

    SciTech Connect

    Mazumder, M.K.; Lindquist, D.; Tennal, K.B.

    1995-10-01

    The report discusses the progress made during the eighth quarter on the following tasks: assessing beneficiation (sulfur vs. ash); effect of weathering on charging and separation; charge measurement with E-SPART analyzer; particle measurement using image processing; and petrographic analysis. Some experimental data are included.

  11. Los Angeles County Juvenile Justice Crime Prevention Act. RAND Quarterly Report, October 2008. Technical Report

    ERIC Educational Resources Information Center

    Fain, Terry; Turner, Susan; Ridgeway, Greg

    2009-01-01

    This document is the second quarterly progress report for the evaluation of Juvenile Justice Crime Prevention Act (JJCPA) programs for the Los Angeles County Probation Department. The report covers the period from July 1, 2008, through September 30, 2008. The intent of the report is to provide Probation and the community-based organizations (CBOs)…

  12. Educational Technology Program. Quarterly Technical Summary, 1 September Through 30 November 1972.

    ERIC Educational Resources Information Center

    Frick, Frederick C.

    Several on-goint activities were conducted during this quarter. Field trials of the Lincoln Training System-3 (LTS-3) at Keesler Air Force Base were extended to include high-aptitude students previously excluded. Results showed such students scored significantly higher on achievement tests and learned substantially faster when they received LTS…

  13. Educational Technology Program. Quarterly Technical Summary, 1 March through 31 May 1973.

    ERIC Educational Resources Information Center

    Frick, Frederick C.

    During this quarter further investigations of alternative designs for the Lincoln Training System LTS-4 project's features and subsystems continued. Software efforts proceeded concurrently in three areas: 1) system architecture, monitor, and input/output programs; 2) a new version of the Lincoln Terminal Language, LTL-2; and 3) programs to apply…

  14. Educational Technology Program. Quarterly Technical Summary, 1 June through 31 August 1971.

    ERIC Educational Resources Information Center

    Frick, Frederick C.

    During the quarter covered by this report, the design of the Lincoln Training System-3 (LTS-3) Terminal System was completed and construction of a prototype unit begun. Four major hardware developments occurred: 1) An Image Systems, Incorporated Model 201 CARD Reader was converted into the LTS-3 audio-visual student terminal; 2) the first of five…

  15. Los Angeles County Juvenile Justice Crime Prevention Act. RAND Quarterly Report, October 2008. Technical Report

    ERIC Educational Resources Information Center

    Fain, Terry; Turner, Susan; Ridgeway, Greg

    2009-01-01

    This document is the second quarterly progress report for the evaluation of Juvenile Justice Crime Prevention Act (JJCPA) programs for the Los Angeles County Probation Department. The report covers the period from July 1, 2008, through September 30, 2008. The intent of the report is to provide Probation and the community-based organizations (CBOs)…

  16. Fischer Tropsch synthesis in supercritical fluids. Quarterly technical progress report, January 1, 1995--March 31, 1995

    SciTech Connect

    Akgerman, A.; Bukur, D.B.

    1996-05-01

    Our objectives for this quarter were: (1) to install and test the temperature probe and the flammable gas detector: (2) to conduct Fischer-Tropsch synthesis experiments at baseline conditions and at a high pressure in order to test the newly constructed fixed bed reactor assembly.

  17. Educational Technology Program. Quarterly Technical Summary; 1 December 1974 through 28 February 1975.

    ERIC Educational Resources Information Center

    Frick, Frederick C.

    The development of the Lincoln Terminal System (LTS) terminals is described. During the quarter, a decision was made to discontinue work on a cassette-based microfiche storage and retrieval system and to continue work on a carousel-based system. The center has continued its preparation of lessons for use with LTS. Application of LTS to the…

  18. Projects at the Western Environmental Technology Office. Quarterly technical progress report, January 1--March 31, 1995

    SciTech Connect

    1995-06-01

    This quarterly report briefly describes recent progress in eight projects. The projects are entitled Biomass Remediation Project; Heavy Metal-Contaminated Soil Project; MHD Shutdown; Mine Waste Technology Program; Plasma Projects; Resource Recovery Project; Spray Casting Project; and Watervliet Arsenal Project.

  19. Methyl chloride via oxyhydrochlorination of methane. Quarterly technical progress report No. 6, January--March 1993

    SciTech Connect

    Not Available

    1993-11-01

    The purpose of this contract is to develop a process for converting light alkane gases to methyl chloride via oxyhydrochlorination using highly selective, stable catalysts in fixed-bed reactors designed to remove the large amount of heat generated, so as to control the reaction temperature. Further, the objective is to obtain the engineering data base necessary for developing a commercially feasible process and to evaluate the economics of the process. This document reports significant progress this quarter toward the development of a stable heterogeneous packed bed catalyst for the oxyhydrochlorination of methane. This quarter`s data shows a catalyst which gave an average 18% methane conversion and 78% MeCl selectivity for a 12 day period of time. The PDU (Process Development Unit) design engineering effort made significant progress this quarter. A bid on a modular unit by Xytel Corp. was received and evaluated. The pre-engineering estimate showed that costs were considerably higher than the original project capital estimates. A rigorous effort was made to eliminate all non-essential equipment and scope of work. A reduced scope was agreed upon and in the second round both Xytel and the Dow Corning in-house facilities engineering team were allowed to bid on the package.

  20. Preparation of super-clean coal. Technical progress report for third and fourth quarters, March 15, 1984-September 14, 1984

    SciTech Connect

    Yonn, R.H.; Adel, G.T.; Luttrell, G.H.

    1984-01-01

    To better understand the fundamental steps involved in the froth flotation process, the collection efficiencies for the flotation of a very hydrophobic, ash-free coal sample have been determined. The results show that the collection efficiency increases drastically with decreasing bubble size, as predicted from a hydrodynamic model proposed by Weber and Paddock (1983). A mathematical model has been developed in the present work to predict the rate constant as a function of bubble size using theoretical collision efficiency values. The experimental rate constants determined in the present work, using a run-of-mine coal, exhibit a power relationship predicted from the model, but the values are lower than the model predictions by approximately 35 to 45%. This discrepancy may be attributed to other efficiency terms, e.g., adhesion efficiency, not considered in this model. 5 references, 9 figures.

  1. Coal plasticity at high heating rates and temperatures. First technical progress report for the fourth quarter 1989

    SciTech Connect

    Darivakis, G.S.; Peters, W.A.; Howard, J.B.

    1990-01-01

    The broad objective of this project is to obtain improved, quantitative understanding of the transient plasticity of bituminous coals under high heating rates and other reaction and pretreatment conditions of scientific and practical interest. To these ends the research plan is to measure the softening and resolidification behavior of two US bituminous coals with a rapid-heating, fast response, high-temperature coal plastometer, previously developed in this laboratory. Specific measurements planned for the project include determinations of apparent viscosity, softening temperature, plastic period, and resolidificationtime for molten coal: (1) as a function of independent variations in coal type, heating rate, final temperature, gaseous atmosphere (inert, 0{sub 2} or H{sub 2}), and shear rate; and (2) in exploratory runs where coal is pretreated (preoxidation, pyridine extraction, metaplast cracking agents), before heating. The intra-coal inventory and molecular weight distribution of pyridine extractables will also be measured using a rapid quenching, electrical screen heater coal pyrolysis reactor. The yield of extractables is representative of the intra-coal inventory of plasticing agent (metaplast) remaining after quenching. Coal plasticity kinetics will then be mathematically modeled from metaplast generation and depletion rates, via a correlation between the viscosity of a suspension and the concentration of deformable medium (here metaplast) in that suspension. Work during this reporting period has been concerned with re-commissioning the rapid heating rate plastometer apparatus.

  2. Development of the selective coagulation process. Fourth quarter technical progress report, July 1, 1991--September 30, 1991

    SciTech Connect

    Yoon, R.H.; Luttrell, G.H.

    1991-12-31

    The aim of this project is to develop an economical method for producing low-sulfur and low-ash coals using the selective hydrophobic coagulation (SHC) process. This work has been divided into three tasks: (1) project planning and sample acquisition; (2) studies of the fundamental mechanism(s) of the selective coagulation process and the parameters that affect the process of separating coal from both the ash-forming minerals and pyritic sulfur; and (3) bench-scale process development test work to establish the best possible method(s) of separating the hydrophobic and coagula from the dispersed mineral matter.

  3. Hydrocarbons associated with brines from geopressured wells. Fourth quarterly technical progress report, 1 October 1990--30 December 1990

    SciTech Connect

    Not Available

    1991-01-15

    The purpose of this research is to determine the concentration of the cryocondensates in fluids of the various USDOE Geopressured wells as a function of production volume, to correlate the production of these compounds with reservoir and well production characteristics, to precisely measure solubilities of cryocondensates components in water and sodium chloride solutions (brines) as a function of ionic strength and temperature and the component`s distribution coefficients between these solutions and oil, to develop models of the reservoir which are consistent with the data obtained, to monitor the wells for the production of aliphatic oils and relate any such production with the data obtained, and to develop a harsh environment pH probe for use in well brines. Results are summarized.

  4. Short-term energy outlook. Quarterly projections, first quarter 1996

    SciTech Connect

    1996-02-01

    The Energy Information Administration (EIA) prepares quarterly, short-term energy supply, demand, and price projections for publication in February, May, August, and November in the Outlook. The forecast period for this issue of the Outlook extends from the first quarter of 1996 through the fourth quarter of 1997. Values for the fourth quarter of 1995, however, are preliminary EIA estimates (for example, some monthly values for petroleum supply and disposition are derived in part from weekly data reported in the Weekly Petroleum Status Report) or are calculated from model simulations using the latest exogenous information available (for example, electricity sales and generation are simulated using actual weather data). The historical energy data, compiled into the first quarter 1996 version of the Short-Term Integrated Forecasting System (STIFS) database, are mostly EIA data regularly published in the Monthly Energy Review, Petroleum Supply Monthly, and other EIA publications. Minor discrepancies between the data in these publications and the historical data in this Outlook are due to independent rounding. The STIFS database is archived quarterly and is available from the National Technical Information Service. The cases are produced using the Short-Term Integrated Forecasting System (STIFS). The STIFS model is driven principally by three sets of assumptions or inputs: estimates of key macroeconomic variables, world oil price assumptions, and assumptions about the severity of weather. Macroeconomic estimates are produced by DRI/McGraw-Hill but are adjusted by EIA to reflect EIA assumptions about the world price of crude oil, energy product prices, and other assumptions which may affect the macroeconomic outlook.

  5. OTEC support services. Quarterly technical progress report No. 8, February 15-May 14, 1980

    SciTech Connect

    Lipari, M. V.

    1980-05-01

    Technical engineering and management support services provided by the VSE Corporation for the Ocean Thermal Energy Conversion Program of the Ocean Systems Branch, Division of Central Solar Technology are reported. Tasks include: (1) survey, analysis, evaluation, and recommendation concerning program performance; (2) program technical monitoring; (3) development and implementation of methodology to identify and evaluate program alternatives; (4) technical assessments; (5) OTEC system integration; (6) environment and siting considerations; and (7) transmission subsystem considerations. (WHK)

  6. Wetland treatment of oil and gas well wastewaters. Quarterly technical report, August 25--November 24, 1992

    SciTech Connect

    Kadlec, R.H.; Srinivasan, K.R.

    1992-12-24

    In this quarterly report, results of efforts on Tasks 2 and 3 are presented and discussed. Construction of a laboratory-type wetland (green house) has been begun and this undertaking is described in this report. The literature search has shown that clay amendments to wetlands are beginning to be used in Europe for P removal in agricultural drainage systems. The authors have undertaken similar studies on the use of inexpensive amendments to wetlands such as modified-clays and algae to enhance the performance of a constructed wetland for the treatment of oil and gas well wastewaters. The results from these studies are presented and analyzed in this report. Further, the literature search (nominally completed under Task 1) unearthed more recent studies (some unpublished) and a summary is included in this quarterly report.

  7. FETC/EPRI Biomass Cofiring Cooperative Agreement. Quarterly technical report, April 1-June 30, 1997

    SciTech Connect

    Hughes, E.; Tillman, D.

    1997-12-01

    The FETC/EPRI Biomass Cofiring Program has accelerated the pace of cofiring development by increasing the testing activities plus the support activities for interpreting test results. Past tests conducted and analyzed include the Allen Fossil Plant and Seward Generating Station programs. On-going tests include the Colbert Fossil Plant precommercial test program, the Greenidge Station commercialization program, and the Blount St. Station switchgrass program. Tests in the formative stages included the NIPSCO cofiring test at Michigan City Generating Station. Analytical activities included modeling and related support functions required to analyze the cofiring test results, and to place those results into context. Among these activities is the fuel availability study in the Pittsburgh, PA area. This study, conducted for Duquesne Light, supports their initial investigation into reburn technology using wood waste as a fuel. This Quarterly Report, covering the third quarter of the FETC/EPRI Biomass Cofiring Program, highlights the progress made on the 16 projects funded under this cooperative agreement.

  8. Methyl chloride via oxyhydrochlorination of methane. Quarterly technical progress report No. 10, January 1944--March 1994

    SciTech Connect

    1994-08-01

    In work related to the design and construction of the Process Development Unit (PDU) this quarter involved further detail design and a real start to the construction activities. Status updates are given below for each discipline in the Task 2.0 and 3.0 headings. This work is progressing well. with the caveat of several small slips in the scheduling. On the catalyst development front this quarter was extremely productive. Many catalyst screening experiments were completed and they showed that control of the reaction exotherm is going to be quite challenging under PDU conditions. The presence of much more efficient reactor design and the ability to maintain closer to isothermal conditions is expected to give a significant advantage in actual PDU operation. A major concern at the moment is the cost of La in the catalyst being used. An action plan to remedy this is being put together.

  9. [Geothermal system temperature-depth database and model for data analysis]. 5. quarterly technical progress report

    SciTech Connect

    Blackwell, D.D.

    1998-04-25

    During this first quarter of the second year of the contract activity has involved several different tasks. The author has continued to work on three tasks most intensively during this quarter: the task of implementing the data base for geothermal system temperature-depth, the maintenance of the WWW site with the heat flow and gradient data base, and finally the development of a modeling capability for analysis of the geothermal system exploration data. The author has completed the task of developing a data base template for geothermal system temperature-depth data that can be used in conjunction with the regional data base that he had already developed and is now implementing it. Progress is described.

  10. Energy efficient louver and blind. Technical progress report for Quarter 2, 1996

    SciTech Connect

    Khajavi, S.

    1996-07-26

    In this quarter we jumped ahead and performed Task 5 which is testing to get empirical energy saving data. One 4` X 3` horizontal Incredibling prototype and one black and one white conventional control blinds with the same size were delivered to the Lawrence Berekely Laboratories Mobile Test Facility in Reno. The blinds are still in testing since we had only two sunny days in the month of June and we encountered some hardware problem with the computers at the lab.

  11. Quarterly Performance/Technical Report of the National Marrow Donor Program

    DTIC Science & Technology

    2006-05-01

    typing can be used to design computer algorithms to predict the best matched donor. (B.3) Efforts of these Aims are to support the hypothesis that HLA...frequency data and primary DNA data can be used to predict the best-matched donor. Approaches to insure data validation and provide public...match prediction has been implemented as part of the HapLogic TM algorithm. During the past quarter software was implemented to predict the DRBI

  12. [Establishment and support of the International Power Institute]. Quarterly technical progress report, October--December, 1997

    SciTech Connect

    Coles, J.E.

    1998-04-02

    This is the quarterly report of the International Power Institute for October--December 1997. The topics of the report include pre-cooperative agreement activities, a discussion of the deputy director position, the IPI brochure, exploration of collaborative arrangements, formation of the IPI advisory board, a review of the advisory board meeting, report of a meeting with African electric utility executives, report of a visit to South Africa to explore a collaborative relationship.

  13. SRC-1 solvent-refined coal. Quarterly technical report, January-March 1980

    SciTech Connect

    Not Available

    1980-01-01

    Four papers in this quarterly report have been entered individually into EDB and ERA. They deal with reducing organic solvent losses in the Kerr-McGee solvent deashing process; with the design of heaters for the process (which involved determining the temperature dependence of the enthalpy of the organic solvent, coal and hydrogen mixture); with a review of the carbon dioxide greenhouse effect on global climates; and with a methodology for fractionating and evaluating the coal liquids produced. (LTN)

  14. Quarterly Performance/Technical Report of the National Marrow Donor Program

    DTIC Science & Technology

    2011-01-28

    quarter 2011: o KIR-DS, CIBMTR Sample Tracking Application , 09 MRD Study • All Audit Recipient module development milestones are complete...CSS Custom Search Support PSA Public Service Announcement CT Confirmatory Testing PT Proficiency Testing CTA Clinical Trial Application QAMS Quality...the first week of October 2010 with a Recovery Time of 42 hours. Tier 1 is comprised of the following Core Business critical applications and

  15. Advanced separation technology for flue gas cleanup. Quarterly technical report No. 8, [January--March 1994

    SciTech Connect

    Bhown, A.S.; Alvarado, D.; Pakala, N.; Ventura, S.; Sirkar, K.K.; Majumdar, S.; Bhaumick, D.

    1994-03-01

    During the first quarter of 1994, we continued work on Tasks 2, 3, 4, 5, and 6. We also began work on Task 7. In Task 2, we incorporated 4.5% O{sub 2} into our simulated flue gas stream during this quarter`s NO{sub x}-absorption experiments. We also ran experiments using Cobalt (II)-phthalocyanine as an absorbing agent We observed higher absorption capacities when using this solution with the simulated flue gas containing O{sub 2}. In Task 3, we synthesized a few EDTA polymer analogs. We also began scaled up synthesis of Co(II)-phthalocyanine for use in Task 5. In Task 4, we performed experiments for measuring distribution coefficients (m{sub i}) Of SO{sub 2} between aqueous and organic phases. This was done using the liquor regenerating apparatus described in Task 6. In Task 5, we began working with Co(II)-phthalocyanine in the 301 fiber hollow fiber contactor. We also calculated mass transfer coefficients (K{sub olm}) for these runs, and we observed that the gas side resistance dominates mass transfer. In Task 6, in the liquor regeneration apparatus, we observed 90% recovery of SO{sub 2} by DMA from water used as the scrubbing solution. We also calculated the distribution of coefficients (m{sub i}). In Task 7, we established and began implementing a methodology for completing this task.

  16. Particulate hot gas stream cleanup technical issues. Quarterly report, April 1 - June 30, 1996

    SciTech Connect

    1996-12-31

    This is the seventh in a series of quarterly reports describing the activities performed for this project. Our analyses of Hot Gas Stream Cleanup (HGCU) ashes and descriptions of filter performance address aspects of filter operation that are apparently linked to the characteristics of the collected ash or the performance of the ceramic barrier filter elements. Task 1 is designed to generate a data base of the key characteristics of ashes collected from operating advanced particle filters (APFs) and to relate these ash properties to the operation and performance of these filters. Task 2 concerns testing and failure analysis of ceramic filter elements. Under Task 1 during the past quarter, we received and analyzed a hopper ash sample from the Transport Reactor Demonstration Unit (TRDU) located at the University of North Dakota`s Energy and Environmental Research Center (UNDEERC). We also received six ash samples from the Ahlstrom 10 MWt Pressurized Fluidized Circulating Fluid Bed (PCFB) facility located at Karhula, Finland. We selected one of the filter cake ashes from this batch of samples for detailed analyses. We continued our work on the HGCU data base we are constructing in Microsoft Access{reg_sign}. We have been entering a variety of information into the data base, including numerical values, short or long text entries, and photographs. Task 2 efforts during the past quarter focused on hoop tensile testing of Schumacher FT20 and Refractron candle filter elements removed from the Karhula APF after {approximately}540 hours of service.

  17. OTEC support services. Quarterly technical progress report No. 20, 15 February - 14 May 1983

    SciTech Connect

    Not Available

    1983-01-01

    The following task areas are described briefly for the system integration, system engineering, and management services provided for the OTEC program: (1) survey, analysis and evaluation; (2) program technical monitoring; (3) development and implementation of methodology; (4) technical assessment; (5) OTEC systems integration; (6) environment and siting considerations; and (7) transmission subsystem considerations.

  18. OTEC support services. Quarterly technical progress report No. 21, 15 May-15 August 1983

    SciTech Connect

    Not Available

    1983-09-01

    Progress is reported on the system integration, system engineering, and management services for the OTEC program under the following tasks: (1) survey, analysis, and evaluation; (2) program technical monitoring; (3) development and implementation of methodology; (4) technical assessments; (5) OTEC systems integration; (6) environment and siting considerations; and (7) transmission subsystem considerations.

  19. Development and Evaluation of an Experimental Curriculum for the New Quincy (Mass.) Vocational-Technical School. First Quarterly Technical Report.

    ERIC Educational Resources Information Center

    Morrison, Edward J.

    Technical activity from April 1 through June 30, 1965 was concentrated in behavior analysis and guidance program development. The behavior analysis involved identifying 1,051 jobs as candidates for inclusion in the training program and grouping them into 30 sub-families on the basis of task similarities. Data necessary for decision to include the…

  20. Separation of flue-gas scrubber sludge into marketable products. Second year, fourth quarterly technical progress report, Quarter No. 8, June 1, 1995--August 31, 1995

    SciTech Connect

    Kawatra, S.K.; Eisele, T.C.

    1995-09-01

    To reduce their sulfur emissions, many coal-fired electric power plants use wet flue-gas scrubbers. These scrubbers convert sulfur oxides into solid sulfate and sulfite sludge, which must then be disposed of. This sludge is a result of reacting limestone with sulfur dioxide to precipitate calcium sulfite and calcium sulfate. It consists of calcium sulfite (CaSO{sub 3}{sm_bullet}0.5H{sub 2}O), gypsum (CaSO{sub 4}{sm_bullet}2H{sub 2}O), and unreacted limestone (CaCO{sub 3}) or lime (Ca(OH){sub 2}), with miscellaneous objectionable impurities such as iron oxides, silica, and magnesium, sodium, and potassium oxides or salts. These impurities prevent many sludges from being utilized as a replacement for natural gypsum, and as a result they must be disposed of in landfills, which presents a serious disposal problem. Knowledge of scrubber sludge characteristics is necessary for the development of purification technologies which will make it possible to directly utilize scrubber sludges rather than landfilling them. This project is studying the use of minimal-reagent froth flotation as the purification process, using the surface properties of the particles of unreacted limestone to remove them and their associated impurities from the material, leaving a purified calcium sulfite/gypsum product.

  1. Separation of flue-gas scrubber sludge into marketable products. Fourth year, first quarterly technical progress report, September 1, 1996--December 31, 1996 (Quarter No. 13)

    SciTech Connect

    Kawatra, S.K.; Eisele, T.C.

    1996-12-01

    To reduce their sulfur emissions, many coal-fired electric power plants use wet flue-gas scrubbers. These scrubbers convert sulfur oxides into solid sulfate and sulfite sludge, which must then be disposed of. This sludge is a result of reacting limestone with sulfur dioxide to precipitate calcium sulfite and calcium sulfate. It consists of calcium sulfite (CaSO{sub 3}{circ}0.5H{sub 2}O), gypsum (CaSO{sub 4}{circ}2H{sub 2}O), and unreacted limestone (CaCO{sub 3}) or lime (Ca(OH)2), with miscellaneous objectionable impurities such as iron oxides, silicates, and magnesium, sodium, and potassium oxides or salts. These impurities prevent many sludges from being utilized as a replacement for natural gypsum, and as a result they must be disposed of in landfills, which presents a serious disposal problem. Knowledge of scrubber sludge characteristics is necessary for the development of purification technologies which will make it possible to directly utilize scrubber sludges rather than landfilling them. This project is studying the use of minimal-reagent froth flotation as the purification process, using the surface properties of the particles of unreacted limestone to remove them and their associated impurities from the material, leaving a purified calcium sulfite/gypsum product.

  2. Identification and Evaluation of Fluvial-Dominated Deltaic Reservoirs. Quarterly technical report, January 1-March 31, 1997

    SciTech Connect

    Banken, M.K.; Andrews, R.

    1997-09-12

    This document is provided as a Quarterly Technical Progress Report for the program entitled `Identification and Evaluation of Fluvial- Dominated Deltaic (Class 1 Oil) Reservoirs in Oklahoma`, covering the reporting period of January 1 - March 31, 1997. Work is progressing as expected for the project. The FDD computer facility is fully operational. During this quarter, there were 28 industry `visits` to use the facility. The Red Fork Play workshop was completed on March 5 in Norman, and on March 12, 1997 in Bartlesville, with a total of 195 attendees. The Tonkawa Play workshop is scheduled for July 9, 1997 in Norman. The Tonkawa text, figures, maps, and plates are in preparation. The Bartlesville workshop is scheduled for October, 1997, although the exact time and place have yet to be determined. Regional work and field studies for that play are in progress. This project is serving an extremely valuable role in the technology transfer activities for the Oklahoma petroleum industry, with very positive industry feedback.

  3. Hot gas cleanup test facility for gasification and pressurized combustion. Quarterly technical progress report, April 1--June 30, 1992

    SciTech Connect

    Not Available

    1992-12-01

    This quarterly technical progress report summarizes work completed during the Seventh Quarter of the First Budget Period, April 1 through June 30, 1992, under the Department of Energy (DOE) Cooperative Agreement No. DE-FC21-90MC25140 entitled ``Hot Gas Cleanup Test Facility for Gasification and Pressurized Combustion.`` The conceptual design of the facility was extended to include a within scope, phased expansion of the existing Hot Gas Cleanup Test Facility Cooperative Agreement to also address systems integration issues of hot particulate removal in advanced coal-based power generation systems. This expansion will include the consideration of the following modules at the test facility in addition to the existing Transport Reactor gas source and Hot Gas Cleanup Units: Carbonizer/Pressurized Circulating Fluidized Bed Gas Source; Hot Gas Cleanup Units to mate to all gas streams. Combustion Gas Turbine; Fuel Cell and associated gas treatment; and Externally Fired Gas Turbine/Water Augmented Gas Turbine. This expansion to the Hot Gas Cleanup Test Facility is herein referred to as the Power Systems Development Facility (PSDF).

  4. Coal-fired MHD combustor development project: Phase IIIB. First quarterly technical progress report, 13 January-30 April 1982

    SciTech Connect

    1982-05-20

    The first quarterly technical progress report of the Coal-Fired MHD Combustor Development Project (Phase IIIB) presents the accomplishments during the period 13 January to 30 April, 1982. The scope of work covered by this quarterly report relates to those tasks associated with preparing the TRW 20 MW/sub t/ MHD coal combustor for delivery to AERL for integrated power tests and the work associated with the preliminary design of a 50 MW/sub t/ coal-fired combustor. Progress during this reporting period is described. All new 20 MW/sub t/ hardware was designed and fabricated. Interface coordination meetings were conducted with AERL and DOE. Interface control drawings were completed and a 20 MW/sub t/ coal combustion User's manual was delivered to AERL. The User's manual contained a shipping plan, a crew training plan, an assembly manual, interface documentation and recommended operating procedures. Facility/combustor set-up was completed and the pre-delivery 20 MW/sub t/ coal combustor qualification test series was completed. The 50 MW/sub t/ coal-fired MHD combustor preliminary designs were finalized and the DOE preliminary design review (PDR) was successfully completed.

  5. CO{sub 2} Huff-n-Puff process in a light oil shallow shelf carbonate reservoir. Quarterly technical progress report, October--December 1996

    SciTech Connect

    Wehner, S.; Prieditis, J.

    1996-12-31

    The principal objective of the Central Vacuum Unit (CVU) CO{sub 2} Huff-n-Puff (H-n-P) project is to determine the feasibility and practicality of the technology in a waterflooded shallow shelf carbonate environment. The results of parametric simulation of the CO{sub 2} H-n-P process, coupled with the CVU reservoir characterization components will be used to determine if this process is technically and economically feasible for field implementation. The technology transfer objective of the project is to disseminate the knowledge gained through an innovative plan in support of the Department of energy`s (DOE) objective of increasing domestic oil production and deferring the abandonment of shallow shelf carbonate reservoirs. Texaco Exploration and Production Inc`s. (TEPI) mid-term plans are to implement a full-scale miscible CO{sub 2} project in the CVU. TEPI concluded all of the tasks associated with the First Budget Period by October, 1995. The DOE approved the TEPI continuation application. Budget Period No. 2 is in progress. Initial injection of CO{sub 2} began in November, and after a short shut-in period for the soak, the well was returned to production in late December, 1995. This report, covers TEPI`s efforts at history matching the results of the field demonstration. Costs and economics of the work are presented. The majority of effort during the fourth quarter has revolved around the selection of a new project site and refinement of the demonstration design and well selection.

  6. Molecular biological enhancement of coal biodesulfurization. Quarterly technical report, September 1, 1993--November 30, 1993

    SciTech Connect

    Kilbane, J.J. II

    1993-12-31

    IGT has developed a microbial culture of Rhodococcus rhodochrous, designated as IGTS8, that is capable of specifically cleaving carbon-sulfur bonds in a range of organosulfur model compounds and is capable of removing organic sulfur from coal and petroleum without significantly sacrificing the calorific value of the fuel. Although IGTS8 possesses the ability to specifically remove organic sulfur from coal, a major research need is to develop improved strains of microorganisms that possess higher levels of desulfurization activity and therefore will permit more favorable biodesulfurization process conditions: faster rates, more complete removal, and smaller reactor size. strain improvement is the single most important aspect to the development of a practical coal biodesulfurization process and accordingly is the focus of research in this project. During this quarter the promoter probe vectors that were constructed last quarter were found to be unstable in E. coli. Fragments of R. rhodochrous IGTS8 chromosomal DNA were cloned into pRCAT3 and pRCM1 (previously described in final ICCI report 1993). Many derivatives of pRCM1 and pRCAT3 receiving inserts that regulated the expression of chloramphenicol resistance in Rhodococcus rhodochrous IGTS8 proved to be unstable in E. coli frequently yielding plasmids containing deletions. Stable inserts have been observed ranging from 100 bp to 2.0 kb that regulated expression in Rhodococcus rhodochrous IGTS8. Subtractive hybridization studies continue, several candidates have been isolated and are being confirmed for inducible promoters. Primer extension analysis of the Rhodococcus rhodochrous IGTS8 16S RNA promoter region was initiated this quarter.

  7. Robotic weld overlay coatings for erosion control. Quarterly technical progress report, October 1994--December 1994

    SciTech Connect

    Levin, B.F.; Dupont, J.N.; Marder, A.R.

    1995-01-25

    Research is presently being conducted to develop a criteria for selecting weld overlay coatings for erosion mitigation in Circulated Fluidized Beds. Initially, eleven weld overlay alloys were selected for erosion testing based upon a literature review. All eleven coatings were deposited on 1018 steel substrates using the plasma arc welding process. Ten samples from each coating were prepared for erosion testing. The coating deposition and sample preparation procedures were described in the second quarterly report. All selected coatings were erosion tested at 400{degree}C and their erosion resistance was evaluated by determining the steady state erosion rate. In addition, the microstructure of each coating was characterized before and after the erosion tests. The results of the tests are discussed in the third quarterly report. No correlations were found between room temperature hardness of the weld overlay coatings and their erosion resistance at elevated temperature. During the last quarter tensile tests were performed at 400{degree}C for the Ultimet, Inconel-625, 316L SS, C-22, and Stellite-6 wrought alloys. The erosion tests for these materials at 400{degree}C are in progress. The results of mechanical and erosion tests will be used to correlate mechanical properties of selected wrought alloys such as tensile toughness, ductility, strain hardening coefficient and yield strength to their erosion resistance at 400{degree}C. Also, the erosion behavior of the wrought alloys compared with similar weld alloys will be analyzed. The experimental procedure and results of the tensile tests are presented in this progress report.

  8. Regulatory and technical reports (abstract index journal): Compilation for third quarter 1996 July--September. Volume 21, Number 3

    SciTech Connect

    1997-02-01

    This compilation consists of bibliographic data and abstracts for the formal regulatory and technical reports issued by the US Nuclear Regulatory Commission (NRC) Staff and its contractors. It is NRC`s intention to publish this compilation quarterly and to cumulate it annually. The main citations and abstracts in this compilation are listed in NUREG number order: NUREG-XXXX, NUREG/CP-XXXX, NUREG/CR-XXXX, and NUREG/IA-XXXX. These precede the following indexes: secondary report number index; personal author index; subject index; NRC originating organization index (staff reports); NRC originating organization index (international agreements); NRC contract sponsor index (contractor reports); contractor index; international organization index; and licensed facility index. A detailed explanation of the entries precedes each index.

  9. Regulatory and technical reports (abstract index journal): Compilation for third quarter 1994, July--September. Volume 19, Number 3

    SciTech Connect

    1994-12-01

    This compilation consists of bibliographic data and abstracts for the formal regulatory and technical reports issues by the U.S. Nuclear Regulatory Commission (NRC) Staff and its contractors. It is NRC`s intention to publish this compilation quarterly and to cumulate it annually. The main citations and abstracts in this compilation are listed in NUREG number order: NUREG-XXXX, NUREG/CP-XXXX, NUREG/CR-XXXX, and NUREG/IA-XXXX. These precede the following indexes: Secondary Report Number Index, Personal Author Index, Subject Index, NRC Originating Organization Index (Staff Reports), NRC Originating Organization Index (International Agreements), NRC Contract Sponsor Index (Contractor Reports) Contractor Index, International Organization Index, Licensed Facility Index. A detailed explanation of the entries precedes each index.

  10. Robotic weld overlay coatings for erosion control. Quarterly technical progress report, April 1993--June 1993

    SciTech Connect

    Levin, B.F.; Dupont, J.N.; Marder, A.R.

    1993-07-20

    Twelve weld overlay hardfacing alloys have been selected for preliminary erosion testing based upon a literature review. Four of the selected coatings were deposited on a 1018 steel substrate using plasma arc welding process. During the past quarter, the remaining eight coatings were deposited in the same manner. Ten samples from each coatings were prepared for erosion testing. Microstructural characterization of each coating is in progress. This progress report describes coating deposition and sample preparation procedures. Relation between coatings hardness and formation of cracks in coatings is discussed.

  11. Novel concepts in electrochemical solar cells. Quarterly technical progress report, December 15, 1980-March 15, 1981

    SciTech Connect

    Not Available

    1981-01-01

    During the past quarter, the following areas were emphasized: (a) characterization of redox couples with very positive potentials in room-temperature AlCl/sub 3/-BPC electrolytes and comparison of the electrochemical behavior of decamethyl ferrocene in these electrolytes with the previously-studied ferrocene/ferricenium ion couple, (b) photoelectrochemical characterization of CdSe thin-film anodes in aqueous polysulfide electrolytes and (c) refinement of the admittance measurement technique for extraction of Mott-Schottky parameters. The results of research in these areas are detailed in turn below.

  12. Mild coal pretreatment to improve liquefaction reactivity. Quarterly technical progress report, September--November 1991

    SciTech Connect

    Miller, R.L.

    1991-12-31

    This report describes work completed during the fifth quarter of a three year project to study the effects of mild chemical pretreatment on coal dissolution reactivity during low severity liquefaction or coal/oil coprocessing. The overall objective of this research is to elucidate changes in the chemical and physical structure of coal by pretreating with methanol or other simple organic solvent and a trace amount of hydrochloric acid and measure the influence of these changes on coal dissolution reactivity. Work this quarter focused on analytical characterization of untreated and treated Wyodak subbituminous coal and Illinois {number_sign}6 bituminous coal. Mossbauer spectroscopy and x-ray diffraction techniques were used to study the effect of methanol/HCl pretreatment on the composition of each coal`s inorganic phase. Results from these studies indicated that calcite is largely removed during pretreatment, but that other mineral species such as pyrite are unaffected. This finding is significant, since calcite removal appears to directly correlate with low severity liquefaction enhancement. Further work will be performed to study this phenomenon in more detail.

  13. Cuprous oxide photovoltaic cells. Third quarterly technical progress report, October 9, 1979 to January 8, 1980

    SciTech Connect

    Trivich, D.

    1980-01-08

    Previous work in this laboratory on cuprous oxide Schottky barrier photovoltaic cells showed that some potential improvements were limited by chemical degradations at the junction (1), e.g., in Al/Cu/sub 2/O cells, the aluminum reduced the surface of the Cu/sub 2/O to metallic Cu. The present project is being devoted to a study of methods to avoid this problem and also to the development of other methods of improving the efficiency of Cu/sub 2/O cells. The first quarterly report was devoted to a study of thin oxide interlayers between the metal and the Cu/sub 2/O which gives MIS structures. The most stable interlayers were obtained with SiO/sub 2/. The second quarterly report covered some initial work on heterojunctions with other oxides on Cu/sub 2/O. The most stable heterojunctions were obtained with CdO on Cu/sub 2/O. The present report presents some results on Auger studies of the oxide heterojunctions, the preparation of doped Cu/sub 2/O by introduction of impurities in the starting copper, the exploration of several method for the study of diffusion length, and some initial attempts on the laser annealing of Cu/sub 2/O.

  14. Commercialization of atom interferometers for borehole gravity gradiometry. Quarterly technical progress report, October--December 1992

    SciTech Connect

    Clauser, J.F.

    1993-01-30

    Perform a mathematical analysis of the tomography inversion problem for various configurations of a borehole gravity gradiometer. Our simulations typically call for logging a hole for about 4km of depth. Within the limits imposed by our presumed detector sensitivity, the device appears to be capable of measuring the 0.1 g/cm{sup 3} density in all rings to about 10% accuracy, with the rings extending out to about 500 meters from the hole. At this range, the vertical resolution has dropped to about 50m. Closer to the hole, the resolution improves so that we can determine the density in each of about 400 rings. We anticipate that this most important task (No. l) will be complete within the next quarter.

  15. Pulsed atmospheric fluidized bed combustion. Quarterly technical progress report, July 1992--September 1992

    SciTech Connect

    Not Available

    1992-10-01

    The design of the Pulsed Atmospheric Fluidized Bed Combustor (PAFBC) as described in the Quarterly Report for the period April--June, 1992 was reviewed and minor modifications were included. The most important change made was in the coal/limestone preparation and feed system. Instead of procuring pre-sized coal for testing of the PAFBC, it was decided that the installation of a milling system would permit greater flexibility in the testing with respect to size distributions and combustion characteristics in the pulse combustor and the fluid bed. Particle size separation for pulse combustor and fluid bed will be performed by an air classifier. The modified process flow diagram for the coal/limestone handling system is presented in Figure 1. The modified process flow diagrams of the fluidized bed/steam cycle and ash handling systems are presented in Figures 2 and 3, respectively.

  16. Fischer Tropsch synthesis in supercritical fluids. Quarterly technical progress report, October 1, 1993--December 31, 1993

    SciTech Connect

    Akgerman, A.; Bukur, D.B.

    1993-12-31

    Objectives for the first quarter for Task A, Diffusion Coefficients of F-T Products in Supercritical Fluids, were to measure diffusion coefficients of 1-tetradecene in subcritical propane and the diffusion coefficients of 1-octene and 1-tetradecene in subcritical propane and the diffusion coefficients of 1-octene and 1-tetradecene in subcritical and supercritical ethane. We planned to use ethane as a solvent because its lower critical temperature enabled measurements without modification of the existing unit. Our objective was to investigate the behavior of the diffusion coefficients in crossing from subcritical to supercritical conditions. Objectives for Task B, Fischer Tropsch reaction related studies, were: (1) to install and test the temperature probe and the flammable gas detector: (2) to conduct Fischer-Tropsch experiments at baseline conditions and at a high pressure in order to test the newly constructed fixed bed reactor assembly. Accomplishments and problems, are presented.

  17. Coal-feeder development. Second quarterly technical progress report, January-March 1980

    SciTech Connect

    Mistry, D.K.

    1981-04-01

    The pilot-scale piston-feeder development is progressing satisfactorily and should proceed as planned. The bench scale testing of components, sub-system and critical areas continued to provide very useful information in support of the development of the complete feeder. The K30M seals and polyurethane scrapers are showing very promising results. The components development facility is being upgraded and testing at the bench scale level should be vigorously perused. The upgrading of the pilot scale feeder and its system will be emphasized during the next quarter to perform feeder capabilities and limitations testing. No progress on the 5.5-in. diameter pilot scale screw feeder has been made because IRRI is waiting decision from METC as to when the feeder can be installed on the 42-in. gas producer.

  18. Pulsed atmospheric fluidized bed combustion. Quarterly technical progress report, April--June 1993

    SciTech Connect

    Not Available

    1993-07-30

    In this quarter the design of the plant structures was completed 70%. The design philosophy of the structure economizes on the use of steel by providing supports for the hot cyclone and hot gas duct connecting the cyclone to the boiler while fulfilling the needs for platforms and walkways at the various levels necessary for operational access. Figures 1 through 6 indicate the layout of the plant structure. At the same time the structure for the Coarse Coal Silo V-2 and Limestone Silo V-4 were incorporated and completed. Following completion of the piping pressure drop calculations, pipe sizing and layout drawings, detailed drawings of the piping in different views are being prepared. The pulse combustor is used to burn fine coal particles and provide an ignition source and supplementary heat to the fluid bed. The following is a description of the components: air plenum, fine coal injectors, aerovalves, water jacket, and tailpipe inserts.

  19. OTEC support services. Quarterly technical progress report No. 9, 15 May-14 August 1980

    SciTech Connect

    1980-08-01

    System integration, system engineering, and management support services provided by the VSE Corporation for the Ocean Thermal Energy Conversion Program of the Ocean Systems Branch, Division of Central Solar Technology, DOE are described. The services are provided under seven task areas: (1) survey, analysis, evaluation, and recommendation concerning program performance; (2) program technical monitoring; (3) development and implementation of methodology to identify and evaluate program alternatives; (4) technical assignments; (5) OTEC system integration; (6) environment and siting considerations; and (7) transmission subsystem considerations. (WHK)

  20. Development of analytical procedures for coprocessing. Quarterly technical progress report, April 1, 1991--June 30, 1991

    SciTech Connect

    Green, J.B.; Anderson, R.P.

    1991-07-01

    The overall objective of the contract is to improve understanding of the fundamental chemistry of coprocessing. A primary objective is to evaluate methods to distinguish between compound classes originating from coal versus those originating from petroleum resid while a corollary objective is to provide detailed knowledge on the composition of coprocessing products. This and the prior quarterly report summarize work conducted in support of the latter objective in which process development unit samples produced by HRI, Inc. were subjected to detailed analysis. Coprocessing resid samples selected for detailed analysis were made under constant conditions except for variations in coal concentration or in the coal (New Mexico subbituminous or Texas lignite). Separation of the resids into acid, base, saturate, and neutral-aromatic subtractions, separation of the neutral-aromatics by ring number and high temperature gas chromatography were discussed in the previous quarterly. This report includes results of nonaqueous titrations, elemental analyses and infrared spectroscopy. The hydrocarbon skeletons of saturated hydrocarbons in the coprocessing resids appear to be fundamentally different than those of aromatic species. Neutral-aromatic fractions contain minor levels of sulfur compounds, an unknown proportion of ether or other oxygen-containing species, and major concentrations of aromatic hydrocarbons containing from 3 to 7 aromatic rings. Base fractions contain predominantly single nitrogen compounds of azaarene or aminoaromatic type. Aminoaromatics (compounds analogous to aniline) are present in significant amounts in products made from New Mexico subbituminous coal but are nearly absent in the Texas lignite product. Acid fractions contain appreciable quantities of pyrrolic benzologs, but surprisingly low concentrations of compounds with a free OH group.

  1. Particulate hot gas stream cleanup technical issues. Quarterly report, January 1--March 31, 1998

    SciTech Connect

    1998-08-01

    The analyses of Hot Gas Stream Cleanup (HGCU) ashes and descriptions of filter performance studied under this contract are designed to address problems with filter operation that are apparently linked to characteristics of the collected ash. Task 1 is designed to generate a data base of the key characteristics of ashes collected from operating advanced particle filters (APFs) and to relate these ash properties to the operation and performance of these filters and their components. APF operations have also been limited by the strength and durability of the ceramic materials that have served as barrier filters for the capture of entrained HGCU ashes. Task 2 concerns testing and failure analyses of ceramic filter elements currently used in operating APFs and the characterization and evaluation of new ceramic materials. Task 1 research activities during the past quarter included characterizations of samples collected during a site visit on January 20 to the Department of Energy/Southern Company Services Power Systems Development Facility (PSDF). Comparisons were made between laboratory analyses of these PSDF ashes and field data obtained from facility operation. In addition, selected laboratory techniques were reviewed to assess their reproducibility and the influence of non-ideal effects and differences between laboratory and filter conditions on the quantities measured. Further work on the HGCU data base is planned for the next quarter. Two Dupont PRD-66 candle filters, one McDermott candle filter, one Blasch candle filter, and one Specific Surfaces candle filter were received at SRI for testing. A test plan and cutting plan for these candles was developed. Acquisition of two of the Dupont PRD-66 candle filters will allow candle-to-candle variability to be examined.

  2. Responsive copolymers for enhanced petroleum recovery. Quarterly technical progress report, September 22, 1992--December 22, 1992

    SciTech Connect

    McCormick, C.; Hester, R.

    1992-12-31

    The overall goal of this research is the development of advanced water-soluble copolymers for use in enhanced oil recovery which rely on reversible microheterogeneous associations for mobility control and reservoir conformance. Technical progress is summarized for the following tasks: advanced copolymer synthesis; characterization of macromolecular structure and properties; and solution rheology in a porous media.

  3. Educational Technology Program. Quarterly Technical Summary Report, March 31 through May 31, 1971.

    ERIC Educational Resources Information Center

    Frick, Frederick C.

    The report describes hardware and software development for Lincoln Training System #3 (LTS-3) at M.I.T.'s Lincoln Laboratory. The report provides specifications of an LTS-3 student console, and describes refinements of LTS-3 teaching techniques and lesson materials resulting from a test of the system at a U. S. Air Force technical training school.…

  4. Amarillo National Resource Center for Plutonium. Quarterly technical progress report, May 1--July 31, 1998

    SciTech Connect

    1998-09-01

    Progress is reported on research projects related to the following: Electronic resource library; Environment, safety, and health; Communication, education, training, and community involvement; Nuclear and other materials; and Reporting, evaluation, monitoring, and administration. Technical studies investigate remedial action of high explosives-contaminated lands, radioactive waste management, nondestructive assay methods, and plutonium processing, handling, and storage.

  5. Responsive copolymers for enhanced petroleum recovery. Quarterly technical progress report, December 22, 1992--March 21, 1993

    SciTech Connect

    Hester, R.; McCormick, C.

    1993-06-01

    The overall objective of this research is the development of advanced water-soluble copolymers for use in enhanced oil recovery which rely on reversible microheterogeneous associations for mobility control and reservoir conformance. Technical progress is summarized for the following tasks: advanced copolymer synthesis; characterization of molecular structure; and solution rheology.

  6. Technical progress report for the quarter 1 October-31 December 1980

    SciTech Connect

    Not Available

    1981-01-01

    This report describes the technical accomplishments on the commercial nuclear waste management programs and on the geologic disposal of nuclear wastes. The program is organized into eight tasks: systems, waste package, site, repository, regulatory and institutional, test facilities and excavations, land acquisition, and program management. (DLC)

  7. Educational Technology Program. Quarterly Technical Summary, Period Ending 31 May 1970.

    ERIC Educational Resources Information Center

    Frick, Frederick C.

    An overview of the Lincoln Training System (LTS) and descriptions of the hardward and software of the LTS-1 and LTS-2 systems are provided. The overall program seeks to develop, test, and evaluate technical aids to vocational training systems. These are appropriate to this field because the high costs need to be reduced and because there are clear…

  8. [Gas cooled fuel cell systems technology development program]. Quarterly technical progress narrative No. 30, March 1, 1990--May 31, 1990

    SciTech Connect

    Not Available

    1990-06-01

    This report addresses the fourth logical unit of work of a multiyear program whose overall objective is the development of a gas-cooled phosphoric acid fuel cell (PAFC) for electric utility power plant application. This PAFC Technology Development Program continuation is structured to build upon the current cell technology baseline so as to advance critical component technologies to meet the performance, endurance, reliability and cost goals associated with successful energy service. The primary technical objectives established for achievement in the fourth logical unit of the program, estimated to cover the period August 24, 1987 through December 1991 inclusive, are: (1) Demonstrate performance endurance of current cell technology in 10-cell stacks at 70 psia, 190{degree}C, and 267 mA/cm{sup 2}. (2) Select and utilize materials, procedures, and methods that improve cell degradation rate to less than 8 mV/1000 hours. (3) Develop cost-effective criteria, processes, and design configurations for stack components. (4) Develop design configuration for multiple stack unit and a single 100 kW size fuel cell stack and attain performance goals. (5) Develop design configuration for a 375 kW fuel cell module and demonstrate by test the average cell beginning-of-use performance objectives. (6) Manufacture two 375 kW fuel cell modules and establish performance characteristics and interactions with other systems in a pilot power plant.

  9. Short-term energy outlook. Quarterly projections, second quarter 1996

    SciTech Connect

    1996-04-01

    The Energy Information Administration prepares quarterly, short-term energy supply, demand, and price projections. The forecasts in this issue cover the second quarter of 1996 through the fourth quarter of 1997. Changes to macroeconomic measures by the Bureau of Economic Analysis have been incorporated into the STIFS model used.

  10. A novel carbon-based process for flue gas cleanup. Fifth quarterly technical progress report, July 1--September 30, 1992

    SciTech Connect

    Gangwal, S.K.; Silveston, P.L.

    1992-10-01

    The objective of this project is to demonstrate the preliminary technical and economic feasibility of a novel carbon-based process for removal of at least 95% S0{sub 2} and at least 75 % NO{sub x}, from coal combustion flue gas. In the process, flue gas leaving the electrostatic precipitator (ESP) is passed through a trickle bed of activated carbon catalyst employing a periodic flush of low strength sulfuric acid. The S0{sub 2} is oxidized to S0{sub 3} and removed as medium strength sulfuric acid. The S0{sub 2}-free flue gas is then mixed with NH{sub 3}, and the NO{sub x} in the gas is subjected to selective catalytic reduction (SCR) to N{sub 2} over a fixed bed of activated carbon catalyst. In the previous four quarters, a detailed project management plan was prepared describing the experimental setup, work plan, and test plan. The experimental system was completed for SO{sub 2} conversion at Waterloo and for NO{sub x} conversion at Research Triangle Institute. Shakedown experiments were completed. The NO{sub x} removal performance of two additional modified carbon catalysts (MCCII and MCCIII) was studied. MCCII showed NO{sub 2} removal efficiency which was similar to that observed for MCCI. However, MCCIII was considerably less active for NO{sub x} removal. In the present quarter, further tests of MCCI were performed for SO{sub 2} removal with NO in the feed gas, except the reactor was operated at 130{degrees}C (instead of 80{degrees}C during previous tests). Tests were also performed with MCCII for NO removal with nominally 100 ppm SO{sub 2} in the feed gas.

  11. ERIP invention 637. Technical progress report 2nd quarter, April 1997--June 1997

    SciTech Connect

    Thacker, G.W.

    1997-07-22

    This technical report describes progress in the development of the Pegasus plow, a stalk and root embedding apparatus. Prototype testing is reported, and includes the addition of precision tillage. Disease data, organic matter, and nitrogen levels results are very briefly described. Progress in marketing is also reported. Current marketing issues include test use by cotton and wheat growers, establishment of dealer relationships, incorporation of design modifications, expansion of marketing activities, and expansion of loan and lease program.

  12. Low-cost-silicon-process development. Phase IV: process improvement. Second quarterly technical progress report

    SciTech Connect

    Giraudi, R. V.; Newman, C. G.

    1981-04-01

    A number of promising techniques for improving the overall yield and economics of the tribromosilane based process to produce solar cell grade silicon is investigated. The current work is aimed at the identification of an optimum process and the characterization of that process through mini-plant operation and analysis. The three project tasks include process improvement studies, kinetic studies, and process economic studies. During this second quarter reporting period process improvement studies continued in the mini-plant, focusing on the correlation of current mini-plant yield results with prior laboratory scale work. Silicon bromination in the synthesis unit and tribromosilane purification in the distillation unit proceeded efficiently and without complication during this reporting period. Tribromosilane yields in the synthesis unit were low due to unobtainable higher reaction temperatures. Initial polycrystalline silicon production studies have indicated consistent yields of 85%. The laboratory scale static bulb reactor system was calibrated by observing the decomposition of t-butyl chloride. These results compared very well to results obtained by previous investigators for the same decomposition. Upon the conclusion of the calibration tests, the tribromosilane decomposition rate study was initiated. Two decompositions were completed and it was concluded that the reaction order can not be determined at this time. A free space reactor apparatus was assembled and tribromosilane decompositions, as a function of dilution in argon, was studied.

  13. Mild pyrolysis of selectively oxidized coals. [Quarterly] technical report, March 1, 1992--May 31, 1992

    SciTech Connect

    Hippo, E.J.; Palmer, S.R.

    1992-10-01

    The primary objective of this study is to investigate the removal organic sulfur from selectively oxidized Illinois coals using mild thermal/chemical processes. Work completed this quarter primarily concerned the investigation of the desulfurization of the selectively oxidized coals using aqueous or alcoholic base mixtures. Model compound studies were initiated. Results were: Levels of desulfurization obtained in this study are at, or very close to, the 90% removal levels required for these coals to be in compliance with the Clean Air Act legislation; Up to 89.4% of the sulfur in the IBC 101 coal and 88.9% of the sulfur in the IBC 106 coal has been removed by combining selective oxidation and alcoholic/base reactions; Overall, selective oxidation pretreatment always led to a lower sulfur product than the untreated sample; Substantial enhancement in the reactivity of the sulfur in the coal has been achieved by the selective oxidation pretreatment; The highest levels of desulfurization obtained so far all involve bases as additives; The water/Na{sub 2}CO{sub 3} combination, was superior than any of the aqueous hydroxide bases. Possible synergistic interactions between the alcohol and the base are suspected. Over 70% of the sulfur in the IBC 101 coal can be removed by performing vacuum pyrolysis on the selectively oxidized coal. Lower sulfur contents are obtained by lowing the pyrolysis pressure.

  14. GBRN/DOE Project: Dynamic enhanced recovery technologies. Quarterly technical report, January 1994--March 1994

    SciTech Connect

    Anderson, R.N.

    1994-04-15

    Global Basins Research Network will perform a field demonstration of their ``Dynamic Enhanced Recovery Technology`` to test the concept that the growth faults in EI-330 field are conduits through which producing reservoirs are charged and that enhanced production can be developed by producing directly from the fault zone. The site, operated by Penzoil, is located in 250 feet of water the productive depth intervals include 4000 to 9000 feet. Previous work, which incorporated pressure, temperature, fluid flow, heat flow, seismic, production, and well log data, indicated active fluid flow along fault zones. The field demonstration will be accomplished by drilling and production test of growth fault systems associated with the EI-330 field. The project utilizes advanced 3-D seismic analysis, geochemical studies, structural and stratigraphic reservoir characterization, reservoir simulation, and compact visualization systems. The quarterly progress reports contains accomplishments to date for the following tasks: Management start-up; database management; field and demonstration equipment; reservoir characterization, modeling; geochemistry; and data integration.

  15. VHF EPR analysis of organic sulfur in coal. [Quarterly] technical report, September 1--November 20, 1991

    SciTech Connect

    Clarkson, R.B.

    1991-12-31

    This report covers progress made in the first yearly quarter of a two year investigation using novel, very high frequency electron paramagnetic resonance (VHF EPR) spectroscopy techniques and instrumentation (one of only two W-band spectrometers in existence) developed earlier by these authors, to conduct further qualitative and quantitative studies of heteroatomic organic molecules in coal with particular emphasis on sulfur. Previous W-band (96 GHz) work is being extended to studies of new model compounds as well as coal and desulfurized coal samples. Typically, the model compounds under investigation and their analogues are found in coals as stable free radicals which give rise to an EPR signal. The preparation of radicals from compounds having widely varying structures and physical properties in a stable environment has long been a very difficult task. To address this problem, the refinement of several new and very useful methods of preparing of these stable free radicals in various glasses, at catalytic surfaces, and in solution, are presented in this first report. Free radical generation was accomplished by both UV photolysis as well as chemical oxidation/reduction techniques. By these methods, over 25 new compounds, often commercially derived from coal extracts, have been prepared and studied by conventional X-band EPR (9 GHz). Several representative W-band spectra are also presented.

  16. Western Research Institute quarterly technical progress report, July--September 1993

    SciTech Connect

    Not Available

    1993-12-31

    Accomplishments for the quarter are described briefly for the following areas of research: oil shale; tar sand; coal; advanced exploratory process technology; and jointly sponsored research. Oil shale research covers process studies. Tar sand research is on recycle oil pyrolysis and extraction (ROPE{sup TM}) Process. Coal research includes: coal combustion; integrated coal processing concepts; and solid waste management. Advanced exploratory process technology includes: advanced process concepts; advanced mitigation concepts; and oil and gas technology. Jointly sponsored research covers: CROW{sup TM} field demonstration with Bell Lumber and Pole; operation and evaluation of the CO{sub 2} HUFF-N-PUFF Process; fly ash binder for unsurfaced road aggregates; solid state NMR analysis of Mesaverde group, Greater Green River Basin, tight gas sands; characterization of petroleum residua; shallow oil production using horizontal wells with enhanced oil recovery techniques; surface process study for oil recovery using a thermal extraction process; oil field waste cleanup using tank bottom recovery process; remote chemical sensor development; in situ treatment of manufactured gas plant contaminated soils demonstration program; solid state NMR analysis of Mowry formation shale from different sedimentary basins; solid state NMR analysis of naturally and artificially matured kerogens; and development of an effective method for the clean-up of natural gas.

  17. Characterization of available coals from Illinois mines. [Quarterly] technical report, March 1, 1993--May 31, 1993

    SciTech Connect

    Demir, I.; Harvey, R.D.; Ruch, R.R.; Chaven, C.; Damberger, H.H.; Steele, J.D.; Frankie, W.T.

    1993-09-01

    The goal of this project is to characterize marketed coals from Illinois mines. The characterization parameters that are being determined include the concentration of all trace and minor elements that are of environmental concern, proximate and ultimate compositions, the pyrite size distribution and maceral association, preliminary froth flotation cleanability, slagging and fouling characteristics relevant to the coal`s behavior in utility boilers, chlorine forms and distribution, and certain gasification and rheology parameters. During the third quarter, the trace element data base on Illinois coals was fully checked and edited. The determinations of the trace and minor element contents and proximate and ultimate compositions of the 34 project samples were largely completed. The pyritic S content, still high in some of the marketed samples, could be reduced further in the samples by advanced physical cleaning techniques. Results from the analysis of all 34 samples for Ba, Hg, Mn, and Zr indicate that these elements are primarily or partly associated with mineral matter and, therefore, their concentrations could also be reduced further in the product coals by advanced physical cleaning techniques. A sequential extraction of Cl from two of the samples revealed that regardless of the initial chlorine concentration of the two coals, the total combined amount of chlorine extracted by water, ammonia, and sodium hydroxide is about the same.

  18. National Institute for Petroleum and Energy Research quarterly technical report, January 1--March 31, 1990

    SciTech Connect

    Not Available

    1990-04-19

    Fuels research is discussed in the following areas: (1) Department of Analytical Methodology for Analysis of Heavy Crudes; and (2) thermochemistry and thermophysical properties of organic nitrogen-, and diheteroatom-containing compounds. This quarter for project (1), inspection analysis of five 1000{degree}F+ resids employed in the carbonization study were completed. Also, subfractionation of Cerro Negro neutrals fraction was carried out. Progress on Project 2 consisted of: a thermodynamic analysis for the key hydrogen-consuming steps in the hydrodenitrogenation (HDN) reaction network for quinoline; heat-capacity and enthalpy measurements were completed for the diheteroatom-containing compound, thianthrene. Following completion measurements on thianthrene, the heat capacity of the empty calorimeter was determined, and in another calorimeter, heat-capacity and enthalpy studies were started on benzoxazole. Methods to convert benzoxazole to its low-temperature form were developed, and measurements were completed between 80 and 240 K; and high-temperature heat capacities were determined for phenoxathin and carbazole. 1 ref., 14 figs., 11 tabs.

  19. Development of analytical procedures for coprocessing. Quarterly technical progress report, July 1, 1990--September 30, 1990

    SciTech Connect

    Anderson, R.P.

    1991-05-01

    This is the eighth quarterly report under DOE Contract No. DE-AC22-88PC88810, Development of Analytical Procedures for Coprocessing. The overall objective of the contract is to improve our understanding of the fundamental chemistry of coprocessing. This includes the evaluation of methods to distinguish between compound classes originating from coal versus those originating from petroleum resid. Techniques being evaluated include carbon isotope ratios and the variations in compound classes in response to changes in the coal/resid ratio in the feed. A final objective of this project is to provide detailed knowledge on the composition of coprocessing products. This report reviews the use of isotope ratios to determine the source of compound classes (e.g., acids, bases, neutrals, aromatics, saturates, etc.). Selective isotope fractionation is a complicating factor in the use of carbon isotope ratios to determine the source of coprocessing products. Other researchers have shown that through the use of appropriate correction factors to correct for this isotope selectivity, isotope ratios can be used to quantitatively determine the source of coprocessing fractions obtained by distillation. It is concluded in this report that although isotope ratios may provide qualitative information on the source of coprocessing compound classes, that the high degree of isotope selectivity in compound classes originating from a single feed prohibits the quantitative determination of the origin of such compound classes.

  20. The Kelastic variable wall mining machine. Third quarterly technical report, April 1--July 1, 1997

    SciTech Connect

    1997-12-31

    The Project Team accomplished two tasks during the third quarter: preparation and presentation of professional papers; and development of simulation models and sub models of the hypothetical variable wall mining installation. The project team also continued its search for the suitable animation software to be adapted to the underground mining systems. Meanwhile work is progressing along the lines of updating the original open loop flow diagram that deals with the automatic control of the thrusting, advance, and rotation of the auger train which both cuts (extracts) and transports the coal across the face. The team is integrating the control systems into a deterministic mathematical equation for optimizing the mining and material flow rate in the operating system. The long range plan is to integrate the current deterministic equations in a suitable animation program with a number of adjustable and controllable parameters. This will enable coal operators and engineers to visualize how the variations can affect the safety, cost and production levels of the system.

  1. Mild pyrolysis of selectively oxidized coals. [Quarterly] technical report, December 1, 1991--February 29, 1992

    SciTech Connect

    Hippo, E.J.; Palmer, S.R.

    1992-08-01

    The primary objective of this study is to investigate the removal organic sulfur from selectively oxidized Illinois coals using mild thermal/chemical processes. Work completed this quarter primarily concerned establishing the level of selective oxidation required for successful desulfurization in subsequent treatments. Many desulfurization reactions were performed on pretreated as well as unoxidized coal. The results obtained support the following new conclusions: (1) The extent of selective oxidation in the pretreatment step does not effect the level of desulfurization obtained by pyrolysis alone. However this factor was important in the desulfurization obtained with supercritical methanol (SCM)/base. (2) Up to 84% of the sulfur in the IBC 106 coal and 86% of the sulfur in the IBC 106 coal has been removed by combining selective oxidation and SCM/base reactions. (3) Most desulfurizations at 250{degree}C did not produce significant levels of desulfurization. However as the temperature was increased levels of desulfurization increased considerably. (4) Although aqueous base was successful in removing sulfur from both pretreated and untreated samples, the most pronounced desulfurizations were obtained for the untreated samples. This is explained primarily by the dissolution of pyrite in the untreated samples. (5) The best desulfurizations involved SCM and base. Possible synergistic interactions between the methanol and the base are suspected. (6) Overall, selective oxidation pretreatment always led to a lower sulfur product. The severity of desulfurization is reduced by selective oxidation pretreatment.

  2. National Institute for Petroleum and Energy Research quarterly technical report, January 1--March 31, 1993

    SciTech Connect

    Not Available

    1993-06-01

    Accomplishments for the past quarter are briefly described for the following tasks: chemical flooding -- supporting research; gas displacement -- supporting research; thermal recovery -- supporting research; geoscience technology; resource assessment technology; and microbial technology. Chemical flooding covers: surfactant flooding methods; development of improved alkaline flooding methods; mobility control and sweep improvement in chemical flooding; and surfactant-enhanced alkaline flooding field project. Gas displacement covers: gas flooding performance prediction improvement; and mobility control, profile modification and sweep improvement in gas flooding. Thermal recovery includes: thermal processes for light oil recovery; thermal processes for heavy oil recovery; and feasibility study of heavy oil recovery in the mid-continent region -- Oklahoma, Kansas, and Missouri; simulation analysis of steam-foam projects; and field application of foams for oil production symposium. Geoscience technology covers: three-phase relative permeability; and imaging techniques applied to the study of fluids in porous media. Resource assessment technology includes: reservoir assessment and characterization; TORIS research support; upgrade the BPO crude oil analysis data base; and compilation and analysis of outcrop data from the Muddy and Almond Formations. Microbial technology covers development of improved microbial flooding methods; and microbial-enhanced waterflooding field project.

  3. Particulate hot gas stream cleanup technical issues. Quarterly report, October 1995--December 1995

    SciTech Connect

    1996-03-01

    This is the fifth quarterly report describing the activities performed under Contract No. DE-AC21-94MC31160. Task 1 of this contract concerns analyses of HGCU ashes and descriptions of filter performance that are designed to address the problems with filter operation linked to the characteristics of the collected ash. Task 2 of this contract includes characterization of new and used filter elements. Some of the problems observed at the Tidd and Karhula PFBC facilities include excessive filtering pressure drop, the formation of large, tenacious ash deposits within the filter vessel, and bent or broken candle filter elements. These problems have been attributed to ash characteristics, durability of the ceramic filter elements, and specific limitations of the filter design. In addition to these problems related to the characteristics of PFBC ashes, our laboratory characterizations of gasifier and carbonizer ashes have shown that these ashes also have characteristics that might negatively affect filtration. Problems with the durability of the filter elements are being addressed by the development and evaluation of elements constructed from alternative ceramic materials.

  4. Biodesulfurization of mild gasification liquid products. [Quarterly] technical report, March 1, 1993--May 31, 1993

    SciTech Connect

    Kilbane, J.J. II

    1993-09-01

    The mild gasification of coal is a promising new technology that can convert coal to multiple products: gas, solid, and liquids. However, the sulfur content and aromaticity of mild gasification liquids limits their usefulness. Biodesulfurization can potentially decrease both sulfur content and aromaticity. The objective of this project is to investigate the feasibility of using biodesulfurization to upgrade the quality of mild gasification liquids. Previously it was shown that the middle distillate (360--440{degrees}F) fraction of liquids derived from the mild gasification of coal could be biodesulfurized. During this quarter it was demonstrated that unfractionated liquids can be biodesulfurized. Moreover, it was demonstrated that lysed cell preparations and freeze-dried cells can be used to biodesulfurize mild coal gasification liquids. The importance of the finding that freeze-dried biocatalysts can be used to biodesulfurize mild coal gasification liquids is that freezedried cells can be produced at one location, stored indefinitely, and then shipped to another location for coal biodesulfurization. Moreover, freeze-dried biocatalysts can be added directly to mild coal gasification liquids with only minimal additions of water so that reactor volumes can be minimized.

  5. Coal liquefaction process streams characterization and evaluation. Quarterly technical progress report, October 1--December 31, 1992

    SciTech Connect

    Brandes, S.D.; Winschel, R.A.; Burke, F.P.; Robbins, G.A.

    1993-10-01

    The Research and Development Department of CONSOL Inc. is conducted a program to characterize process and product streams from direct coal liquefaction process development projects sponsored by the Department of Energy. In this program, CONSOL obtains samples from current process development activities in coal liquefaction and coal-oil coprocessing, and characterizes them using established analytical techniques. In addition, selected samples are characterized by other analytical techniques to evaluate their potential for aiding process development. These analyses and interpretation of the results in relation to process operations are provided by the subcontractor. Major topics reported in this thirteenth quarterly report are the following: (1) Analyses were performed on three coals and eleven process oils from HRI, Inc. process development unit Run 260--03, which was the first process development unit test of Black Thunder Mine subbituminous coal, significant operating problems were encountered, and sample properties are discussed in context to the operational problems; (2) a summary of the status of the Participants Program is given; (3) summaries of the final reports produced by the University of Chicago, the University of Utah, Iowa State University, and the University of Kentucky under the Participants Program, are presented.

  6. Microbial stabilization of sulfur-laden sorbents. [Quarterly] technical report, March 1, 1993--May 31, 1993

    SciTech Connect

    Miller, K.W.

    1993-09-01

    Clean coal technologies that involve limestone for in situ sulfur capture generate lime/limestone products laden with sulfur at various oxidation states. If sulfur is completely stabilized as sulfate, the spent sorbent is ready for commercial utilization as gypsum. However, the presence of reduced sulfur species requires additional processing. Thermal oxidation of reduced sulfur frequently results in undesirable release of SO{sub 2}. Microbial oxidation might provide an inexpensive and effective alternative. Sorbents laden with reduced forms of sulfur such as sulfide or sulfite can serve as growth substrates for sulfur-oxidizing bacteria, which convert all sulfur to sulfate. The goals of this project are the following: (1) to optimize conditions for sulfate generation from sulfide, thiosulfate, and sulfite; (2) to test and optimize the effectiveness of microbial processing on spent sorbents from flue gas desulfurization, coal gasification, and fluidized bed combustion; (3) to search for hyperalkalinophilic thiobacilli, which would be effective up to pH 11. This quarter, temperature, nitrogen, and phosphate requirements for sulfate generation on thiosulfate were optimized with respect to two named strains and two promising isolates. Spent sorbents from three different power plants were tested for sulfite and thiosulfate contents, in preparation for bioprocessing.

  7. Oxidation of phenolics in supercritical water. Quarterly technical progress report, September 1, 1993--November 30, 1993

    SciTech Connect

    Savage, P.E.

    1993-12-31

    Oxidation reactions are accomplished in an isothermal, high-pressure, flow reactor designed specifically for operation at supercritical water conditions. The reactor feed stream is prepared by mixing two separate streams. One stream is an aqueous solution of the phenolic reactant and the second stream is water with dissolved oxygen. Controlling the flow rates of these two streams allows us to control the reactor residence time and the relative amounts of the phenol and oxygen fed to the reactor. The reactor effluent is cooled and depressorized and then collected for analysis. The gaseous products are analyzed by gas chromatography (GC). The liquid-phase products are analyzed by GC, high-performance liquid chromatography, and GC-mass spectrometry. Our work to date has focused on the oxidation of cresols in SCW. We have explored the effects of temperature, pressure, and the concentrations of o-cresol, oxygen, and water. Table I gives these experimental conditions and the resulting ocresol conversions. We reported a portion of this data in our previous quarterly report. New information is given in the last three columns where we report the molar yields of phenol, CO{sub 2}, and CO. Molar yields were calculated as the molar flow rate of a given product divided by the initial molar flow rate of o-cresol and normalized by the stoichiometric coefficient. Earlier, we used the o-cresol conversion data to determine the parameters in a global reaction rate law for o-cresol disappearance.

  8. Solvent Refined Coal (SRC) process. Quarterly technical progress report, April 1979-June 1979

    SciTech Connect

    Not Available

    1980-02-01

    This report summarizes the progress of the Solvent Refined Coal (SRC) Project for the period March 25, 1979, through June 24, 1979. SRC-I turnaround activities at the Fort Lewis Pilot Plant and several other problems delayed successful startup until April 11. Slurry was injected to the Lummus Deashing Unit for the first time April 12. After approximately eight days, slurry feed was diverted because of indications that solids were accumulating in the settler vessel. The Fort Lewis Pilot Plant was shut down from April 28 to May 12, 1979, while the Lummus Unit settler vessel was hydroblasted. Cleaning of the settler vessel was complete May 10. Modifications to the unit were nearly complete at the end of the reporting period. Slurry feed to the Lummus Unit was reestablished June 15. To date, continuous production of specification product at design rates has not been achieved. One material balance run, MBR 79-1, was completed using Kentucky No. 9/14 coal at proposed design conditions for the SRC-I Demonstration Plant. Process Development Unit P-99 was on-stream for all of the second quarter of 1979, with the exception of a two-week scheduled turn-around. Six different run conditions were tested feeding Pittsburgh Seam coal from the Powhatan No. 5 Mine.

  9. Isobutanol-methanol mixtures from synthesis gas. Quarterly technical progress report, 1 January--31 March 1995

    SciTech Connect

    Iglesia, E.

    1995-04-24

    The contract objectives are: to design a catalytic material for the synthesis of isobutanol with a productivity of 200 g isoalcohols/g-cat-h and a molar isobutanol/methanol ratio near unity; and to develop structure-function rules for the design of catalysts for the selective conversion of synthesis gas to isoalcohols. Several catalyst samples have been prepared by controlled co-precipitation from aqueous mixtures of metal nitrates. The composition of these materials is based on reports of best available catalysts for methanol synthesis, for isobutanol synthesis, and for methanol coupling reactions. The mechanical construction and pressure testing of the microreactor system has been completed. The in-situ infrared spectrophotometer equipped with a nitrogen purge is fully operational. The temperature-programmed surface reaction (TPSR) unit has been designed; construction will begin during the third quarter FY`95. Air Products and Chemicals has provided us with a sample of a BASF isobutanol synthesis catalyst and with catalytic data obtained on this catalyst in a LaPorte test run. This catalyst will serve as a benchmark for the certification of our new microreactor system.

  10. PEPCO turbo-Z battery charger system. Technical progress report, calendar quarter ending March 31, 1998

    SciTech Connect

    Rose, J.

    1998-04-30

    During the First Quarter of 1998, the engineers working on this Grant have dramatically increased the rate of work. They are developing a Flexible Battery Charger Control Board, a Battery Charger Test Stand, and writing software that can be used with both. The status is as follows: (a) Flexible Battery Charger Control Board -- a preliminary electrical design is complete. They are now investigating how the control design might incorporate provisions for an additional Electric Vehicle charging feature. This additional design is based on SAE J2293 -- Recommended Practice for EV Communications. Investigation of J2293 is being considered for controlling a power supply using proprietary Capacitive Charging Coupler, and controlling the power supply with this control board. (b) Battery Test Stand -- the preliminary hardware design is complete. The design includes some very desirable additions to the specifications, including an AC line source for the charger being tested and a battery simulator. Purchasing of the equipment and materials for the test stand is underway. The engineers have been working in the SAE standards setting committees for Electric Vehicles for several years. In particular, they have been working to set the Capacitive Coupler as the standard for connecting an EV to the utility grid system. Substantial test data has been distributed to the committee members on the Conductive and Inductive Charging Systems. It is their opinion that they have a superior coupling mechanism, and they are proceeding to develop this technology.

  11. Stable carbon isotope analysis of coprocessing materials: Quarterly technical progress report, October 1--December 31, 1988

    SciTech Connect

    Burke, F.P.; Winschel, R.A.; Lancet, M.S.

    1989-03-01

    Consol R and D will develop and demonstrate stable carbon isotope analysis as a method to quantitatively distinguish coal-derived and petroleum-derived carbon in products from coal/petroleum coprocessing. The approach taken will be to develop the method, then demonstrate its application on authentic continuous-unit products. The significance of selective isotopic fractionation will be determined and, if necessary, corrections will be applied to account for it. Precision, accuracy and range of applicability will be defined. The value of accessory analytical techniques will also be assessed. Results achieved this quarter include: feed and product fractions from hydroprocessing bench unit runs at the Kentucky Center for Applied Energy Research (CAER) were received, and samples from a Kentucky tar sand bitumen-only run were analyzed for carbon isotope ratios. Repeat carbon isotope analyses of seven samples from HRI Coprocessing Run 227-53 resulted in improved carbon balances for one run period. Athabasca ASB, Cold Lake ASB and Maya ASB were fractionated by distillation and solubility fractionation to determine the homogeneity of each petroleum with respect to carbon isotope ratios. 9 figs., 2 tabs.

  12. Advanced separation technology for flue gas cleanup. Quarterly technical report No. 7, [October--December 1993

    SciTech Connect

    Bhown, A.S.; Alvarado, D.; Stearns, P.; Ventura, S.; Sirkar, K.K.; Majumdar, S.; Bhaumick, D.

    1994-02-01

    During the third quarter of 1993, we continued work on Tasks 2, 3, 4, 5, and 6. In Task 2, we tested the NO{sub x} sorption capacity of Fe(II)-EDTA and five new SRI-synthesized compounds. We also made a comparison of all the tests so far and have selected two compounds as the leading candidates. In Task 3, we electrochemically converted FE(III) phthalocyanine to its Fe(II) analog and synthesized several metal phthalocyanine compounds. In Task 4, we evaluated 200-fiber HFC modules for SO{sub 2} removal with water and solutions of Na{sub 2}SO{sub 3}. We also connected this HFC unit to the liquor regenerating HFC unit described in Task 6. We continue to observe 95--100% SO{sub 2} removal. In Task 5, we calculated the overall mass transfer coefficients of earlier Fe(II)-EDTA runs for scrubbing NO{sub x}. We also obtained a new module from Hoechst-Celanese and began its characterization. In Task 6, we demonstrated that the spent liquor from Task 4 can be regenerated using a second HFC. The spent liquor was regenerating using DMA with initial recovery of SO{sub 2} up to 52%.

  13. Molecular biological enhancement of coal biodesulfurization. [Quarterly] technical report, December 1, 1993--February 28, 1994

    SciTech Connect

    Kilbane, J.J. II

    1994-06-01

    IGT has developed a microbial culture of Rhodococcus rhodochrous, IGTS8, that is capable of specifically cleaving carbon-sulfur bonds in a range of organosulfur model compounds and is capable of removing organic sulfur from coal and petroleum. Although IGTS8 possesses the ability to specifically remove organic sulfur from coal, a major research need is to develop improved strain`s of microorganisms that possess higher levels of desulfurization activity and therefore wall permit more favorable biodesulfurization process conditions: faster rates, mare complete removal, and smaller reactor size. Strain improvement is the single most important aspect to the development of a practical coal biodesulfurization process and accordingly is the focus of research in this project. Several possible strong promoters have been isolated and are in the process of being analyzed. When these promoters have been characterized for inducibility, strength, transcriptional start sites and other physical properties, they will be placed in front of the desulfurization genes and expression will be monitored. Improved promoter probe vectors have been constructed, allowing a conclusive screen of all putative Rhodococcus promoters. With the improved methodologies in the handling of Rhodococcus RNA, we have begun to gauge promoter expression using Northern blots. During this quarter we have constructed and successfully used a promoter probe vector using the {beta}-galactosidane gene from E. coli. A chromosomal promoter library was constructed upstream from the {beta}-galactosidase gene. Over 200 colonies were isolated that yielded {beta}-galactosidase activity.

  14. [Dynamic enhanced recovery techniques]. Quarterly technical report, April 1994--June 1994

    SciTech Connect

    Anderson, R.N.

    1994-07-15

    Global Basins Research Network will perform a field demonstration of their ``Dynamic Enhanced Recovery Technology`` to test the concept that the growth of faults in Eugene Island Block 330 (EI-330 field) are conduits through which producing reservoirs are charged and that enhanced production can be developed by producing directly from the fault zone. The site, operated by Penzoil, is located in 250 feet of water and the productive depth intervals include 4000 to 9000 feet. The field demonstration will be accomplished by drilling and production testing of growth fault systems associated with the EI-330 field. The project utilizes advanced 3-D seismic analysis, geochemical studies, structural and stratigraphic reservoir characterization, reservoir simulation, and compact visualization systems. In this quarterly report, progress reports are presented for the following tasks: Task one--management start-up; Task two--database management; Task three--field demonstration experiment; Task four--reservoir characterization; Task five--modeling; Task six--geochemistry; and Task seven--data integration.

  15. Basalt Waste Isolation Project. Quarterly report, July 1, 1980-September 30, 1980

    SciTech Connect

    Deju, R.A.

    1980-11-01

    This report presents the technical progress for the Basalt Waste Isolation Project for the fourth quarter of fiscal year 1980. The overall Basalt Waste Isolation Project is divided into the following principal work areas: systems integration; geosciences; hydrology; engineered barriers; near-surface test facility; engineering testing; and repository studies. Summaries of major accomplishments for each of these areas are reported.

  16. Short-term energy outlook: Quarterly projections, second quarter 1997

    SciTech Connect

    1997-04-01

    The Energy Information Administration (EIA) prepares quarterly short-term energy supply, demand, and price projections for publication in January, April, July, and October in the Outlook. The forecast period for this issue of the Outlook extends from the second quarter of 1997 through the fourth quarter of 1998. Values for the first quarter of 1997, however, are preliminary EIA estimates (for example, some monthly values for petroleum supply and disposition are derived in part from weekly data reported in EIA`s Weekly Petroleum Status Report) or are calculated from model simulations that use the latest exogenous information available (for example, electricity sales and generation are simulated by using actual weather data). The historical energy data, compiled in the second quarter 1997 version of the Short-Term Integrated Forecasting System (STIFS) database, are mostly EIA data regularly published in the Monthly Energy Review, Petroleum Supply Monthly, and other EIA publications. Minor discrepancies between the data in these publications and the historical data in this Outlook are due to independent rounding. The STIFS database is archived quarterly and is available from the National Technical Information Service. The STIFS model is driven principally by three sets of assumptions or inputs: estimates of key macroeconomic variables, world oil price assumptions, and assumptions about the severity of weather. Macroeconomic estimates are produced by DRI/McGraw-Hill but are adjusted by EIA to reflect EIA assumptions about the world price of crude oil, energy product prices, and other assumptions which may affect the macroeconomic outlook. By varying the assumptions, alternative cases are produced by using the Short-Term Integrated Forecasting System (STIFS). 34 figs., 19 tabs.

  17. I-NERI QUARTERLY TECHNICAL PROGRESS REPORT - JANUARY 1 - MARCH 31, 2005

    SciTech Connect

    Chang Oh

    2005-03-01

    The objective of this Korean/United States/laboratory/university collaboration is to develop new advanced computational methods for safety analysis codes for very-high-temperature gas-cooled reactors (VHTGRs) and numerical and experimental validation of these computer codes. The research will improve two well-respected light water reactor transient response codes (RELAP5/ATHENA and MELCOR) in the modeling of molecular diffusion and chemical equilibrium, and to validate these codes against the VHTGR accident data, i.e., air ingress and others from the literature. The VHTGR is intrinsically safe, has a proliferation-resistant fuel cycle, and many advantages relative to light water reactors (LWRs). This study consists of five tasks for FY-03: (1) development of computational methods for the VHTGR, (2) theoretical modification of aforementioned computer codes for molecular diffusion (RELAP5/ATHENA) and modeling CO and CO{sub 2} equilibrium (MELCOR), (3) development of a state-of-the-art methodology for VHTGR neutronic analysis and calculation of accurate power distributions and decay heat deposition rates, (4) reactor cavity cooling system experiment, and (5) graphite oxidation experiment. First quarter of Year 3: (A) Prof. NO and Kim continued Task 1. We first performed the chemical reaction test for the VELUNA pebble oxidation experiment and then the analysis of the air ingress accident for PBMR 268MWt. In the GAMMA analysis, significant rise in pebble temperature was observed at the bottom of the core due to graphite oxidation. Since the air ingress process depends on the vault conditions, further analysis coupled with more detailed vault or containment modeling would be necessary as a future study. (B) Prof. Park continued Task 2. The experiments for SNU-RCCS were continued to provide the experimental data for the validation of the thermal hydraulic code being developed at KAIST and to evaluate the performance of the system using the experiments and system analysis

  18. Molecular biological enhancement of coal biodesulfurization. Third quarterly technical progress report

    SciTech Connect

    Litchfield, J.H.; Fry, I.; Wyza, R.E.; Palmer, D.T.; Zupancic, T.J.; Conkle, H.N.

    1990-03-15

    The objective of this project is to produce one or more microorganisms capable of removing the organic and inorganic sulfur in coal. The original specific technical objectives of the project were to: Clone and characterize the genes encoding the enzymes of the ``4S`` pathway (sulfoxide/sulfone/sulfonate/sulfate) for release of organic sulfur from coal; Return multiple copies of genes to the original host to enhance the biodesulfurization activity of that organism; Transfer this pathway into a fast-growing chemolithotrophic bacterium; Conduct a batch-mode optimization/analysis of scale-up variables.

  19. Decontamination Systems Information and Research Program. Quarterly technical progress report, January 1--March 31, 1993

    SciTech Connect

    Not Available

    1993-04-01

    This reports reports the progress/efforts performed on six technical projects: 1. systematic assessment of the state of hazardous waste clean-up technologies; 2. site remediation technologies (SRT):drain- enhanced soil flushing for organic contaminants removal; 3. SRT: in situ bio-remediation of organic contaminants; 4. excavation systems for hazardous waste sites: dust control methods for in-situ nuclear waste handling; 5. chemical destruction of polychlorinated biphenyls; and 6. development of organic sensors: monolayer and multilayer self-assembled films for chemical sensors.

  20. Molecular biological enhancement of coal biodesulfurization. Tenth quarterly technical progress report, [September--December 1991

    SciTech Connect

    Litchfield, J.H.; Zupancic, T.J.; Kittle, J.D.; Baker, B.; Palmer, D.T.; Fry, I.J.; Traunero, C.G.; Wyza, R.E.; Schweitzer, A.; Conkle, H.N.; Chakravanty, L.; Tuovinen, O.H.

    1991-12-13

    The objective of this project is to produce one or more microorganisms capable of removing the organic and inorganic sulfur in coal. The specific technical objectives of the project are to: clone and characterize the genes encoding the enzymes of the ``4S`` pathway (sulfoxide/sulfone/sulfonate/sulfate) for release of organic sulfur from coal; return multiple copies of genes to the original host to enhance the biodesulfurization activity of that organism; transfer this pathway into a fast-growing chemolithotrophic bacterium; and conduct a batch-mode optimization/analysis of scale-up variables.

  1. Molecular biological enhancement of coal biodesulfurization. First quarterly technical progress report

    SciTech Connect

    Litchfield, J.H.; Palmer, D.T.; Zupancic, T.J.; Conkle, H.N.

    1989-09-15

    The objective of this project is to produce one or more microorganisms capable of removing the organic and inorganic sulfur in coal. The original specific technical objectives of the project were to: Clone and characterize the genes encoding the enzymes of the ``4S`` pathway (sulfoxide/sulfone/sulfonate/sulfate) for release of organic sulfur from coal; return multiple copies of genes to the original host to enhance the biodesulfurization activity of that organism; transfer this pathway into a fast-growing chemolithotropic bacterium; conduct a batch-mode optimization/analysis of scale-up variables.

  2. Molecular biological enhancement of coal biodesulfurization. Ninth quarterly technical progress report

    SciTech Connect

    Litchfield, J.H.; Zupancic, T.J.; Baker, B.; Palmer, D.T.; Fry, I.J.; Tranuero, C.G.; Wyza, R.E.; Schweitzer, A.; Conkle, H.N.; Chakravanty, L.; Tuovinen, O.H.

    1991-09-13

    The objective of this project is to produce one or more microorganisms capable of removing the organic and inorganic sulfur in coal. The original specific technical objectives of the project were to: clone and characterize the genes encoding the enzymes of the ``4S`` pathway (sulfoxide/sulfone/sulfonate/sulfate) for release of organic sulfur from coal; return multiple copies of genes to the original host to enhance the biodesulfurization activity of that organism; transfer this pathway into a fast-growing chemolithotropic bacterium; conduct a batch-mode optimization/analysis of scale-up variables.

  3. Electrochemical photovoltaic cells. Project 65021 quarterly technical progress report, October 15, 1979-January 15, 1980

    SciTech Connect

    Ang, P.G.P.; Remick, R.J.; Sammells, A.F.

    1980-03-01

    During the third quarter of this program, liquid junction devices based upon the semiconductors MoSe/sub 2/, MoS/sub 2/, GaAs, and CdSe have been evaluated. Lifetime testing of MoSe/sub 2/ and MoS/sub 2/ materials in acidic halogen electrolytes at constant current densities of 5 mA/cm/sup 2/ have shown excellent stability to date. For MoSe/sub 2/ single crystals in the electrolyte 1M HBr + 1M Br/sub 2/, short-circuit currents of 63 mA/cm/sup 2/ were achieved with a power conversion efficiency of 6.7% for 200 mW/cm/sup 2/ xenon light illumination. Transient potentiostatic measurements made on MoSe/sub 2/ in this electrolyte indicated little diffusion control, with exchange currents being of the order of 1 to 10 mA/cm/sup 2/. Good photoresponse of MoS/sub 2/ has been observed in 1M HBr + 1M Br/sub 2/. The performance of the natural crystal is comparable to the performance of a single-crystal MoS/sub 2/ in this electrolyte. CdSe thermally evaporated onto porous titanium gave efficiencies of about 4% with 100 mW/cm/sup 2/ xenon illumination. Experimental work was initiated on the dye sensitization of Fe/sub 2/O/sub 3/ and TiO/sub 2/ materials. Of the twelve dyes evaluated, little enhancement of the photoresponse of these materials was noted. Solid-state photoelectrochemical cells have been fabricated, based upon LiI. Cells of the configuration - cond. glass CdSe/LiI + PbI/sub 2//LiI/LiI + C + PbI/sub 2//cond. glass - were fabricated. Photoresponses up to 150 mV were observed.

  4. Advanced direct liquefaction concepts for PETC generic units. Quarterly technical progress report, October 1993--December 1993

    SciTech Connect

    Not Available

    1994-02-01

    Several promising leads that have developed during the course of this program are being evaluated in this phase of the study. These have been selected from those that can be economically evaluated within the time constraints of the program schedule. A detailed plan for evaluating these approaches was formulated. The individual steps that will be evaluated are: (1) Dewaxing of the distillate recycle solvent stream treating either 25% or 100% of the stream. (2) Hydrotreating the dewaxed distillate streams in a downflow fixed bed reactor. (3) Agglomerating the coal using both the 25% and 100% dewaxed-hydrotreated distillate streams. (4) Liquefying the as-received coal and the agglomerated coals using two different Mo-promoted hematite particulate catalysts. (5) Liquefying two different Mo-Fe impregnated coals. (6) Liquefying the two off-agglomerated, Mo-Fe impregnated coals. The effect of the presence of molybdenum in the 1050{degrees}F{sup +} will be determined by making comparisons in both Mo-containing and Mo-free full range V-131B process solvent. The solvents that will be used in this study are the full-range reconstituted Mo-containing V-131B from Run 262E and a Mo-free V-131B made up of 1050{degrees}F{sup +} bottoms from Run 258K V-131B and V-1074 distillate from Run 262E. The series of experiments are described and a chart has been prepared summarizing this series of runs. The plan requires significant exchange of samples between the different participants in the program with the schedule timed for providing the data for economic evaluation within the next quarterly reporting period.

  5. Methyl chloride via oxyhydrochlorination of methane. Quarterly technical progress report No. 7, April--June 1993

    SciTech Connect

    Not Available

    1994-01-01

    The purpose of this contract is to develop a process for converting light alkane gases to methyl chloride via oxyhydrochlorination using highly selective, stable catalysts in fixed-bed reactors designed to remove the large amount of heat generated, so as to control the reaction temperature. Further, the objective is to obtain the engineering data base necessary for developing a commercially feasible process and to evaluate the economics of the process. Several key technology areas were evaluated this quarter. The catalyst definition effort focused on the determination of the role of the Li and La promoters that have been found to be useful in enhancing Cu based oxyhydrochlorination of methane catalysts. Initial experiments show that the La acts to provide a much more active catalyst than the Cu only case. The role of the Li is ambiguous at this point. The Li enhances the stability of the La promoted catalyst, but gives only marginal improvement by itself This work will be continued, with additional emphasis on the analysis of the catalysts to determine the structural role that the promoters may play. The separation unit operation definition made significant progress by demonstrating in a laboratory system that a process solvent may be used to remove the product CH{sub 3}Cl from the reactor effluent stream. To date the data has been qualitative, but clear. Work will continue to gather the information possible in the laboratory to help with PDU design. An extensive amount of testing was performed on the chosen process solvent, Multitherm. A comprehensive review of all the thermal testing and associated FTIR, UV/VIS, and physical property testing is included in this report. This work shows that Multitherm should give the desired stability and solubility that are necessary to make the separation unit operation successful.

  6. Syn-Fuel reciprocating charge pump improvement program. Quarterly technical project report, April-June 1984

    SciTech Connect

    Not Available

    1984-01-01

    Major accomplishments during the second quarter of 1984 were completion of the Diaphragm Separation Seal clear liquid testing, and initiation of Phase III Field Testing. Diaphragm operational testing was conducted on a clear water test loop. The test goals were to ensure; mechanical reliability of the Diaphragm Seal, safe operation with simulated component failure, and proper operation of the Diaphragm Buffer Volume Control System. This latter system is essential in controlling the phasing of the diaphragm with its driving plunger. These tests were completed successfully. All operational problems were solved. However, it must be emphasized that the Diaphragm Seal would be damaged by allowing the pump to operate in a cavitating condition for an extended period of time. A change in the Field Test phase of the program was made regarding choice of field test site. There is no operating Syn-Fuel pilot plant capable of inexpensively producing the slurry stream required for the reciprocating pump testing. The Field Tests will now be conducted by first testing the prototype pump and separation seals in an ambient temperature sand water slurry. This will determine resistence to abrasive wear and determine any operation problems at pressure over a lengthy period of time. After successful conclusion of these tests the pump and seals will be operated with a high temperature oil, but without solids, to identify any problems associated with thermal gradients, thermal shock and differential growth. After successful completion of the high temperature clean oil tests the pump will be deemed ready for in-line installation at a designated Syn-Fuel pilot plant. The above approach avoids the expense and complications of a separate hot slurry test loop. It also reduces risk of operational problems while in-line at the pilot plant. 5 figs.

  7. (Pittsburgh Energy Technology Center): Quarterly technical progress report for the period ending December 31, 1985

    SciTech Connect

    Not Available

    1986-10-01

    Microbial desulfurization is the use of ''bugs'' to remove sulfur from coal. Four projects illustrate the variety of ways in which microbes can be used to desulfurize coal. In the liquefaction program area, a joint effort between PETC and Catalytic, Inc., was established for process-modeling studies of two-stage coal liquefaction experiments at Wilsonville. Researchers at PETC have developed a process model for Integrated Two-Stage Liquefaction and are currently focusing on characterization of an engineering (ASPEN Public) simulator. The goal of this work is to establish realistic process performance indices for different reactor configurations and coal feedstocks based on heat and material balance calculations. In another liquefaction research effort this quarter, Hydrocarbon Research, Inc., started the first bench run under its new contract for research on low-severity, two-stage liquefaction. The run is planned for 29 days and will test nine separate operating conditions. Research in the field of magnetohydrodynamics (MHD) continued at the Avco Everett Research Laboratory (AERL). A significant achievement fiscal year was the first-time operation of the Avco MK VIII channel with the total power controlled and/or consolidated using nonresistive circuitry. An electrostatic precipitator (ESP) was delivered, installed, and tested at the DOE's MHD Coal-Fired Flow Facility at the University of Tennessee Space Institute. Shakedown tests of PETC's Continuous Life-Cycle Copper Oxide Test Facility are complete. This PETC facility will be used to conduct the first integrated process tests of the Fluidized-Bed Copper Oxide Process unit for the control of SO/sub 2/ and NO/sub x/. PETC has recently initiated a project to study the fundamental properties of coal surfaces by measuring the heat of immersion of coal and its associated mineral matter using a Setaram C-80 heat flow calorimeter.

  8. Fundamental mechanisms in flue gas conditioning. Quarterly technical progress report, April 1995--June 1995

    SciTech Connect

    Snyder, T.R.; Bush, P.V.

    1995-07-11

    This project is divided into four tasks. We developed our Management Plan in Task 1. Task 2, Evaluation of Mechanisms in FGD Sorbent and Ash Interactions, focused on characteristics of binary mixtures of these distinct powders. Task 3, Evaluation of Mechanisms in Conditioning Agents and Ash, was designed to examine effects of various conditioning agents on fine ash particles to determine mechanisms by which these agents alter physical properties of ash. We began Tasks 2 and 3 with an extensive literature search and assembly of existing theories. We completed this phase of the project with publication of two special Topical Reports. In our literature reviews reported in Topical Reports 1 and 2, we emphasized the roles adsorbed water can have in controlling bulk properties of powders. During the next phase of the project we analyzed a variety of fly ashes and fine powders in the laboratory. The experiments we performed were primarily designed to define the extent to which water affects key properties of ashes, powders, and mixtures of sorbents and ashes. We have recently completed a series of pilot-scale tests designed to determine the effects that adsorbed water has on fabric filtration and electrostatic precipitation of entrained fly ash particles in actual flue gas environments. Under Task 4 we will issue our Final Report that will summarize the results of our laboratory and pilot-scale work and will also include a model of flue gas conditioning. Our efforts during this reporting quarter have been directed toward production of the Draft Final Report and the Flue Gas Conditioning Model. In addition to these efforts, we have prepared a paper for presentation at the Eleventh Annual Coal Preparation, Utilization, and Environmental Control Contractor`s Conference to be held in Pittsburgh in July, 1995.

  9. Development of analytical procedures for coprocessing. Quarterly technical progress report, January 1, 1991--March 31, 1991

    SciTech Connect

    Anderson, R.P.

    1991-06-01

    This is the tenth quarterly report under DOE Contract No. DE-AC22-88PC88810, Development of Analytical Procedures for Coprocessing. The overall objective of the contract is to improve understanding of the fundamental chemistry of coprocessing. A primary objective is to evaluate methods to distinguish between compound classes originating from coal versus those originating from petroleum resid while a corollary objective is to provide detailed knowledge on the composition of coprocessing products. This report summarizes work conducted in support of the latter objective in which process development unit samples produced by HRI, Inc. are being subjected to detailed analysis. Coprocessing resid samples selected for detailed analysis were made under constant conditions except for variations in coal concentration or in the coal (New Mexico subbituminous or Texas lignite). The soluble material was separated into strong and weak acids, strong and weak bases, and neutrals. The predominant fraction from the ABN separations was the neutral fraction (67-81%). All of the polar fractions increase with increasing coal concentration. The concentration of saturates in the neutrals is high in a run with 33% subbituminous coal but drops substantially with either increasing coal concentration or the substitution of lignite for subbituminous coal. High temperature gas chromatography showed that both the neutral aromatics fractions and saturates fractions from all of the runs are extremely similar regardless of the coal concentration or coal type. The neutral aromatics fractions were further separated by ring number separation. Chromatograms were again very similar regardless of the initial coal concentration or coal type with most material eluting in the 3-ring to 6-ring region.

  10. (Pittsburgh Energy Technology Center): Quarterly technical progress report, period ending September 30, 1986

    SciTech Connect

    Not Available

    1986-01-01

    Among the major energy technology milestones was the selection of nine projects by the US DOE that will demonstrate innovative clean coal technologies under the nearly $400 million first phase of the Clean Coal Technology Program. Four of the projects, which are to be cost-shared by private industry, were assigned to PETC for negotiation and management. A DOE contractor, the Union Carbide Corp., has filed three patent applications for the development of Fischer-Tropsch catalysts. The improvements in synthesis gas conversion technology resulting from these inventions include lower methane production, increased yield of non-gaseous products; higher yield of olefins; improved levels of single-pass, synthesis gas conversion; and greater catalyst stability. A major impetus this quarter was in flue gas cleanup technology that seeks to develop low-cost options for controlling pollutants produced from coal combustion. As part of an experimental program to study the direct injection of sorbent into a duct for combined SO/sub 2//NO/sub x/ removal, researchers at the University of Tennessee Space Institute characterized the hydrodynamics of the injection process. Nearly all of the design work was completed for the first part of General Electric's Environmental Services Division's contract that involves the design and construction of a 12-MW proof-of-concept plant to test SO/sub 2/ removal by spraying a sorbent directly into the flue gas contained in a duct. Researchers at PETC are investigating a technique called explosive comminution, or shattering of the coal into very small bits, to produce a premium low-ash, low-sulfur solid fuel. Significant milestones were achieved in PETC's MHD.

  11. Preliminary evaluation of resinite recovery from Illinois coal. [Quarterly] technical report, September 1--November 30, 1994

    SciTech Connect

    Crelling, J.C.

    1994-12-31

    Resinite is a naturally occurring substance found in coal and derived from original plant resins. It is ubiquitous in North American coals. It makes up one to four percent by volume of most Illinois coals. It has been commercially exploited in the western USA for use in adhesives, varnishes and thermal setting inks. The overall objective of this project is to compare the properties of the resinite contained in Illinois Basin coals to resinite being commercially exploited in the western United States, and to recover the resinite from Illinois coals by microbubble column floatation techniques. The significance of this study is that it has the potential to show the way to recover a valuable chemical, resinite, from coal using only physical processing techniques. The value of the resinite at $1.00/kg or $0.50/lb makes it about fifty times more valuable than steam coal. The removal of resinite from coal does not decrease the value of the remaining coal in any way. The unique aspects are that: (1) it is the first examination of the resinite recovery potential of Illinois coal, (2) it integrates the latest characterization techniques such as density Gradient centrifugation, microspectrofluorometry, and gas chromatography- mass spectrometry, and (3) it uses microbubble column flotation to determine the resinite recovery potential. During this quarter samples were obtained, information from both the databases of both the Illinois State Geological Survey (ISGS) and the Pennsylvania State University (PSU) was obtained and evaluated, and EBCSP samples from the Herrin No. 6, the Springfield No. 5 and the Colchester No. 2 seams were analyzed petrographically and the resinites in these samples were characterized by fluorescence spectral analysis.

  12. Direct catalytic decomposition of nitric oxide. Quarterly technical progress report No. 10, January--March 1994

    SciTech Connect

    Flytzani-Stephanopoulos, M.; Sarofim, A.F.; Zhang, Y.; Sun, T.

    1994-06-01

    This project investigates a suitable catalyst system for the direct nitric oxide decomposition in post-combustion gas streams. This process does not use a reductant, such as the ammonia used in the Selective Catalytic Reduction (SCR) of NO{sub x} to nitrogen. Therefore, it is a greatly simplified process basically involving passing the flue gas through a catalytic converter. Catalysts are prepared by incorporating metal cations into zeolite supports according to ion exchange procedures widely used in preparation of metal/zeolite catalysts. Particular emphasis is given in this work on promoted Cu-exchanged zeolites, especially the catalyst systems Mg/Cu-ZSM-5 and Ce/Cu-ZSM-5, which are promising for NO conversion to nitrogen at typical flue gas O{sub 2} and NO levels and over the temperature range of 673--873{degrees}C. The effect of zeolite modification, copper exchange level and catalyst preparation conditions on the catalytic activity are studied in O{sub 2}-free, O{sub 2}-rich gases, as well as wet (2--20% H{sub 2}O) gas streams in a packed-bed microreactor. Characterization of catalysts is performed by XRD, STEM, TEM and ESR. During this quarter it was found that severe steaming (20% H{sub 2}O) of Na-ZSM-5 at temperatures above 600{degrees}C caused partial vitreous glass formation and dealumination. Unpromoted Cu-ZSM-5 catalysts suffer drastic loss of NO decomposition activity in wet gas streams at 500{degrees}C. Activity is partially recovered in dry gas. Copper migration out of the zeolite channels leading to CuO formation has been identified by STEM/EDX. In Ce/Cu-ZSM-5 catalysts the wet gas activity i`s greatly improved. CuO particle formation is less extensive and the dry gas activity is largely recovered upon removal of the water vapor.

  13. MHD Integrated Topping Cycle Project. Fifteenth quarterly technical progress report, February 1991--April 1991

    SciTech Connect

    Not Available

    1992-02-01

    A summary of the work is excerpted here. Final design of an MHD channel for the ITC program POC test has been completed. The channel was designed to be capable of 1.5 MW {sub e} power output and a lifetime of 2000 hours. Emphasis was placed upon durability and reliability. Hence, specific measures were taken to design against channel damage due to electric faults. The life-limiting issues associated with electrochemical corrosion and erosion of gas-side surfaces were addressed by the use of various materials with proven wear characteristics in a coal-fired MHD channel environment. Pitting of prototypical sidewall coupons was observed in the CDIF workhorse testing. The most likely cause of the observed pitting, water leaks resulting from cooling water tube braze failures, has been remedied. New brazing procedures and isolation of the sidebar gas-side material from water contact will prevent sidebar pitting in the prototypical channel. Water-side corrosion tests reported in this quarterly report include the latest results of tungsten-copper elements at controlled pH, heat flux and voltage levels. In the combustion subsystem, efforts continued to focus on understanding and improving the current levels of slag recovery and seed utilization achieved by the combustor. Analytical support was also provided in the areas of slag rejection system operation, precombustor operation, and oil burner design modification. Channel data analysis activities continued in support of prototypical coupon testing at the CDIF. Analyses are presented on channel wall slagging behavior and sidewall voltage distributions.

  14. Quarterly technical progress report for the period ending June 30, 1984

    SciTech Connect

    Not Available

    1984-10-01

    The Magnetohydrodynamics Program (Component Development and Integration Facility) in Butte, Montana, continued its site preparation for the TRW first-stage combustor installation. In the area of flue gas cleanup, our in-house research program is continuing its investigation into the causes of sorbent attrition in PETC's fluidized-bed copper oxide process for simultaneous SO/sub 2//NO/sub x/ removal. Interwoven with these tests is a series of spray dryer/electrostatic precipitator tests that are being conducted with the cooperation of Wheelabrator-Frye, Inc. This test series was completed this quarter, and the data show that when using a Kentucky coal, Wheelabrator-Frye's electrostatic precipitator provides excellent particulate control efficiency while using a spray dryer for sulfur dioxide removal. A unique project at Carnegie-Mellon University is looking at the concept of integrated environmental control for coal-fired power plants making use of precombustion, combustion, and postcombustion control, including systems for the simultaneous removal of more than one pollutant. The objective of this research is to develop a computer model and assessment for integrated environmental control systems that utilize conventional or advanced systems. The Liquid Phase Methanol Project Development Unit in LaPorte, Texas, was restarted after a successful shakedown run was completed. PETC has recently begun an in-house research project aimed at exploring the basic chemistry of liquefying coal in the presence of water under supercritical conditions. In the Alternative Fuels Technology Program, the Gulf Research and Development Company has completed the preliminary testing phase of its erosion test loop. Their results indicate that when pumping a coal-water slurry fuel through a flow loop, the erosion rate increases as velocity increases, suggesting a well-defined relationship between these two parameters.

  15. Solvent Refined Coal (SRC) process. Quarterly technical progress report, January 1979-March 1979

    SciTech Connect

    Not Available

    1980-02-01

    This report summarizes the progress of the Solvent Refined Coal (SRC) Project by the Pittsburg and Midway Coal Mining Co. for the Department of Energy for the period January 1, 1979 to March 31, 1979. Activities included the operation and modification of the Solvent Refined Coal Pilot Plant at Fort Lewis, Washington; the Process Development Unit P-99 at Harmarville, Pennsylvania; and research at Merriam Laboratory in Merriam, Kansas. The Pilot Plant processed Powhatan No. 5 Coal in the SRC-II mode of operation studying the effect of coal particle size and system temperature on coal slurry blending and the effect of carbon monoxide concentration in the reaction feed gas on process yields. January and February were spent completing installation of a fourth High Pressure Separator on Process Development Unit P-99 to better simulate operating conditions for the proposed Demonstration Plant. During March, one run was completed at P-99 feeding Pittsburgh Seam Coal from the Powhatan No. 5 Mine. Merriam investigations included a study of the effect of iron containing additives on SRC-I operation, the addition of carbon monoxide to the feed gas, utilization of a hydrogenated solvent (Cresap process solvent) in the SRC-I mode under both normal and short residence time operating conditions, and development of a simulated distillation technique to determine the entire boiling range distribution of product oils.

  16. Acoustic agglomeration of power plant fly ash: Quarterly technical report, November 5, 1986--February 5, 1987

    SciTech Connect

    Reethof, G.

    1987-03-20

    The objective of this project is to complete the investigations on the use of high intensity acoustic energy to agglomerate micron and submicron sized particulates in fly ash aerosols in order to provide the necessary scientific knowledge and design criteria for the specification of technically and economically viable intermediate flue gas treatment of coal fired power plants. The results of the project are to provide technical and economic information for the better development and evaluation of potential fine particulate control systems. The goals of the proposed work are to further the understanding of certain fundamental processes by means of theoretical and experimental investigations, to include this knowledge in an advanced computerized model of the agglomeration processes. Tests with the two acoustic agglomerators available in Penn State's new High Intensity Acoustics Laboratory will be used to verify the results from the agglomeration simulation. Research work will continue on high power, high efficiency sirens with special emphasis on the nonlinear acoustic phenomena and novel means of significantly increasing siren efficiency. A study will be carried out to evaluate the economics of conventional coal fired power plant clean-up systems using acoustic agglomerators as intermediate flue gas treatment.

  17. H-Area, K-Area, and Par Pond Sewage Sludge Application Sites Groundwater Monitoring Report. Fourth quarter 1994 and 1994 summary

    SciTech Connect

    Chase, J.A.

    1995-04-01

    Groundwater samples from the three wells at the H-Area Sewage Sludge Application Site (HSS wells) are analyzed quarterly for constituents as required by South Carolina Department of Health and Environmental Control Construction Permit 12,076. Samples from the three wells at the K-Area Sewage Sludge Application Site (KSS wells) and the three wells at the Par Pond Sewage Sludge Application Site (PSS wells) are analyzed quarterly for constituents required by SCDHEC Construction Permit 13,173. All samples are also analyzed as requested for other constituents as part of the Savannah River Site Groundwater Monitoring Program. Annual analyses for other constituents, primarily metals. also are required by the permits.

  18. Bench-scale testing of the multi-gravity separator in combination with microcel. Fourth quarterly report, July 1, 1993--September 30, 1993

    SciTech Connect

    Not Available

    1993-12-06

    Work this quarter included equipment installation, shakedown testing, and the beginning of the detailed testing program. With the exception of ongoing Task 4: Sample Characterization, Tasks 1 through 8 are now complete. Task 10: Detailed Testing and Task 12: Sample Analysis began this quarter and will consume all available time during the 5th quarter. Installation and testing of the process equipment, mechanical systems, as well as the electrical systems were completed. The shakedown process uncovered several necessary modifications to the circuit which were subsequently completed. Most of the changes concerned piping and valving modifications which allowed for better material flow and sampling. The circuit was operated with coal to determine the time for each unit to reach steady state. The primary objective of the proposed work is to design, install, and operate an advanced fine coal processing circuit combining the Microcel{trademark} and Multi-Gravity-Separator (MGS) technologies. Both of these processes have specific advantages as stand-alone units. For example, the Microcel column effectively removes ash-bearing mineral matter, while the MGS efficiently removes coal-pyrite composites.

  19. Phase 2: Photovoltaics for utility scale applications (PVUSA). Second quarterly technical report, 1994

    SciTech Connect

    Not Available

    1994-08-01

    Seventy-five people attended PVUSA`s ``Grid-Support PV: Application and Assessment`` workshop in San Francisco on June 9--10. Results from the Kerman project`s distributed benefits evaluation were presented, along with results of four Sandia-sponsored utility case studies. Presentations on SMUD`s and UPVG`s PV programs were given, and several speakers addressed broader issues, such as the role of distributed generation in the changing utility environment, utility restructuring, and PV markets and applications. SMUD`s 200-kW UPG system at their Hedge substation site in Sacramento, California was brought on line in early April and christened at a dedication ceremony on April 18. This system uses SSI modules mounted on twenty rows of UPG-designed one-axis tracking structures, with power fed to a tingle Omnion PCU. In May, SSI notified PVUSA that it would cease additional work on its US-1 system at Davis. Rather than continue development work on both of the system`s Blue Point PCUs, SSI requested to close out its contract with just one of the system`s two PCUs in operation. One unit, inverter ``A``, continued to fail after over two years of troubleshooting and repairs. The other unit, inverter ``B``, has operated reasonablywell, although it too has frequently tripped off line. The half system was mted at 67 kill, 23% less than expected based on one half of the contract target 174 kill. Subsequent I-V curves suggest much of the shortfall may be traced to a 15% shortfall in the dc array field`s maximum power. The EMT and US systems at six PVUSA sites generated nearly 750,000 kWh this quarter, the same energy used by about 500 homes over the same period. For the first half of 1994, the performance index, or ratio of actual to expected generation has exceeded 90%, for six of the twelve completed systems for which data are available. Five of the remaining six systems have generated between 80% and 90% of their expected output.

  20. Advanced direct liquefaction concepts for PETC generic units. Quarterly technical progress report, April 1993--June 1993

    SciTech Connect

    Not Available

    1993-08-01

    Section 1 contains a report of the progress by the University of Kentucky Center for Applied Energy Research on the following tasks: laboratory support (liquefaction in dewaxed and hydrotreated dewaxed solvent); CO pretreatment (effect of process variables on CO pretreatment, CO-pretreated product characterization, and liquefaction results); and iron based dispersed catalysts (production, characterization and testing of sulfated hematites and reaction model development). Section 2 contains a progress report by CONSOL, Inc. on the following tasks: laboratory support; pretreatment work on dewaxing; pretreatment work on agglomeration; and economic evaluation. Progress by Sandia National Laboratories is reported in Section 3 on the following: laboratory support (TGA methods) and solvent pretreatment (coker tar hydrogenation and coal liquefaction results). Section 4 gives a preliminary technical assessment by LDP Associates on the following: baseline economic assessment; assessment of improved coal conversion; and fluid coking.

  1. West Hackberry Tertiary Project. Quarterly technical progress report, September 3, 1993--December 3, 1993

    SciTech Connect

    Fassihi, M.R.; Gillham, T.H.

    1993-11-30

    The goal of the West Hackberry Tertiary Project is to demonstrate the technical and economic feasibility combining air injection with the Double Displacement Process for tertiary oil recovery. The Double Displacement Process is the gas displacement of a water invaded oil column for the purpose of recovering oil through gravity drainage. The novel aspect of this project is the use of air as the injection fluid. The target reservoirs for the project are the Camerina C- 1,2,3 Sands located on the west flank of West Hackberry Field in Cameron Parish, Louisiana. If successful, this project win demonstrate that the use of air injection in the Double Displacement Process can economically recover oil in reservoirs where tertiary oil recovery is presently uneconomical.

  2. Salt Repository Project. Technical progress report for the quarter, 1 April-30 June 1984

    SciTech Connect

    Not Available

    1984-01-01

    This report describes the technical accomplishments during the period from April through June 1984, on the commercial nuclear waste management programs under the direction of the US Department of Energy (DOE), Salt Repository Project Office (SRPO), Office of Nuclear Waste Isolation (ONWI). ONWI's activities within the Salt Repository Project include comprehensive geologic exploration, technology development, equipment testing, and model verification activities, as well as work which supports the design, licensing, construction, operation, and decommissioning activities required to provide geologic repositories and spent fuel handling and packaging facilities. Work in other geologic media (basalt, tuff, and crystalline media such as granite) is carried on by other Office of Civilian Radioactive Waste Management (OCRWM) components. Additionally, development of the technology, methodology, and facilities for interim spent fuel storage, waste treatment, and waste transportation, which are interfacing activities with the terminal isolation activity in the national waste management program, is being carried out in other OCRWM efforts.

  3. Pipeline gas demonstration plant, Phase I. Quarterly technical progress report for September 1980-November 1980

    SciTech Connect

    Eby, R.J.

    1980-12-01

    Work was performed in the following tasks in Phase I of the Pipeline Gas Demonstration Plant Program: Site Evaluation and Selection; Demonstration Plant Environmental Analysis; Feedstock Plans, Licenses, Permits and Easements; Demonstration Plant Definitive Design; Construction Planning; Economic Reassessment; Technical Support; Long Lead Procurement List; and Project Management. The Preliminary Construction Schedule was delivered to the Government on October 3, 1980, constituting an early delivery of the construction schedule called for in the scope of work for Task VI. The major work activity continues to be the effort in Task VI, Demonstration Plant Definitive Design, with two 30% Design Review meetings being held with the Government. Work in Task VII, Construction Planning, was initiated. Work has progressed satisfactorily in the other tasks in support of the Demonstration Plant Program. A Cost Change Proposal was submitted because of an increase in the scope of work and an extension of the schedule for Phase I to 47 months.

  4. Responsive copolymers for enhanced petroleum recovery. Quarterly technical progress report, June 23--September 21, 1994

    SciTech Connect

    McCormick, C.; Hester, R.

    1994-12-31

    Summaries are given on the technical progress on three tasks of this project. Monomer and polymer synthesis discusses the preparation of 1(7-aminoheptyloxymethyl)naphthalene and poly(maleic anhydride-alt-ethyl vinyl ether). Task 2, Characterization of molecular structure, discusses terpolymer solution preparation, UV analysis, fluorescence analysis, low angle laser light scattering, and viscometry. The paper discusses the effects of hydrophobic groups, the effect of pH, the effect of electrolyte addition, and photophysical studies. Task 3, Solution properties, describes the factorial experimental design for characterizing polymer solutions by light scattering, the light scattering test model, orthogonal factorial test design, linear regression in coded space, confidence level for coded space test mode coefficients, coefficients of the real space test model, and surface analysis of the model equations.

  5. Advanced direct liquefaction concepts for PETC generic units. Quarterly technical progress report, April 1994--June 1994

    SciTech Connect

    1994-09-01

    The technical approach of the contract has been expanded to provide additional economic evaluation of related process options. Additional data will be developed in the following areas to facilitate these evaluations. The effect of several modified pretreatments on liquefaction will be investigated. These include catalytic and thermal dewaxing of distillate solvents, the effect that adding light resid to distillate solvent has on hydrotreating and dewaxing, the liquefaction behavior of dense-media separated low-rank coals, and methods of selectively removing oxygen from low-rank coals. Additional chemical, physical, and performance information on improved first-stage catalysts will be developed. Upgrading of ash concentrate to recover catalysts and improve low-rank coals will be assessed. The conversion of residual fractions to distillate by hydropyrolysis will be evaluated. The economic impact of these processes will be determined.

  6. Soot formation in synthetic-fuel droplets. First quarterly technical progress report

    SciTech Connect

    England, G.; Kramlich, J.; Payne, R.

    1981-01-01

    The objective of this project is to provide detailed information on methods of minimizing soot formation during synthetic liquid fuel combustion under conditions which minimize fuel nitrogen conversion to nitric oxide. The program consists of two tasks. The purpose of the first task, Fuel Screening Studies, is to investigate the impact of fuel properties on particulate production, to establish the importance of droplet size and examine atomizer effects, and to develop techniques for surrogate fuels productions. In the second task, Flame Studies, the fundamental details of soot formation from synfuel droplet combustion will be investigated in variable slip velocity configurations. This present report describes technical progress during the first three months of the program effort (October-December 1980). During this initial period, attention has focused on the definition of the different experimental efforts and on the design and construction of the required hardware. Aspects of this work are discussed.

  7. Development and Evaluation of an Experimental Curriculum for the New Quincy (Mass.) Vocational-Technical School. Fourth Quarterly Technical Report, a Vocational Guidance Plan for Junior High School.

    ERIC Educational Resources Information Center

    Morrison, Edward J.; Hudak, Vivian M.

    Activity from January 1 through March 31, 1966 was centered on the derivation of topic objectives for each course of study and on the completion of junior high school guidance program plans. This report describes the procedures for developing the guidance program by describing the guidance program as it now exists in the Quincy Public Schools,…

  8. Bench-scale testing of the micronized magnetite process. Third quarterly technical progress report, January 1995--March 1995

    SciTech Connect

    1995-04-29

    The major focus of the project, which is scheduled to occur through December 1995, will be to install and test a 500{number_sign}/hr. fine-coal cleaning circuit at DOE`s Process Research Facility (PRF), located at the Pittsburgh Energy Technology Center (PETC). The circuit will utilize an extremely fine, micron-sized magnetite media and small diameter cyclones to make efficient density separations on minus-28-Mesh coal. The overall objectives of the project are to: Determine the effects of operating time on the characteristics of the recirculating medium in a continuous integrated processing circuit, and subsequently, the sensitivity of cyclone separation performance to the quality of the recirculating medium; and determine the technical and economic feasibility of various unit operations and systems in optimizing the separation and recovery of the micronized magnetite from the coal products. This report contains a short discussion of the project description, objectives, budget, schedule, and teaming arrangement. The final section contains an outline of the specific project goals for the next quarterly reporting period.

  9. Bioconversion of coal derived synthesis gas to liquid fuels. Quarterly technical progress report, 1 April--30 June 1994

    SciTech Connect

    Jain, M.K.; Worden, R.M.; Grethlein, A.

    1994-07-18

    The overall objective of the project is to develop an integrated two-stage fermentation process for conversion of coal-derived synthesis gas to a mixture of alcohols. This is achieved in two steps. In the first step, Butyribacterium methylotrophicum converts carbon monoxide (CO) to butyric and acetic acids. Subsequent fermentation of the acids by Clostridium acetobutylicum leads to the production of butanol and ethanol. The tasks for this quarter were: development/isolation of superior strains for fermentation of syngas; evaluation of bioreactor configuration for improved mass transfer of syngas; recovery of carbon and electrons from H{sub 2}-CO{sub 2}; initiation of pervaporation for recovery of solvents; and selection of solid support material for trickle-bed fermentation. Technical progress included the following. Butyrate production was enhanced during H{sub 2}/CO{sub 2} (50/50) batch fermentation. Isolation of CO-utilizing anaerobic strains is in progress. Pressure (15 psig) fermentation was evaluated as a means of increasing CO availability. Polyurethane foam packing material was selected for trickle bed solid support. Cell recycle fermentation on syngas operated for 3 months. Acetate was the primary product at pH 6.8. Trickle bed and gas lift fermentor designs were modified after initial water testing. Pervaporation system was constructed. No alcohol selectivity was shown with the existing membranes during initial start-up.

  10. Separation of flue-gas scrubber sludge into marketable products. Third year, second quarterly technical progress report, December 1, 1995--February 29, 1996 (Quarter {number_sign}10)

    SciTech Connect

    Kawatra, S.K.; Eisele, T.C.

    1996-03-01

    To reduce their sulfur emissions, many coal-fired electric power plants use wet flue-gas scrubbers. These scrubbers convert sulfur oxides into solid sulfate and sulfite sludge, which must then be disposed of. Knowledge of scrubber sludge characteristics is necessary for the development of purification technologies which will make it possible to directly utilize scrubber sludges rather than landfilling them. This project is studying the use of minimal-reagent froth flotation as the purification process, using the surface properties of the particles of unreacted limestone to remove them and their associated impurities from the material, leaving a purified calcium sulfite/gypsum product. In the current quarter, research was focused on two different areas. The first part of this quarter the optimization of the feed slurry percent solids for the two inch water-only cyclone was completed. The optimization of the vortex finder, spigot diameter and inlet feed pressure was completed in the previous quarter. The second part of this quarter began the investigation of why water-only cycloning helps froth flotation performance. The hypothesis is that water-only cycloning scrubs the surface of the unreacted limestone. This scrubbing effect provides a clean calcium carbonate surface, which results in better flotation reagent adsorption. This study used the scanning electron microscope to investigate the surface of the unreacted limestone particles.

  11. After Two Years, Three Elementary Math Curricula Outperform a Fourth. NCEE Technical Appendix. NCEE 2013-4019

    ERIC Educational Resources Information Center

    Agodini, Roberto; Harris, Barbara; Remillard, Janine; Thomas, Melissa

    2013-01-01

    This appendix provides the details that underlie the analyses reported in the evaluation brief, "After Two Years, Three Elementary Math Curricula Outperform a Fourth." The details are organized in six sections: Study Curricula and Design (Section A), Data Collection (Section B), Construction of the Analysis File (Section C), Curriculum…

  12. I-NERI Quarterly Technical Report (April 1 to June 30, 2005)

    SciTech Connect

    Chang Oh; Prof. Hee Cheon NO; Prof. John Lee; Prof. William Martin; Prof. James Holloway; Prof. Jong Kim; Prof. Goon Cherl Park

    2005-06-01

    The objective of this Korean/United States/laboratory/university collaboration is to develop new advanced computational methods for safety analysis codes for very-high-temperature gas-cooled reactors (VHTGRs) and numerical and experimental validation of these computer codes. This study consists of five tasks for FY-03: (1) development of computational methods for the VHTGR, (2) theoretical modification of aforementioned computer codes for molecular diffusion (RELAP5/ATHENA) and modeling CO and CO2 equilibrium (MELCOR), (3) development of a state-of-the-art methodology for VHTGR neutronic analysis and calculation of accurate power distributions and decay heat deposition rates, (4) reactor cavity cooling system experiment, and (5) graphite oxidation experiment. Second quarter of Year 3: (A) Prof. NO and Kim continued Task 1. As a further plant application of GAMMA code, we conducted two analyses: IAEA GT-MHR benchmark calculation for LPCC and air ingress analysis for PMR 600MWt. The GAMMA code shows comparable peak fuel temperature trend to those of other country codes. The analysis results for air ingress show much different trend from that of previous PBR analysis: later onset of natural circulation and less significant rise in graphite temperature. (B) Prof. Park continued Task 2. We have designed new separate effect test device having same heat transfer area and different diameter and total number of U-bands of air cooling pipe. New design has smaller pressure drop in the air cooling pipe than the previous one as designed with larger diameter and less number of U-bands. With the device, additional experiments have been performed to obtain temperature distributions of the water tank, the surface and the center of cooling pipe on axis. The results will be used to optimize the design of SNU-RCCS. (C) Prof. NO continued Task 3. The experimental work of air ingress is going on without any concern: With nuclear graphite IG-110, various kinetic parameters and reaction

  13. Upgraded coal interest group. First quarterly technical progress report, October 1, 1994--December 31, 1994

    SciTech Connect

    Weber, W.; Lebowitz, H.E.

    1994-12-31

    The interest group got under way effective January 1, 1994, with nine utility members, EPRI, Bechtel, and the Illinois Clean Coal Institute. DOE participation was effective October 1, 1994. The first meeting was held on April 22, 1994 in Springfield, Illinois and the second meeting was held on August 10--11, 1994 at Johnstown, Pennsylvania. Technical reviews were prepared in several areas, including the following: status of low rank coal upgrading, advanced physical coal cleaning, organic sulfur removal from coal, handling of fine coal, combustion of coal water slurries. It was concluded that, for bituminous coals, processing of fines from coal cleaning plants or impoundments was going to be less costly than processing of coal, since the fines were intrinsically worth less and advanced upgrading technologies require fine coal. Penelec reported on benefits of NOX reductions when burning slurry fuels. Project work was authorized in the following areas: Availability of fines (CQ, Inc.), Engineering evaluations (Bechtel), and Evaluation of slurry formulation and combustion demonstrations (EER/MATS). The first project was completed.

  14. Thermal treatment for chlorine removal from coal. [Quarterly] technical report, March 1, 1992--May 31, 1992

    SciTech Connect

    Muchmore, C.B.; Hesketh, H.E.; Chen, Han Lin

    1992-10-01

    It is the goal of this research to provide the technical basis for development of a process to remove chlorine from coal prior to combustion, based on a thermal treatment process. Under the reaction conditions employed, the behavior of other trace elements of concern will also be evaluated. The recovery of the chlorine removed from the coal as a marketable byproduct, calcium chloride suitable for use as a road deicer, is also being investigated using a novel absorption/crystallization device. A value of 6.29 hr{sup {minus}1} was determined for the dechlorination rate constant of IBC-109 coal at 385{degrees}C, and an activation energy of 34.7 kcal/mol was obtained from an Arrhenius plot over the temperature range of 300--385{degrees}C. A significant removal of chlorine (84.3%) was attained while retaining 92% of the energy of the coal in the solid product by preheating the coal at lower temperatures prior to a six-minute reaction at 385{degrees}C. Volatiles lost during the thermal dechlorination may be recovered for their heating value, and/or as a source of chemical feedstocks; this aspect will require further study, but it appears that the overall energy balance on the system should prove to be favorable. The design of the bench scale fluidized bed thermal dechlorination unit has been completed, and components ordered. Operation of this system should provide the information required for further scale-up of the process.

  15. Pipeline gas demonstration plant, Phase I. Quarterly technical progress report, December 1980-February 1981

    SciTech Connect

    Eby, R.J.

    1981-03-01

    Work was performed in the following areas of the Pipeline Gas Demonstration Plant Program: site evaluation and selection; demonstration plant environmental analysis; feedstock plans, licenses, permits and easements; demonstration plant definitive design; construction planning; economic reassessment; technical support; long lead procurement list; and project management. Major work activity continued to be the effort on Demonstration Plant Definitive Design. A Construction Readiness Audit was held on January 14 to 16, 1981 by a Government/Procon team to review the project and assess the readiness of the project to proceed into the construction phase. Documents for the 60% Design Review were prepared for ICGG review and submitted to the Contracting Officer's authorized representative prior to transmittal to the Corps of Engineers for review. The Corps of Engineers conducted a design audit. The primary objective of the audit was to prepare an independent estimate of the work remaining to complete Phase I of the project. Work continued on the production of a single bid package for the Demonstration Plant, suitable for release to a single constructor, and organized so it can be easily broken down into subpackages by construction specialty. A formal audit of the ICGG R/QA Plan and implementation thereof was performed February 11-12, 1981 by the Corps of Engineers. The Contract Deliverable Final Feedstock-Product-Waste Disposal Plan was delivered to the Government on February 25, 1981.

  16. Advanced Coal Conversion Process Demonstration Project. Quarterly technical progress report, January 1, 1994--March 31, 1994

    SciTech Connect

    1996-02-01

    This report describes the technical progress made on the Advanced Coal Conversion Process (ACCP) Demonstration Project from January 1, 1994, through March 31, 1994. This project demonstrates an advanced, thermal, coal drying process, coupled with physical cleaning techniques, that is designed to upgrade high-moisture, low-rank coals to a high-quality, low-sulfur fuel, registered as the SynCoal{reg_sign} process. The coal is processed through three stages (two heating stages followed by an inert cooling stage) of vibrating fluidized bed reactors that remove chemically bound water, carboxyl groups, and volatile sulfur compounds. After thermal processing, the coal is put through a deep-bed stratifier cleaning process to separate the pyrite-rich ash from the coal. Rosebud SynCoal Partnership`s ACCP Demonstration Facility entered Phase III, Demonstration Operation, in April 1992 and operated in an extended startup mode through August 10, 1993, when the facility became commercial. Rosebud SynCoal Partnership instituted an aggressive program to overcome startup obstacles and now focuses on supplying product coal to customers. Significant accomplishments in the history of the SynCoal{reg_sign} process development are shown in Appendix A.

  17. TIDD PFBC Demonstration Project. First quarterly technical progress report, CY 1993

    SciTech Connect

    Not Available

    1993-04-01

    This is the 24th Technical Progress Report submitted in connection with the cooperative agreement between the DOE and the Ohio Power Company for the Tidd Pressurized Fluidized Bed Combustion (PFBC) Demonstration Plant. This report covers the period from January 1, 1993 to March 31, 1993. The following activities are reported: The unit was operated for a total of 331 hours (including gas turbine air prewarming). There were three gas turbine starts, five bed preheater starts, and two operating periods with coal fire. The peak gross output of 61 MWH was achieved for the period of 2200 to 2300 hours on January 20, 1993. The longest coal fire was 273 hours beginning at 0605 hours on January 20, 1993; total gross generation was 13,453 MWH, and coal consumption was 6,481 tons; The sorbent fines injection system was installed and is ready for use; A totally new secondary ash removal system was designed; New sparge ducts are being fabricated to replace the existing ducts; The plant was found to be in compliance with applicable Ohio regulation after an EPA inspection; and The unit has been out of service since early February due to the failure of the gas turbine. Replacement parts are being fabricated

  18. Soot formation in synthetic-fuel droplets. Second quarterly technical progress report

    SciTech Connect

    England, G.; Kramlich, J.; Payne, R.

    1981-04-01

    The main objective of this program is to provide detailed information on methods of minimizing soot formation during synthetic liquid fuel combustion under conditions which minimize the formation of nitric oxides. The program comprises two main tasks, Fuel Screening Studies, and Flame Studies. The purpose of the first task is to investigate the impact of fuel properties on particulate production, to establish the importance of droplet size and examine atomizer effects, and to develop techniques for surrogate fuels production. In the second task, fundamental details of soot formation from synfuel droplet combustion will be investigated in variable slip velocity configurations. This report describes technical progress during the second three-month period of program effort (January-March 1981). During this period attention has continued to be focussed on the design, construction and commissioning of experimental systems. The Task 1 tunnel furnace modification was completed and made operational, and some preliminary fuel screening studies were carried out. Similarly, construction of the controlled flow droplet reactor was completed and efforts directed towards the design and testing of diagnostic systems. Details of this work are discussed.

  19. Advanced emissions control development program. Quarterly technical progress report No. 9, October 1--December 31, 1996

    SciTech Connect

    Evans, A.P.

    1996-12-31

    Babcock & Wilcox (B&W) is conducting a five-year project aimed at the development of practical, cost-effective strategies for reducing the emissions of hazardous air pollutants (commonly called air toxics) from coal-fired electric utility plants. The need for air toxic emissions controls may arise as the U.S. Environmental Protection Agency proceeds with implementation of Title III of the Clean Air Act Amendment of 1990. Data generated during the program will provide utilities with the technical and economic information necessary to reliably evaluate various air toxics emission compliance options such as fuel switching, coal cleaning, and flue gas treatment. The development work is being carried out using B&W`s new Clean Environment Development Facility (CEDF) wherein air toxics emission control strategies can be developed under controlled conditions, and with proven predictability to commercial systems. Tests conducted in the CEDF provide high quality, repeatable, comparable data over a wide range of coal properties, operating conditions, and emissions control systems. Development work to date has concentrated on the capture of mercury, other trace metals, fine particulate, and the inorganic species hydrogen chloride and hydrogen fluoride.

  20. Jointly sponsored research program quarterly technical progress report, January--March 1994

    SciTech Connect

    Not Available

    1994-08-01

    Progress reports are presented for the following tasks: Development and demonstration of a practical electric downhole steam generator for thermal recovery of heavy oil and tar; wetting behavior of selected crude oil/brine/rock systems; coal gasification, power generation, and product market study; impact of leachate from clean coal technology waste on the stability of clay liners; investigation of coprocessing of heavy oil, automobile shredder residue, and coal; injection into coal seams for simultaneous CO{sub 2} mitigation and enhanced recovery of coalbed methane; optimization of carbonizer operations in the FMC coke process; chemical sensor and field screening technology development; demonstration of the Koppelman ``Series C`` Power River Basin coal as feed; remote chemical sensor development; market assessment and technical feasibility study of PFBC ash use; solid-state NMR analysis and interpretation of naturally and artificially matured kerogens; Crow{trademark} field demonstration with Bell Lumber and Pole; ``B`` series pilot plant tests; and in-situ treatment of manufactured gas plant contaminated soils demonstration program.

  1. Jointly sponsored research program. Quarterly technical progress report, October--December 1993

    SciTech Connect

    Deans, H.A.

    1994-05-01

    This is a progress report on work performed by Western Research Institute for the U.S. DOE, Morgantown Energy Technology Center in the period October- December 1993. Tasks addressed include: development and demonstration of a practical electric downhole steam generator for thermal recovery of heavy oil and tar; wetting behavior of selected crude oil/brine/rock systems; coal gasification, power generation, and product market study; the impact of leachate from clean coal technology waste on the stability of clay liners; investigation of coprocessing of heavy oil, automobile shredder residue, and coal; injection into coal seams for simultaneous CO{sub 2} mitigation and enhanced recovery of coalbed methane; optimization of carbonizer operations in the FMC coke process; chemical sensor and field screening technology development; demonstration of the koppelman {open_quotes}series c{close_quotes} process using a batch test unit with Powder River Basin coal as feed; remote chemical sensor development; market assessment and technical feasibility study of PFBC ash use; solid-state NMR analysis and interpretation of naturally and artificially matured kerogens; Crow{trademark} field demonstration with bell lumber and pole; {open_quotes}B{close_quotes} series pilot plant tests; in situ treatment of manufactured gas plant contaminated soils demonstration program.

  2. Pulverized coal firing of aluminum melting furnaces. Quarterly technical progress report, July 1-September 30, 1979

    SciTech Connect

    West, C E

    1980-09-01

    The ultimate objective of this program is the commercial demonstration of an efficient, environmentally acceptable coal firing process suitable for implementation on melting furnaces throughout the aluminum industry. To achieve this goal, the program has been divided into two phases. Phase I has begun with the design and construction of a 350 pound (coal) per hour staged slagging cyclone combustor (SSCC) attached to a 7-ft diameter aluminum melting ladle furnace. Process development will culminate with a 1000 pph prototype SSCC firing a 40,000 pound capacity open hearth melting furnace at the Alcoa Laboratories. Phase II implementation is currently planned for Alcoa's Lafayette, IN, Works, where two of the ingot plant's five open hearth melting furnaces will be converted to utilize coal. In addition to confirmation of data gathered in Phase I, the effect of extended production schedule operation on equipment and efficiencies will be determined. This work would begin in 1982 pursuant to technical and economic evaluation of the process development at that time.

  3. An investigation of the mechanism of IGA/SCC of alloy 600 in corrosion accelerating heated crevice environments. Quarterly Technical Progress Report No. 4 for the period May 1, 2000 through July 31, 2000

    SciTech Connect

    Dr. Jesse Lumsden

    2000-07-31

    OAK-B135 An investigation of the mechanism of IGA/SCC of alloy 600 in corrosion accelerating heated crevice environments. Quarterly Technical Progress Report No. 4 for the period May 1, 2000 through July 31, 2000

  4. LFCM vitrification technology. Quarterly progress report, July-September 1985

    SciTech Connect

    Burkholder, H.C.; Jarrett, J.H.; Minor, J.E.

    1986-05-01

    This report is compiled by the Nuclear Waste Treatment Program and the Hanford Waste Vitrification Program at Pacific Northwest Laboratory to document progress on liquid-fed ceramic melter (LFCM) vitrification technology. Progress in the following technical subject areas during the fourth quarter of FY 1985 is discussed: melting process chemistry and glass development, feed preparation and transfer systems, melter systems, canister filling and handling systems, off-gas systems, process/product modeling and control, and supporting studies.

  5. Instrumentation of dynamic gas pulse loading system. Technical progress report, first quarter 1992

    SciTech Connect

    Mohaupt, H.

    1992-04-14

    The overall goal of this work is to further develop and field test a system of stimulating oil and gas wells, which increases the effective radius of the well bore so that more oil can flow into it, by recording pressure during the gas generation phase in real time so that fractures can be induced more predictably in the producing formation. Task 1: Complete the laboratory studies currently underway with the prototype model of the instrumentation currently being studied. Task 2: Perform field tests of the model in the Taft/Bakersfield area, utilizing operations closest to the engineers working on the project, and optimize the unit for various conditions encountered there. Task 3: Perform field test of the model in DGPL jobs which are scheduled in the mid-continent area, and optimize the unit for downhole conditions encountered there. Task 4: Analyze and summarize the results achieved during the complete test series, documenting the steps for usage of downhole instrumentation in the field, and compile data specifying use of the technology by others. Task 5: Prepare final report for DOE, and include also a report on the field tests completed. Describe and estimate the probability of the technology being commercialized and in what time span. The project has made substantial technical progress, though we are running about a month behind schedule. Expenditures are in line with the schedule. Increased widespread interest in the use of DGPL stimulation has kept us very busy. The computer modeling and test instrumentation developed under this program is already being applied to commercial operations.

  6. 49 CFR 573.7 - Quarterly reports.

    Code of Federal Regulations, 2014 CFR

    2014-10-01

    ...; (2) For the second calendar quarter (April 1 through June 30), on or before July 30; (3) For the third calendar quarter (July 1 through September 30), on or before October 30; and (4) For the fourth...

  7. 49 CFR 573.7 - Quarterly reports.

    Code of Federal Regulations, 2012 CFR

    2012-10-01

    ...; (2) For the second calendar quarter (April 1 through June 30), on or before July 30; (3) For the third calendar quarter (July 1 through September 30), on or before October 30; and (4) For the fourth...

  8. Hybrid 240 Ton Off Highway Haul Truck: Quarterly Technical Status Report 19, DOE/AL68080-TSR19

    SciTech Connect

    Tim Richter

    2007-06-30

    This nineteenth quarterly status report for the Hybrid Off Highway Vehicle (OHV) project, DOE Award DE-FC04-02AL68080 presents the project status at the end of June 2007, and covers activities in the nineteenth project quarter, April 2007 – June 2007.

  9. Development of vanidum-phosphate catalysts for methanol production by selective oxidation of methane. Quarterly technical progress report, 1996

    SciTech Connect

    McCormick, R.L.; Alptekin, G.O.

    1996-06-01

    Activities this past quarter, focused on acquisition of kinetic data for oxidation of formaldehyde and methanol on these catalysts. In the next quarter these results will be used to propose a simple reaction network and kinetic model. To date we have completed Task 1: Laboratory Setup and Task 2: Process Variable Study. Activities in the current quarter focused on finalizing these tasks and on Task 3: Promoters and Supports, this task is approximately 50% completed. Task 4: Advanced Catalysts is to be initiated in the next quarter. Specific accomplishments this quarter include: finalizing and calibrating a new reaction product analytical system with markedly improved precision and accuracy relative to older. approaches; development of procedures for accurately feeding formaldehyde to the reactor; examination of formaldehyde and methanol oxidation kinetics over vanadyl pyrophosphate at a range of temperatures; and preliminary studies of methane oxidation over a silica support.

  10. Precombustion removal of hazardous air pollutant precursors. Third quarterly technical progress report, April 1, 1996--June 30, 1996

    SciTech Connect

    1996-07-19

    This project involves the development of an optimized, bench-scale processing circuit capable of efficiently removing trace elements from run-of-mine coals. The optimized circuit will be developed using characterization data obtained from detailed washability studies and release analyses tests conducted with several eastern US coals. The optimized circuit will incorporate a variety of conventional and advanced coal cleaning processes which are believed to be the most cost-effective and commercially viable. The coal products from the optimized circuit will be further treated with complexing agents specifically designed to extract organometallic trace elements that are difficult to remove by physical cleaning operations. Finally, innovative bioremediation schemes will be investigated as a means of controlling the release of trace elements from the process waste streams. Emphasis has been placed on the development of a processing circuit which maximizes the rejection of trace elements, minimizes the production of coal fines which are costly to process and less marketable, and minimizes the downstream impacts of the process waste streams on the environment. During the past quarter, the project work plan and all associated technical/management reports were successfully approved. Activities associated with the selection and acquisition of all three base coal samples have also been completed. Characterization work is continuing to move ahead at an accelerated pace in both Subtask 3.2--Washability Analysis and Subtask 3.3-- Flotation Release Analyses. In addition, mineralogical analyses are underway as part of the characterization work. In Task 4--Bench-Scale Testing, the experimental program is now well underway to assess the trace element cleanability of the Pittsburgh No. 8 coal. Effort has also been initiated under Task 4--Toxics Fate Studies to identify viable methods for controlling the release of trace metals from refuse samples for the Pittsburgh No. 8 seam.

  11. Evaluation, engineering and development of advanced cyclone processes. Quarterly technical progress report No. 15, April 1, 1994--June 30, 1994

    SciTech Connect

    1994-12-31

    The project goal is to develop an advanced coal beneficiation technology that can achieve high recovery of the parent coal`s calorific value, while maximizing pyritic sulfur removal. Coal cleaning is to be accomplished by physical means incorporating an advanced form of cycloning or gravimetric process. Evaluation of different media types and their attendant systems for recovery, concentration, and regeneration is to be completed. Phase I, media evaluation, now completed involved a paper study and a number of laboratory tests to eliminate all but the best media options. Phase II, media testing, involved detailed testing of the more promising media and separators in a closed-loop pilot facility circuit. In the final phase, Phase III, it is proposed to test individual components of the process using the optimum medium, separator, and medium recovery systems(s) selected in prior phases. Some of the highlights for this reporting period are: (1) Outomec conducted a second set of hot water wash experiments. These hot water experiments, using prefiltered medium, yielded a significant improvement in calcium nitrate recovery, and showed a consistent decrease in residuum calcium nitrate with increasing wash rate. (2) Several alternatives were investigated for potential reduction in thermal regeneration process costs. Culligan, Spin Tek, and Rochem, manufacturers of reverse osmosis or ultra filtration systems were contacted. Rochem ultimately performed laboratory experiments. Starting with a dilute medium density of 1.07, the Rochem laboratory system achieved a density of 1.11. A density of 1.22 sg would be commercially attainable. This is less than the target medium density of 1.35, meaning that if their system were utilized, some thermal means would still be required to regenerate medium to operating density. (3) Management and Technical Systems initiated work on a preliminary economic study and will submit a report during the next quarterly reporting period.

  12. Development and Testing of Industrial Scale, Coal Fired Combustion System, Phase 3: Twentieth quarterly technical progress report, October 1-December 31, 1996

    SciTech Connect

    Zauderer, Bert

    1997-02-27

    In the fourth quarter of calendar year 1996, 15 days of combust boiler tests were performed, including 10 days of tests on a parallel DOE sponsored project on sulfur retention in a slagging combustor. Between tests, modifications and improvements that were indicated by these tests were implemented. This brings the total number of test days to the end of December in the task 5 effort to 57, increased to 65 as of the date of this Report, 1/27/97. This compares with a total of 63 test days needed to complete the task 5 test effort, and it completes the number of tests days required to meet the task 5 project plan. The key project objectives of the areas of combustor performance and environmental performance have been exceeded. With sorbent injection in the combustion gas train, NO{sub x} emissions as low as 0.07 lb/MMBtu and SO{sub 2} emissions as low as 0.2 lb/MMBtu have been measured in tests in this quarter. Work in the next quarter will focus on even greater reductions in environmental emissions. Also tests are planned with coals other than the Eastern U.S. bituminous coals tested in this project. For example, it is planned to tests Indian coals whose ash concentration is in the 40% range.

  13. Build, install and demonstrate a variable stroke pump control and windmill system: 2nd quarterly technical progress report

    SciTech Connect

    Not Available

    1986-12-30

    Most of the time during the second quarter has been spent on the new gear drive. At the end of the 1st quarter the VSM (Variable Stroke Mechanism) was approximately 50% complete. Some work was done the second quarter on the VSM. An all steel mount was nearly completed for the hydraulic cyclinder. The purchased parts to finish the plumbing are on hand, the feedback control chain purchased, and one of the two pulleys was made. A safety device, that could be optional, is being designed and constructed. This addition would prevent damage to the equipment if all of the hydraulic fluid were lost for some reason.

  14. TIMSS 2003 Technical Report: Findings from IEA's Trends in International Mathematics and Science Study at the Fourth and Eighth Grades

    ERIC Educational Resources Information Center

    Martin, Michael O., Ed.; Mullis, Ina V.S., Ed.; Chrostowski, Steven J., Ed.

    2004-01-01

    This volume describes the technical aspects of TIMSS 2003 and summarizes the main activities involved in the development of the data collection instruments, the data collection itself, and the analysis and reporting of the data. The thirteen chapters contained herein are: (1) Overview of TIMSS 2003 (Michael O. Martin and Ina V. S. Mullis); (2)…

  15. Study of the effects of ambient conditions upon the performance of fan powered, infrared, natural gas burners. Quarterly technical progress report, October 1, 1996--December 31, 1996

    SciTech Connect

    Bai, T.

    1997-01-01

    This quarterly technical progress report describes work performed under DOE Grant No. DE-FG22-94MT94011 during the period September 1, 1996 to December 31, 1996 which covers the nineth quarter of the project. The objective of this investigation is to characterize the operation of a fan powered infrared burner (IR burner) at various gas compositions and ambient conditions and develop design guidelines for appliances containing PIR burners for satisfactory performance. The fan powered infrared burner is a technology introduced more recently in the residential and commercial markets. It is a surface combustor that elevates the temperature of the burner head to a radiant condition. A variety of metallic and ceramic materials are used for the burner heads. It has been demonstrated that infrared burners produce low CO and NO{sub x} emissions in a controlled geometric space. As the environmental regulations become more stringent, infrared burners are receiving increasing interests.

  16. Engineering development of advanced physical fine coal cleaning technologies: Froth flotation. Quarterly technical progress report No. 15, April 1, 1992--June 30, 1992

    SciTech Connect

    Not Available

    1993-02-12

    The Department of Energy (DOE) awarded a contract entitled ``Engineering Development of Advanced Physical Fine Coal Cleaning Technology - Froth Flotation``, to ICF Kaiser Engineers with the following team members, Ohio Coal Development Office, Babcock and Wilcox, Consolidation Coal Company, Eimco Process Equipment Company, Illinois State Geological Survey, Virginia Polytechnic Institute and State University, Process Technology, Inc. This document a quarterly report prepared in accordance with the project reporting requirements covering the period from July 1, 1992 to September 30, 1992. This report provides a summary of the technical work undertaken during this period, highlighting the major results. A brief description of the work done prior to this quarter is provided in this report under the task headings.

  17. Application of integrated reservoir management and reservoir characterization to optimize infill drilling. Quarterly technical progress report, September 13--December 12, 1996

    SciTech Connect

    1996-12-12

    Eighteen 10-acre infill wells have been drilled and completed as part of the Field Demonstration phase of the project at the North Robertson (Clearfork) Unit (NRU). The fourteen producing wells are pumped-off and producing at stable rates. The four injection wells are completed and have been on injection for three to four weeks. Current Unit production is approximately 3,400 STBO/D, of which approximately 900 STBO/D is being produced from the 10-acre infill wells. A change in the Statement of Work has been approved so that additional 10-acre infill wells can be drilled and/or 20-acre producing wells can be converted to injection during the next quarter as budget constraints and rig availability allow. Technical progress is described for the quarter in many related areas: implementation of the field demonstration; reservoir characterization; reservoir management activities and performance analysis; reservoir simulation; and technology transfer.

  18. [National Institute for Petroleum and Energy Research] quarterly technical report, October 1--December 31, 1992. Volume 2, Energy production research

    SciTech Connect

    Not Available

    1993-04-01

    Accomplishments for the past quarter are described for the following tasks: chemical flooding--supporting research; gas displacement--supporting research; thermal recovery--supporting research; geoscience technology; resource assessment technology; and microbial technology.

  19. Detoxification and generation of useful products from coal combustion wastes: Quarterly technical report, (October--December 1988)

    SciTech Connect

    Not Available

    1988-01-01

    This quarter, samples of dry fly ash, wet bottom ash, and desulfurization gypsum slurry were provided from an Ohio Edison power plant. Chemical analysis mineralogical examination, and an anion analysis were performed on the samples. 2 figs., 1 tab. (CBS)

  20. Flow and design characteristics of the hydrocyclone for the recovery of coal fines. Fourth quarterly report, June 1-August 31, 1982

    SciTech Connect

    Davis, P.K.

    1982-01-01

    The new hydrocyclone system has been completed and is in operation. The design of this system was described in the second quarterly report. The system has performed even beyond our expectations. Parameters that can be varied on this system include flow rate, inlet area, hydrocyclone chamber length, vortex finder diameter and length, underflow diameter and cone angle (from 20/sup 0/ to 120/sup 0/ in 20/sup 0/ increments). This hydrocyclone is much more flexible than the original system; however, both systems are being utilized in this research. Modifications and improvements to the new system that have already been incorporated include the purchase and installation of a doppler flowmeter with digital display. This meter is especially nice in that the sensors are clamped to the outside of the pipe and consequently, do not disturb the flow. The system with digital readout was purchased for $2600. The system has also been modified so that the hydrocyclone now effectively discharges to the atmosphere. Data using the spheres in the new system has been taken to further investigate the effect of cone angle. Studies presently underway address the affects of variable hydrocyclone length (cylindrical portion) on the efficiency of the system.

  1. Quarterly Technical Progress Report

    SciTech Connect

    Mary K. Banken

    1998-06-30

    This project has identified all FDD oil reservoirs in Oklahoma; grouped those reservoirs into plays that have similar depositional origins; collected, organized, and analyzed all available data; conducted characterization and simulation studies on selected reservoirs in each plays; and implemented a technology transfer program targeted to the operators of FDD reservoirs. By fulfilling these objectives, the FDD project has had the goal of helping to sustain the life expectancy of existing wells and provide incentive for development and exploratory wells with the ultimate objective of increasing oil recovery.

  2. Quarterly Technical Progress Report

    SciTech Connect

    Yi Hua Ma

    1998-03-16

    The temperature dependence of the oxygen flux across the BaCe0G03 dense membrane (BCG membrane) tube was investigated. In the temperature range of 688C to 955C, the increase in the oxygen flux with temperature obeyed the Arrhenius law. An increase in the helium sweep flow membrane tube. rate in the tube side resulted in an increase in the oxygen flux through the The oxygen fluxes through the BCG dense membrane tube were measured at different oxygen partial pressures in the shell side. The oxygen flux increased with the oxygen partial pressure in the shell side. The BCG dense membrane was tested in a membrane reactor for the catalytic oxidative coupling of methane. The BCG membrane is not a complete combustion catalyst, and the catalytic activity of the BCG membrane was found to be much higher than the Argonne dense membrane. As the oxygen partial pressure in the shell side increased, the C2 decreased while the C2 yield remained unchanged, indicating that non-selective, reactions still played a significant role in the membrane reactor.

  3. Great Plains Coal Gasification Project, Mercer County, North Dakota. Quarterly technical and environmental report, second quarter, 1984. [Mercer County, North Dakota

    SciTech Connect

    Not Available

    1984-01-01

    Project activities remain on schedule to meet Great Plains Gasification Associates' full gas production date. Detailed engineering is complete for the gasification plant. The only remaining engineering tasks involve field support activities and special projects. Construction is nearly complete. The majority of the remaining tasks involve civil, painting and electrical work. Start-up operations are proceeding very well. Many significant achievements were accomplished during the quarter. Coal was successfully gasified with oxygen. All of the first train's seven gasifiers completed successful production test runs. The only remaining plant permit is the Permit to Operate, which is expected to be issued in late 1985. Quality assurance/quality control activities included major equipment inspections, development of welding procedures and equipment turnover inspections. Freedom Mine development activities remain on schedule.

  4. A novel carbon-based process for flue gas cleanup. Third quarterly technical progress report, January 1--March 31, 1992

    SciTech Connect

    Gangwal, S.K.; Silveston, P.L.

    1992-04-01

    The objective of this project is to demonstrate the preliminary technical and economic feasibility of a novel carbon-based process for removal of at least 95% SO{sub 2} and at least 75% NO{sub x} coal combustion flue gas. In the process, flue gas leaving the electrostatic precipitator (ESP) is passed through a trickle bed of achieved carbon catalyst employing a periodic flush of low strength sulfuric acid. The SO{sub 2} is oxidized to SO{sub 3} and removed as medium strength sulfuric acid. The SO{sub 2}-free flue gas is then mixed with NH{sub 3}, and the NO{sub x} in the gas is subjected to selective catalytic reduction (SCR) to N{sub 2} over a fixed bed of activated carbon catalyst. The experimental work is divided between Research Triangle Institute (RTI) and the University of Waterloo (Waterloo). RTI will conduct the NO{sub x} removal studies, whereas Waterloo will conduct the SO{sub 2} removal studies. The ultimate goal of the project is to demonstrate that the process can be reduce the cost of electricity by 20% over conventional SCR/flue gas desulfurization (FGD) processes. In the present quarter, the continuous SO{sub 2} analyzer system at Waterloo was completed. The SO{sub 2} removal factorial experiments were begun Waterloo with the BPL carbon at 21{degrees}C. Also, SO{sub 2} removal was tested on two catalyst at RTI at 80{degrees}C. NO{sub x} conversion was tested on a variety of catalysts at RTI. It was shown that the BPL carbon could remove over 95% SO{sub 2} at 21{degrees}C but would required several beds at space velocity in each bed of abut 1,500 scc/(cc{center_dot}h) to reduce SO{sub 2} from 2,500 ppm to 100 ppm. A modified carbon catalyst tested at RTI showed 99% SO{sub 2} removal at 80{degrees}C at 1,400 scc/(cc{center_dot}h). Also, it was possible to produce nearly 9 normal H{sub 2}SO{sub 4} by periodic flushing of this catalyst. The modified carbon catalyst also demonstrated removal of more than 80% NO{sub x}. 7 refs., 7 figs., 4 tabs.

  5. Technical Progress Report for PEPCO: Turbo-Z Battery Charging System. Calendar Quarter Ending March 31, 1999

    SciTech Connect

    2000-04-01

    The project is proceeding at a rapid pace now. The software is in development for the control board and the test stand. Portions of the writing and debugging of this software have been in conjunction with the hardware development. The software now interfaces with all the measurement instruments and displays the measurements on the screen, and it saves the measurements to a disc file. There is still cleanup work to do on the display items. Work must still be imparted to the code to control a charging sequence while taking measurements of the results. The test stand hardware has received a good development effort this quarter. The timer-counter board is working in the computer. This board paces the measurement cycle and times the discharge pulse (whine circuit). The thermocouple multiplexer is scanning at the same time the analog to digital converter is taking measurements. We have made a good number of hardware modifications to solve problems revealed while writing the software. The power factor correction for the charger power section is still in development. The engineers have found additional sources for the PFC chips, and they have obtained more technical data sheets and acquired samples. The control board schematics are complete, and the software is far along in the development phase. The functions of the control board have been detailed. The control board must next be integrated with the power supply unit. The next phase of development will concentrate on integrating the components together. At this time, the final debugging of the hardware and software will begin. Additionally, the capacitive coupler development is proceeding. The annual DARPA/DoT Advanced Transportation review will be held on May 16, 1999. We expect to learn the status of our project proposal during this conference. Should we more forward, UL has agreed to help us determine the design requirements of the complete charging system at their EV testing facility, prior to manufacturing. This

  6. Develop data management system for assistance in conducting area of reviews in Texas: Quarterly technical report- 10th quarter, January 1-March 31, 1997

    SciTech Connect

    Wrotenbery, L.; Burgess, D. F.; Weitzel, L.; Williams, D.; Morgan, H.; Matthews, J.

    1997-04-15

    The following technical report provides a detailed status report of the DOE grant project entitled `Develop Data Management System for Assistance in Conducting Area of Reviews (AORS) in Texas.` The grant funding allocated is for the purpose of providing the Railroad Commission of Texas (Commission or RRC) with resources and capabilities to conduct AOR and AOR variance analysis statewide.

  7. Production and screening of carbon products precursors from coal. Quarterly technical progress report No. 5, January 1,1996--March 31, 1996

    SciTech Connect

    1996-04-01

    Individual quarterly reports of four industrial participants of this project are included in this report. The technical emphasis continues to be the supply of coal-based feedstocks to the industrial participants. There have been several iterations of samples and feedback to meet feedstock characteristics for a wide variety of carbon products. Technology transfer and marketing of the Carbon Products Consortium (CPC) is a continual effort. Interest in the program and positive results from the research continue to grow. In several aspects, the program is ahead of schedule.

  8. POC-scale testing of an advanced fine coal dewatering equipment/technique. Quarterly technical progress report 6, January--March 1996

    SciTech Connect

    Tao, D.; Groppo, J.G.; Parekh, B.K.

    1996-05-03

    Froth flotation technique is an effective and efficient process for recovering of ultra-fine clean coal. Economical dewatering of an ultra-fine clean coal product to a 20% level moisture will be an important step in successful implementation of the advanced cleaning processes. This project is a step in the Department of Energy`s program to show that ultra-clean coal could be effectively dewatered to 20% or lower moisture using either conventional or advanced dewatering techniques. The cost-sharing contract effort is for 36 months beginning September 30, 1994. This report discusses technical progress made during the quarter from January 1- March 31, 1996.

  9. Development of vanadium-phosphate catalysts for methanol production by selective oxidation of methane. Quarterly technical progress report No. 9, April 1995--June 1995

    SciTech Connect

    McCormick, R.L.

    1995-09-14

    This document is the ninth quarterly technical progress report under Contract No. DE-AC22-92PC92110 {open_quotes}Development of Vanadium-Phosphate Catalysts for Methanol Production by Selective Oxidation of Methane{close_quotes}. Activities were focused on fine tuning of the microreactor system by elimination of transport effects and improvements in the analytical system. Process variable studies were conducted on vanadyl pyrophosphate and screening studies were conducted on several modified catalyst. One additional catalyst was prepared and characterization studies continued. These results are reported.

  10. Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, November 1991--January 1992

    SciTech Connect

    Not Available

    1992-08-01

    The objective of this research is to develop information to be used by private industry and government agencies for planning waste disposal practices associated with advanced coal processes. To accomplish this objective, DOE has contracted Radian Corporation and the North Dakota Energy & Environmental Research Center (EERC) to design, construct, and monitor a limited number of field disposal tests with advanced coal process wastes. These field tests will be monitored over a three year period with the emphasis on collecting data on the field disposal of these wastes. Accomplishments for this past quarter are as follows: The 9th quarterly measurements at the Colorado site took place in December, 1991. Permeability and neutron absorption moisture content measurements were made and on site data was collected from the data logger; The 9th quarterly sampling at the Ohio site took place in November 1991. Permeability and moisture content measurements were made, and water samples were collected from the wells and lysimeters; The second quarterly core and water samples from the first Illinois test case were collected in mid November, and field data were collected from the data logger; Chemical analysis of all core and water samples continued; all chemical analyses except for some tests on Illinois second quarter cores are now complete.

  11. Development of vanadium-phosphate catalysts for methanol production by selective oxidation of methane. Quarterly technical progress report No. 6, July--September 1994

    SciTech Connect

    McCormick, R.L.

    1995-01-10

    This is the eighth quarterly technical progress report. During this quarter the project was initiated, after transfer via a novation agreement, at the Colorado School of Mines. Project initiation activities have included: set up of catalyst synthesis apparatus; training on x-ray diffraction and FTIR apparatus; set up of catalyst testing reactor; set up of reactor product analytical systems; and set up of method development for measuring catalyst acidity via FTIR. At the end of this quarter significant progress had been made towards completion of these initiation activities. Several catalyst syntheses have been performed and the catalysts characterized by x-ray diffraction and FTIR. The catalyst testing reactor system is operational. Reactor product analysis system is nearing completion. Initiation of this system was delayed by the unavailability of a Valco valve which has just recently arrived. Set up of the in-situ FTIR cell for catalyst acidity studies has begun. In this report the results of several catalyst syntheses are reported along with characterization results. In particular, impregnation of vanadyl pyrophosphate with potassim nitrate dramatically reduced the number of surface hydroxyl groups. Such groups may be important in the non-selective, total oxidation of hydrocarbons. Also, preliminary experimental results on FTIR spectra of adsorbed pyridine are presented. It is shown that pyridine adsorbed on the catalyst surface can be easily observed by the diffuse reflectance IR technique. We plan to apply this technique to measurement of the acid site strength of surfaces modified with promoters.

  12. BX in-situ oil-shale project. Quarterly technical progress report, June 1, 1981-August 31, 1981

    SciTech Connect

    Dougan, P.M.

    1981-09-20

    June 1, 1981-August 31, 1981 was the third consecutive quarter of superheated steam injection at the BX In Situ Oil Shale Project. Injection was continuous except for the period of July 14th to August 1st when the injection was suspended during the drilling of core hole BX-37. During the quarter, 99,760 barrels of water as superheated steam were injected into Project injection wells at an average well head temperature of 752/sup 0/F and an average wellhead pressure of 1312 PSIG. During the same period, 135,469 barrels of fluid were produced from the Project production wells for a produced to injected fluid ratio of 1.36 to 1.0. Net oil production during the quarter was 38 barrels.

  13. Evaluation of using cyclocranes to support drilling and production of oil and gas in wetland areas. Fifth quarterly technical progress report, Third quarter, 1993

    SciTech Connect

    Eggington, W.J.

    1993-12-31

    The planned program falls under wetlands area research related to drilling, production, and transportation of oil and gas resources. Specifically the planned program addresses an evaluation of using cyclocraft to transport drill rigs, mud, pipes and other materials and equipment in a cost effective and environmentally safe manner to support oil and gas drilling and production operations in wetland areas. The cyclocraft is a proven hybrid aircraft that utilizes aerostatic and aerodynamic lift. This type of aircraft has considerable payload capacity, VTOL capability, high controllability, low operating cost, low downwash and high safety. The benefits of using a cyclocraft to transport drill rigs and materials over environmentally-sensitive surfaces would be significant. The cyclocraft has considerable cost and operational advantages over the helicopter. In 1992, Task 1, Environmental Considerations, and Task 2, Transport Requirements, were completed. In the first two quarters of 1993, Task 3, Parametric Analysis, Task 4, Preliminary Design, and Task 6, Ground Support, were completed. Individual reports containing results obtained from each of these tasks were submitted to DOE. In addition, through June 30, 1993, a Subscale Test Plan was prepared under Task 5, Subscale Tests, and work was initiated on Task 7, Environmental Impacts, Task 8, Development Plan, Task 9, Operating Costs, and Task 10, Technology Transfer.

  14. Wetland treatment of oil and gas well wastewaters. Quarterly technical report, November 25, 1992--February 24, 1993

    SciTech Connect

    Kadlec, R.H.; Srinivasan, K.R.

    1993-04-02

    During the first quarter of the above contract, all the elements of Task 1 were completed. The first quarterly report presented an overview of a wetland and its increasing use in industrial wastewater treatment. An idealized, reaction engineering description of wetlands was presented to demonstrate how the various processes that occur in a wetland can be modeled. Previous work on the use of wetlands to remove BOD, TSS, Phosphorus and Nitrogen was reviewed. Recent literature on the application of wetland technology to the treatment of petroleum-related wastewater was critically evaluated and an outline of the research plans for the first year was delineated. Further, our literature search (nominally completed under Task 1) unearthed more recent studies (some unpublished) and a summary was included in the second quarterly report. In the second quarterly report, results of our efforts on the construction of a laboratory-type wetland were also reported. Initial studies on the use of wetland amendments such as modified-clays and algae cells were presented and discussed. Adsorption of heavy metal ions, Cu{sup 2+} and Cr(VI) onto soils drawn from the laboratory-type wetland built as a part of this contract has been undertaken and these results are presented and discussed in this quarterly report. A number of studies on the design and preparation of modified-clays for the adsorption of Cr(VI) and {beta}-naphthoic acid (NA) has been carried out during this quarter and these are also described and discussed in this report. The choice of {beta}-naphthoic acid (NA) as an ionogenic organic compound was made on the basis of a recent personal communication to the Project Director that NA is a major contaminant in many oil and gas well wastewaters.

  15. Compatibility of refrigerants and lubricants with motor materials. Quarterly technical progress report, April 1, 1992--June 30, 1992

    SciTech Connect

    Doerr, R.; Kujak, S.

    1992-07-23

    During this last quarter, evaluations were complete on the motor materials after 500-hr exposures to refrigerants CFC-123, HFC-134a and HCFC-22 at 90{degrees}C. Materials were also evaluated after exposure to nitrogen at 127{degrees}C to determine effect of the thermal exposure. Other exposures were started during this quarter with refrigerants HCFC-124, HFC-125, HFC-143a, HFC-32 and HFC-152a. One 500 hr exposure is set up per week and one is analyzed the same week. This will enable Trane to complete the 500 hour exposures by the end of the year.

  16. Development and testing of a high efficiency advanced coal combustor Phase III industrial boiler retrofit. Quarterly technical progress report, July 1, 1995--September 30, 1995 No. 16

    SciTech Connect

    Borio, R.W.

    1995-12-15

    The objective of this project is to retrofit a burner, capable of firing microfine coal, to a standard gas/oil designed industrial boiler to assess the technical and economic viability of displacing premium fuels with microfine coal. This report documents the technical aspects of this project during the sixteenth quarter (July `95 through September `95) of the program. The overall program has consisted of five major tasks: (1) A review of current state-of-the-art coal firing system components. (2) Design and experimental testing of a prototype HEACC (High Efficiency Advanced Coal Combustor) burner. (3) Installation and testing of a prototype HEACC system in a commercial retrofit application. (4) Economics evaluation of the HEACC concept for retrofit applications. (5) Long term demonstration under commercial user demand conditions.

  17. Improvement of storage, handling, and transportability of fine coal. Quarterly technical progress report No. 4, October 1, 1994--December 31, 1994

    SciTech Connect

    1996-08-20

    The objectives of this project are to demonstrate that: The Mulled Coal process, which has been proven to work on a wide range of wet fine coals at bench scale, will work equally well on a continuous basis, producing consistent quality at a convincing rate of production in a commercial coal preparation plant. The wet product from a fine coal cleaning circuit can be converted to a solid fuel form for ease of handling and cost savings in storage and rail car transportation. A wet fine coal product thus converted to a solid fuel form, can be stored, shipped, and burned with conventional fuel handling, transportation, and combustion systems. During this fourth quarter of the contract period, activities were underway under Tasks 2 and 3. Sufficient characterization of the bench-scale testing and pilot-plant testing results enabled the design and procurement activities to move forward. On that basis, activities in the areas of design and procurement that had been initiated during the previous quarter were conducted and completed.

  18. Development and testing of industrial scale, coal fired combustion system, Phase 3. Sixteenth quarterly technical progress report, October 1--December 31, 1995

    SciTech Connect

    Zauderer, B.

    1996-01-03

    In the fourth quarter of calendar year 1995 the installation and checkout of the 20 MMBtu/hr combustor and auxiliary equipment in Philadelphia was completed. The task 5, Site Demonstration Testing, combustor-boiler tests on gas, oil, and coal were initiated. The task 5 effort involves testing the combustor over extended periods under conditions that fully simulate commercial operation and that meet the combustion and environmental specifications for this project. To meet this project objective within the current work scope requires up to 500 hours of testing. The focus of this testing will be on the component and environmental performance of combustor, boiler, coal preparation and feeding, and the stack gas equipment. The facility can be converted to a 500 kW power plant by the addition of a steam turbine, condenser, and cooling tower. However, this added effort is beyond the current work scope and its implementation will depend on recovering the added costs by placing the steam production from the boiler to beneficial use. During the present quarterly reporting period, all the components needed to implement the initial 100 hours of testing under task 5 were installed at the test site, and checkout of this equipment was performed. Since the present installation contained substantial improvements and simplifications to all sub-systems that had been used in the Williamsport facility, each component and sub-system had to be tested individually.

  19. Energy programs. Quarterly report, January-March 1980

    SciTech Connect

    Not Available

    1980-01-01

    The Johns Hopkins University Applied Physics Laboratory, is engaged in developing energy resource, utilization concepts, and monitoring and storage methods. This Quarterly Report summarizes the work on the various tasks as of 31 March 1980. The Energy Quarterly Report is divided into four sections. The first, Geothermal Energy Development Planning and Technical Assistance, contains reports on the progress of geothermal-related tasks on which effort was concentrated during the quarter. The second section, Operational Research, Hydroelectric Power Development, contains reports on small-scale hydroelectric investigations in the southeastern states. The third section, Seismotectonic Investigation, reports on a neotectonic investigation in Connecticut. The fourth section, Energy Conversion and Storage Techniques, contains two articles, the first on OTEC core unit testing supported by the Department of Energy/Division of Central Solar Technology (DOE/CST), and the second on an analysis of the Community Annual Storage Energy System at the US Naval Air Station, Norfolk, Va.

  20. Preliminary design and assessment of a 50,000-BPD coal-to-methanol-to-gasoline plant. Quarterly technical progress report, 1 April 1982-30 June 1982

    SciTech Connect

    Not Available

    1982-01-01

    The technical efforts associated with the Statement of Work for the preliminary design and assessment of a 50,000-BPD Coal-to-Methanol-to-Gasoline Plant continued at an accelerated rate. Physical accomplishment increased from 39.6% (March 1982) to 69.1% (June 1982). All contracts were in place prior to the commencement of this quarter and the only significant contractual action bearing on Statement of Work requirements was DOE's approval of a Grace request for modification of the Dames and Moore Subcontract to recognize certain additions and/or expansions resulting from the scoping meeting process. The narrative of this report discusses progress of work associated with technical activities for both the 50,000-BPD and 12,500-BPD plants. Significant progress in the process and mechanical design was achieved following the receipt of all design packages and data from vendors for incorporation in process design documentation. This information enabled the preparation of all process and utility flow diagrams, plot plans, evaluations, and associated direct capital cost estimates for the 50,000-BPD plant. The basic design of all process units comprising the Gasoline Plant was completed, and engineering efforts directed toward supplying inputs for the development of capital and operating cost estimates and economic assessments. Development of engineering documentation for the 12,500-BPD plant was initiated and progressed significantly during the quarter. Development of capital and operating cost estimates for the smaller plant was also active.

  1. Superior catalysts for selective catalytic reduction of nitric oxide. Quarterly technical progress report, January 1, 1995--March 31, 1995

    SciTech Connect

    Li, W.B.; Yang, R.T.

    1995-12-01

    During this quarter, progress was made on the following tasks: TPD techniques were employed to study the reaction mechanism of the selective catalytic reduction of nitrogen oxide with ammonia over iron oxide pillared clay catalyst; and a sulfur dioxide resistant iron oxide/titanium oxide catalyst was developed.

  2. Support of enhanced oil recovery to independent producers in Texas. Quarterly technical progress report, July 1, 1995--September 30, 1995

    SciTech Connect

    Fotouh, K.H.

    1995-09-30

    The main objective of this project is to support independent oil producers in Texas and to improve the productivity of marginal wells utilizing enhanced oil recovery techniques. The main task carried out this quarter was the generation of an electronic data base.

  3. CO{sub 2} Huff-n-Puff process in a light oil shallow shelf carbonate reservoir. Quarterly technical progress report, 3rd quarter, 1994

    SciTech Connect

    Wehner, S.; Smith, V.; Cole, R.; Brugman, B.; Vogt, J.

    1994-10-18

    The principal objective of the Central Vacuum Unit (CVU) CO{sub 2} Huff-n-Puff (H-n-P) project is to determine the feasibility and practicality of the technology in a waterflooded shallow shelf carbonate environment. The results of parametric simulation of the CO{sub 2} H-n-P process, coupled with the CVU reservoir characterization components will determine if this process is technically and economically feasible for field implementation. The technology transfer objective of the project is to disseminate the knowledge gained through an innovative plan in support of the Department of Energy`s (DOE) objective of increasing domestic oil production and deferring the abandonment of shallow shelf carbonate (SSC) reservoirs. Texaco Exploration and Production Inc`s. (TEPI) long-term plans are to implement a full-scale miscible CO{sub 2} project in the CVU. However, the current market precludes acceleration of such a capital intensive project. The DOE partnership provides some relief to the associated R and D risks, allowing TEPI to evaluate a proven Gulf-coast sandstone technology in a waterflooded carbonate environment. Technical progress is described on the following studies: Porosity and permeability relationships; Initial water saturation and oil-water contact; Geostatistical realization; and Parametric simulation.

  4. Investigation of mineral transformations and ash deposition during staged combustion. Quarterly technical progress report, January 1, 1996--March 31, 1996

    SciTech Connect

    Harb, J.N.

    1996-05-01

    Progress during the tenth quarter of a three-year study of ash formation and deposition was made in several areas. One of the key contributions this quarter was the development of an algorithm to distinguish between ash particles that are associated with char particles (included) and ash particles which are excluded. This algorithm was used to determine the extent to which pyrite transformations are influenced by whether the pyrite grains are included or excluded. The results indicate that pyrite oxidation is slower for included pyrite grains. Replicate experiments were also performed for the Pittsburgh No. 8 coal (washed) under both staged and conventional conditions. An objective of these experiments was to validate the effect of staged combustion on the size distribution of ash particles as reported for the previous quarter. Analysis of the new samples and repeat analyses of previous samples showed no significant difference in the ash particle size for samples collected at stoichiometric ratios of 0.75 (before the stage) and 1.04. The number of points in the new analyses was considerably higher than in previous analyses, resulting in greater confidence. The similarity in the ash composition for samples collected under staged and conventional conditions was also verified this quarter with replicate samples and analyses. The net result is that staged combustion does not appear to have a significant impact on either ash size or composition for the Pittsburgh No. 8 coal. Finally, numerical simulations of the temperature distribution in the laboratory combustor were performed and evaluated. Also, a paper documenting the classification algorithm developed last quarter was presented at the March ACS meeting in New Orleans and published in the ACS Division of Fuel Chemistry Preprints.

  5. Short-term energy outlook. Quarterly projections, 2nd quarter 1994

    SciTech Connect

    Not Available

    1994-05-01

    The Energy Information Administration (EIA) prepares quarterly, short-term energy supply, demand, and price projections for publication in February, May, August, and November in the Short-Term Energy Outlook (Outlook). An annual supplement analyzes the performance of previous forecasts, compares recent cases with those of other forecasting services, and discusses current topics related to the short-term energy markets. The forecast period for this issue of the Outlook extends from the second quarter of 1994 through the fourth quarter of 1995. Values for the first quarter of 1994, however, are preliminary EIA estimates (for example, some monthly values for petroleum supply and disposition are derived in part from weekly data reported in the Weekly Petroleum Status Report) or are calculated from model simulations using the latest exogenous information available. The historical energy data, compiled into the second quarter 1994 version of the Short-Term Integrated Forecasting System (STIFS) database, are mostly EIA data regularly published in the Monthly Energy Review, Petroleum Supply Monthly, and other EIA publications. Minor discrepancies between the data in these publications and the historical data in this Outlook are due to independent rounding. The STIFS database is archived quarterly and is available from the National Technical Information Service. The cases are produced using the STIFS. The STIFS model is driven principally by three sets of assumptions or inputs: estimates of key macroeconomic variables, world oil price assumptions, and assumptions about the severity of weather. Macroeconomic estimates are produced by DRI/McGraw-Hill but are adjusted by EIA to reflect EIA assumptions about the world price of crude oil, energy product prices, and other assumptions which may affect the macroeconomic outlook. The EIA model is available on computer tape from the National Technical Information Service.

  6. CO{sub 2} Hugg-n-Puff process in a light oil shallow shelf carbonate reservoir. Quarterly technical progress report, 2nd quarter 1996

    SciTech Connect

    1996-07-25

    The principal objective of the Central Vacuum Unit (CVU) CO{sub 2} Huff-n-Puff (H-n-P) project is to determine the feasibility and practicality of the technology in a waterflooded shallow shelf carbonate environment. The results of parametric simulation of the CO{sub 2} H-n-P process, coupled with the CVU reservoir characterization components will determine if this process is technically and economically feasible for field implementation. The technology transfer objective of the project is to disseminate the knowledge gained through an innovative plan in support of the Department of Energy`s (DOE) objective of increasing domestic oil production and deferring the abandonment of shallow shelf carbonate (SSC) reservoirs. Tasks associated with this objective are carried out in what is considered a timely effort for near-term goals.

  7. The development of an integrated multistage fluid bed retorting process. Quarterly technical report, January 1, 1993--March 31, 1993

    SciTech Connect

    Carter, S.; Stehn, J.; Vego, A.

    1993-04-01

    This report summarizes the progress made on the development of an integrated multistage fluidized bed retorting process (KENTORT 11) during the period of January 1, 1993 through March 31, 1993 under Cooperative Agreement No. DE-FC21-90MC27286 with the Morgantown Energy Technology Center, US Department of Energy. The KENTORT II process includes integral fluidized bed zones for pyrolysis, gasification, and combustion of oil shale. The purpose of this program is to design and test the KENTORT II process at the 50-lb/hr scale. The major activity for this quarter was to install various components of the process and provide utility support including air, water, electrical power, and computerized instrumentation. Following the completion of construction activities which is scheduled for next quarter, cold-flow testing and heat-up procedures will be performed.

  8. Characterization and supply of coal based fuels. Quarterly technical progress report, February 1, 1987--April 30, 1987

    SciTech Connect

    Not Available

    1987-07-01

    Contract objectives are as follows: develop fuel specifications to serve combustor requirements; select coals having appropriate compositional and quality characteristics as well as an economically attractive reserve base; provide quality assurance for both the parent coals and the fuel forms; and deliver premium coal-based fuels to combustor developers as needed for their contract work. During the second quarter of this contract effort, the primary activities were involved with: continuation of development of fuel requirements (i.e., specifications, quantities, schedule); acquisition and bench-scale characterization of candidate coal samples; selection of coal water slurry fuel manufacturer; procurement of parent coal for fuel production; deep cleaning by froth flotation of parent coal; production of solid fuel (i.e., size reduction of deep cleaned parent coal) and delivery to combustors/experimenters; production of slurry fuel and delivery to combustors/experimenters; and completion of Final Version of First Quarterly Report.

  9. Advanced alternate planar geometry solid oxide fuel cells. Interim quarterly technical progress report, November 1, 1988--January 31, 1989

    SciTech Connect

    Prouse, D.; Elangovan, S.; Khandkar, A.; Donelson, R.; Marianowski, L.

    1989-12-31

    During this quarter, progress was made at Ceramatec in seal development and conductivity measurements of YIG compositions. A creep test was completed on the porous/dense/porous triilayer. IGT provided a discussion on possible interconnect materials. The following tasks are reported on: cell design analysis, program liaison and test facility preparation, cell component fabrication/development, out-of-cell tests. 9 figs, 2 tabs.

  10. Advanced physical coal cleaning to comply with potential air toxic regulations. [Quarterly] technical report, September 1--November 30, 1994

    SciTech Connect

    Honaker, R.Q.; Paul, B.C.; Wang, D.

    1994-12-31

    This research project will investigate the use of advanced fine coal cleaning technologies for cleaning PCB feed as a compliance strategy. Trace elements considered in this project will include mercury, selenium, cadmium, and chlorine. Work in the first quarter has focused on trace element analysis procedures and sample acquisition. Several experts in the field of trace element analysis of coal have been consulted and these procedures are presently being evaluated.

  11. Magnetic relaxation - coal swelling, extraction, pore size. Quarterly technical progress report, April 1, 1994--June 31, 1994

    SciTech Connect

    Doetschman, D.C.

    1994-08-01

    Work this quarter involved a CW EPR examination of the density separated fractions of the Lewiston-Stockton Argonne Coal and the initiation of EPR studies to probe molecular motion in coal pores. Eighteen densities between 1.24 g/cm{sup 3} and 1.56 g/cm{sup 3} were separated and combined into seven density ranges. Radicals with a narrow EPR line appear only in the samples with densities above 1.48 g/cm{sup 3}.

  12. Effects of surface chemistry on the porous structure of coal. Quarterly technical progress report, April 1996--June 1996

    SciTech Connect

    Anderson, S.A.; Radovic, L.R.; Hatcher, P.G.

    1996-11-01

    Objective is to use {sup 129}Xe NMR to study the microporous structure of coals. During this quarter, we have: performed a presaturation experiment on Wyodak subbituminous coal, monitored the progress of Xe adsorption in an anthracite, focusing on the changes observed in the external-surface adsorbed gas signal, used an echo sequence to obtain {sup 129}Xe NMR spectra of Blind Canyon hvAb coal, and improved and repeated the successive oxygen adsorption and desorption experiment on a microporous carbon.

  13. Investigation of mineral transformations and ash deposition during staged combustion. Quarterly technical progress report, October 1, 1995--December 31, 1995

    SciTech Connect

    Harb, J.N.

    1996-02-07

    Progress during the ninth quarter of a three-year study of ash formation and deposition was made in several areas. One of the key contributions this quarter was the development of an enhanced method for classification of CCSEM data. This classification algorithm permits grouping and comparison of particles previously labeled as ``unclassifiable.`` A second analytical advancement, also made this quarter, provides more detailed information on the distribution of minerals in the coal and the potential for coalescence. This new multiple analysis technique is also applicable to ash and will permit identification of heterogeneous ash particles. Additional analyses of ash samples were also performed and it was found that the firing of Pittsburgh {number_sign}8 under staged combustion conditions yields an ash with a significantly larger particle size distribution than that obtained under conventional firing conditions, but without a significant change in composition. the size difference was noted previously, but the new classification algorithm allowed a detailed comparison of all composition groups, including unclassifiable particles, in the ashes. A mechanistic explanation for this behavior has been developed and is provided in the report. Finally, a paper documenting the new classification algorithm has been prepared and is scheduled for presentation at the March ACS meeting in New Orleans.

  14. Ink jet printing of silver metallization for photovoltaics. Quarterly technical report, October 1, 1984-December 30, 1984

    SciTech Connect

    Vest, R.W.

    1985-01-25

    During this quarter, significant progess was made in the continuing development of the ink jet printing system for thick film circuits. The unit being used in this research is a prototype ink jet printer developed on a contract with the Naval Avionics Center. One of the first tasks completed early in the quarter was the complete documentation of this ink jet printing system as it existed. It was determined that this was an essential step in deciding what modifications were needed to the system and how these modifications would be implemented. After this initial step was completed, design modification studies were started for electronic, mechanical, and programming aspects of the system. These studies were completed at the end of the second month. The areas needing improvement were discussed and applicable changes decided upon. Some of these improvements were completed during this quarter and others have only been started. It should be noted that, although the general areas needing improvement have been identified and some changes decided upon, the exact details of how other changes will be implemented have not yet been decided. During the next months, these details will be discussed further and the modifications put in place accordingly.

  15. Short-term energy outlook. Quarterly projections, Third quarter 1995

    SciTech Connect

    1995-08-02

    The Energy Information Administration (EIA) prepares quarterly, short-term energy supply, demand, and price projections for publication in February, May, August, and November in the Short-Term Energy Outlook (Outlook). An annual supplement analyzes the performance of previous forecasts, compares recent projections with those of other forecasting services, and discusses current topics related to the short-term energy markets. The forecast period for this issue of the Outlook extends from the third quarter of 1995 through the fourth quarter of 1996. Values for the second quarter of 1995, however, are preliminary EIA estimates.

  16. Government Information Quarterly. Volume 7, no. 2: National Aeronautics and Space Administration Scientific and Technical Information Programs. Special issue

    NASA Technical Reports Server (NTRS)

    Hernon, Peter (Editor); Mcclure, Charles R. (Editor); Pinelli, Thomas E. (Editor)

    1990-01-01

    NASA scientific and technical information (STI) programs are discussed. Topics include management of information in a research and development agency, the new space and Earth science information systems at NASA's archive, scientific and technical information management, and technology transfer of NASA aerospace technology to other industries.

  17. Geothermal direct-heat utilization assistance. Quarterly project progress report, July 1995--September 1995

    SciTech Connect

    Lienau, P.

    1995-12-01

    The report summarizes geothermal technical assistance, R&D and technology transfer activities of the Geo-Heat Center at Oregon Institute of Technology for the fourth quarter of FY-95. It describes 80 contacts with parties during this period related to technical assistance with geothermal direct heat projects. Areas dealt with include geothermal heat pumps, space heating, greenhouses, aquaculture, equipment and resources. Research activities are summarized on low-temperature resource assessment, geothermal energy cost evaluation and marketing strategy for geothermal district heating. Outreach activities include the publication of a geothermal direct use Bulletin, dissemination of information, geothermal library, technical papers and seminars, and progress monitor reports on geothermal resources and utilization.

  18. Development of vanadium-phosphate catalysts for methanol production by selective oxidation of methane. Quarterly technical progress report 3, April--June 1993

    SciTech Connect

    McCormick, R.L.; Jha, M.C.; Streuber, R.D.

    1993-08-20

    This document is the third quarterly technical progress report under Contract No. AC22-92PC92110, ``Development of Vanadium-Phosphate Catalysts for Methanol Production by Selective Oxidation of Methane.`` During this quarter, we have continued to develop methods for catalyst activation by investigating activation in wet gas environments. This procedure leads to the formation of highly crystalline (VO){sub 2}P{sub 2}O{sub 7}, while activation under identical conditions, but with no moisture, leads to a poorly crystalline sample. Published data indicate that the highly crystalline form is representative of commercial butane oxidation catalysts. The main focus of our work during this quarter has been in the area of catalyst testing in the microreactor system. In order to confirm that our microreactor system was providing reliable data, we tested a V{sub 2}O{sub 5}/SiO{sub 2} catalyst at atmospheric pressure and temperatures from 500 to 600{degree}C using 90 to 95 percent CH{sub 4}/O{sub 2}. Several studies of methane oxidation using this catalyst have been published with reasonably good agreement between different research groups. We were not able to reproduce the literature data using steel reactors. However, when the steel reactor was lined with quartz and the postcatalyst reactor volume was minimized by packing with quartz chips, we obtained results which agree closely with those previously published. Using the same quartz reactor and test conditions, we also tested a highly crystalline (wet activated) VPO catalyst.

  19. Engineering development of advanced physical fine coal cleaning technologies: Froth flotation. Quarterly technical progress report No. 11, April 1, 1991--June 30, 1991

    SciTech Connect

    Not Available

    1991-12-31

    This document a quarterly report prepared in accordance with the project reporting requirements covering the period from July 1, 1992 to September 30, 1992. This report provides a summary of the technical work undertaken during this period, highlighting the major results. A brief description of the work done prior to this quarter is provided in this report under the task headings. The overall project scope of the engineering development project is to conceptually develop a commercial flowsheet to maximize pyritic sulfur reduction at practical energy recovery values. This is being accomplished by utilizing the basic research data on the surface properties of coal, mineral matter and pyrite obtained from the Coal Surface Control for Advanced Fine Coal Flotation Project, to develop this conceptual flowsheet. The conceptual flowsheet must be examined to identify critical areas that need additional design data. This data will then be developed using batch and semi-continuous bench scale testing. In addition to actual bench scale testing, other unit operations from other industries processing fine material will be reviewed for potential application and incorporated into the design if appropriate. The conceptual flowsheet will be revised based on the results of the bench scale testing and areas will be identified that need further larger scale design data verification, to prove out the design.

  20. Increasing heavy oil reserves in the Wilmington oil field through advanced reservoir characterization and thermal production technologies. Quarterly technical progress report, March 30, 1995--June 30, 1995

    SciTech Connect

    Clarke, D.; Ershaghi, I.; Davies, D.; Phillips, C.; Mondragon, J.

    1995-07-28

    This is the first quarterly technical progress report for the project. Although the contract was awarded on March 30, 1995 and Pre-Award Approval was given on January 26, 1995, the partners of this project initiated work on October 1, 1994. As such, this progress report summarizes the work performed from project inception. The production and injection data, reservoir engineering data, and digitized and normalized log data were all completed sufficiently by the end of the quarter to start work on the basic reservoir engineering and geologic stochastic models. Basic reservoir engineering analysis began June 1 and will continue to March, 1996. Design work for the 5 observation/core holes, oil finger printing of the cored oil sands, and tracers surveys began in January, 1995. The wells will be drilled from July--August, 1995 and tracer injection work is projected to start in October, 1995. A preliminary deterministic 3-D geologic model was completed in June which is sufficient to start work on the stochastic 3-D geologic model. The four proposed horizontal wells (two injectors and two producers) have been designed, equipment has been ordered, and the wells will be drilled from mid-August through September. Four existing steam injection wells were converted to hot water injection in March, 1995. Initial rates were kept low to minimize operational problems. Injection rates will be increased significantly in July.

  1. Combustion characterization of beneficiated coal-based fuels. Quarterly report No. 7, October 1990--December 1990

    SciTech Connect

    Hargrove, M.J.; Chow, O.K.; Nsakala, N.Y.

    1991-02-01

    During the fourth quarter of 1990, the following technical progress was made: (1) Calculated the kinetic characteristics of chars from the combustion of microbubble flotation beneficiated products; (2) continued drop tube combustion tests of the spherical oil agglomeration beneficiated products; (3) analyzed the data from three (MIT) pilot-scale combustion tests of the Upper Freeport feed coal; and (4) continued analyses of the data from the CE pilot-scale tests of nine fuels.

  2. Development of molten carbonate fuel cell power plant. Quarterly technical progress report, February 1-April 30, 1980

    SciTech Connect

    Peterson, J. R.

    1980-01-01

    Work has been initiated during this first quarter under all four program tasks and by all major participants as described. Task 1.0 activity (establish power plant reference design) concentrated upon definition of user requirements and establishment of power plant subsystem alternatives and characteristics. Task 2.0 work (stack and cell design development and verification) was initiated with a heavy emphasis upon test facilities preparation. A total of 27 laboratory cells were operated during this reporting period and a total of nine cells continued on test at the end of the quarter. Investigation of alternative anode and cathode materials proceeded; a dual-porosity anode was fabricated and tested. Over 10,000 endurance hours on a state-of-the-art cell carried-over from a previous program has been achieved and 1500 hours endurance has been obtained with sheet metal cells. Results presented for electrolyte structure development include comparative data for spray-dried and modified aqueous slurry process powders. Shake-down tests with a rotating disc electrode apparatus for fundamental measurements are described. Concept designs for both prototype and subscale stacks have been identified. Task 3.0 effort (development capability for full-scale stack tests) included preparation of an overall test plan to commercialization for molten carbonate fuel cells and of a functional specification for the tenth-scale stack test facility; drafts of both documents were completed for internal review. Cost-effective manufacturing assessment of available designs and processes was initiated. Task 4.0 work (develop capabilities for operation of stacks on coal-derived gas) included gathering of available contaminants concentration and effects information and preparation of initial projections of contaminant ranges and concentrations. Accomplishments to date and activities planned for the next quarter are described.

  3. Upgrading mild gasification liquids to produce electrode binder pitch. [Quarterly] technical report, December 1, 1993--February 28, 1994

    SciTech Connect

    Knight, R.A.

    1994-06-01

    The objective of this program is to investigate the production of electrode binder pitch, valued at $250--$300/ton, from mild gasification liquids. The IGT MILDGAS process pyrolyzes coal at 1000{degrees}--1500{degrees}F and, with Illinois coal, the 750{degrees}F+ distillation residue (crude pitch) comprises 40--70% of the MILDGAS liquids, representing up to 20 wt% of maf feed coal. The largest market for pitch made from coal liquids is the aluminum industry, which uses it to make carbon anodes for electrolytic furnaces. In this project, crude MILDGAS pitch is being modified by a flash thermocracking technique to achieve specifications typical of a binder pitch. Last year, a pitch thermocracking unit was constructed for operation at 1200{degrees}--1600{degrees}F. Reactor design features and process conditions are being examined to optimize the properties of the finished pitch. In the current year, improvements to the thermocracker are being made for better gas and pitch flow control, continuous electronic monitoring of feed rate and pressures, and improvements to allow longer tests. Tests are being conducted under both inert and reducing gases. During the current quarter, equipment modifications, calibrations, and shakedown were completed, and thermocracking tests were resumed. One test was completed at 1600{degrees}F in N{sub 2} with a pitch rate of 11 g/min. Data from this and following tests will be presented in the next quarterly report. During the next quarter, thermocracking tests will be completed and selected products (pitch and/or pitch coke) will be submitted to an aluminum company testing lab for production and evaluation of test electrodes.

  4. POC-scale testing of an advanced fine coal dewatering equipment/technique. Quarterly technical progress report, April 1996--June 1996

    SciTech Connect

    Tao, D.; Groppo, J.G.; Parekh, B.K.

    1996-07-31

    Froth flotation technique is an effective and efficient process for recovering of ultra-fine (minus 74 {mu}m) clean coal. Economical dewatering of an ultra-fine clean coal product to a 20 percent level moisture will be an important step in successful implementation of the advanced cleaning processes. This project is a step in the Department of Energy`s program to show that ultra-clean coal could be effectively dewatered to 20 percent or lower moisture using either conventional or advanced dewatering techniques. The cost sharing contract effort is for 36 months beginning September 30, 1994. This report discusses technical progress made during the quarter from April 1 - June 30, 1996.

  5. POC-scale testing of an advanced fine coal dewatering equipment/technique. Quarterly technical progress report, No. 4, July 1995--September 1995

    SciTech Connect

    Groppo, J.G.; Parekh, B.K.

    1995-11-06

    Froth flotation technique is an effective and efficient process for recovering of ultra-fine (minus 74 {mu}m) clean coal. Economical dewatering of an ultra-fine clean coal product to a 20 percent level moisture will be an important step in successful implementation of the advanced cleaning processes. This project is a step in the Department of Energy`s program to show that ultra-clean coal could be effectively dewatered to 20 percent or lower moisture using either conventional or advanced dewatering techniques. The cost-sharing contract effort is for 36 months beginning September 30, 1994. This report discusses technical progress made during the quarter from July 1 - September 29, 1995.

  6. Bench-scale testing of on-line control of column flotation using a novel analyzer. Second quarterly technical progress report, January 1, 1993--March 31, 1993

    SciTech Connect

    Not Available

    1993-04-16

    This document contains the second quarterly technical progress report for PTI`s Bench-Scale Testing Project of a circuit integrating PTI`s KEN-FLOTE{trademark} Column Flotation Technology and PTI`s On-Line Quality Monitor and Control System. The twelve-month project involves installation and testing of a 200--300 lb/hr. bench-scale testing circuit at PETC`s Coal Preparation Process Research Facility (CPPRF) for two bituminous coals (Upper Freeport and Pittsburgh No. 8 Seam Raw Coals). The project schedule timeline by task series for the twelve month project, as it was laid out in the initial Project Work Plan. At the present time, all tasks are progressing according to schedule with the exception of the Task 800 Circuit Testing and Sample Prep and Task 1000 Circuit Decommissioning, which have slipped approximately five weeks due to delays incurred within in the project.

  7. POC-scale testing of an advanced fine coal dewatering equipment/technique. Quarterly technical progress report 2, January 1995--March 1995

    SciTech Connect

    Groppo, J.G.; Parekh, B.K.

    1995-05-05

    Froth flotation technique is an effective and efficient process for recovering of ultra-fine (minus 74 {mu}m) clean coal. Economical dewatering of an ultra-fine clean coal product to a 20 percent level moisture will be an important step in successful implementation of the advanced cleaning processes. This project is a step in the Department of Energy`s program to show that ultra-clean coal could be effectively dewatered to 20 percent or lower moisture using either conventional or advanced dewatering techniques. The cost-sharing contract effort is for 36 months beginning September 30, 1994. This report discusses technical progress made during the quarter from January 1 to March 31, 1995.

  8. Bioconversion of coal derived synthesis gas to liquid fuels. Quarterly technical progress report, October 1, 1994--December 27, 1994

    SciTech Connect

    Jain, M.K.; Worden, R.M.; Grethlein, A.

    1995-01-16

    The overall objective of the project is to develop an integrated two-stage fermentation process for conversion of coal-derived synthesis gas to a mixture of alcohols. This is achieved in two steps. In the first step, Butyribacterium methylotrophicum converts carbon monoxide (CO) to butyric and acetic acids. Subsequent fermentation of the acids by Clostridium acetobutylicum leads to the production of butanol and ethanol. The tasks for this quarter were: (1) Development/isolation of superior strains for fermentation of syngas; (2) Evaluation of bioreactor configuration for improved mass transfer of syngas, specifically gas lift; (3) Pervaporation for recovery of solvents; (4) Write and submit final report.

  9. Liquefaction of coals using ultra-fine particle, unsupported catalysts: In situ generation by rapid expansion of supercritical fluid solutions. Quarterly technical progress report, January 1, 1991--March 31, 1991

    SciTech Connect

    Not Available

    1991-09-01

    The program objective is to generate ultra-fine catalyst particles (20 to 400 {Angstrom} in size) and quantify their potential for improving coal dissolution in the solubilization stage of two-stage catalytic-catalytic liquefaction systems. In the first quarterly report for this program the concept behind our approach was detailed, the structure of the program was presented, key technical issues were identified, preliminary designs were outlined, and technical progress was discussed. All progress made during the second quarter of this program related to experiment design of the proposed supercritical expansion technique for generating ultra-fine, iron compound, catalyst particles. This second quarterly report, therefore, presents descriptions of the final designs for most system components; diagnostic approaches and designs for determining particles size and size distributions, and the composition of the pre-expansion supercritical solution; and the overall technique progress made during this reporting period. 6 refs., 15 figs., 1 tab.

  10. AFRRI report third - fourth quarters 1996

    SciTech Connect

    1996-12-31

    Table contents: Effect of chloral hydrate on in vivo KCl-induced striatal dopamine release in the rat. Effect of ionizing radiation on in vivo striatal release of dopamine in the rat. Transient and persistent experimental infection of nonhuman primates with Helicobacter pylori: Implications for human disease. Indomethacin attenuation of radiation-induced hyperthermia does not modify radiation-induced motor hypoactivity. Behavioral toxicity and radioprotective efficacy of WR-15l327 in combination with adenosine receptor antagonists. Chromatographic and mass spectral analysis of the radioprotector and chemoprotector S-3-(3 -methylaminopropylamino) propanethiol (WR-15t326) and its symmetrical disulfide (WR-25595501). Mechloretharnine-induced enhancement of radiation sensitivity of guanine.

  11. Environmental Biosciences Program Fourth Quarter Report

    SciTech Connect

    Lawrence C. Mohr, M.D.

    2005-06-30

    In May 2002, the United States Department of Energy (DOE) signed Assistance Instrument Number DE-FC09-02CH11109 with the Medical University of South Carolina (MUSC) to support the Environmental Biosciences Program (EBP). This funding instrument replaces DOE Assistance Instrument Number DE-FC02-98CH10902. EBP is an integrated, multidisciplinary scientific research program, employing a range of research initiatives to identify, study and resolve environmental health risks. These initiatives are consistent with the MUSC role as a comprehensive state-supported health sciences institution and with the nation s need for new and better approaches to the solution of a complex and expansive array of environment-related health problems. The intrinsic capabilities of a comprehensive health sciences institution enable MUSC to be a national resource for the scientific investigation of environmental health issues. EBPs success as a nationally prominent research program is due, in part, to its ability to task-organize scientific expertise from multiple disciplines in addressing these complex problems. Current research projects have focused EBP talent and resources on providing the scientific basis for risk-based standards, risk-based decision making and the accelerated clean-up of widespread environmental hazards. These hazards include trichloroethylene (TCE), polychlorinated biphenyles (PCBs), and low-dose ionizing radiation. A project is also being conducted in the use of geographical information system technology to analyze population health risks related to environmental hazards as a tool for risk-based decision-making. Questions, comments or requests for further information concerning the activities under this cooperative agreement can be forwarded to Dr. Lawrence C. Mohr in the EBP office of the Medical University of South Carolina at (843) 792-1532.

  12. Environmental Biosciences Program Fourth Quarter Report

    SciTech Connect

    Lawrence C. Mohr, M.D.

    2004-06-30

    In May 2002, the United States Department of Energy (DOE) signed Assistance Instrument Number DE-FC09-02CH11109 with the Medical University of South Carolina (MUSC) to support the Environmental Biosciences Program (EBP). This funding instrument replaces DOE Assistance Instrument Number DE-FC02-98CH10902. EBP is an integrated, multidisciplinary scientific research program, employing a range of research initiatives to identify, study and resolve environmental health risks. These initiatives are consistent with the MUSC role as a comprehensive state-supported health sciences institution and with the nation's need for new and better approaches to the solution of a complex and expansive array of environment-related health problems. The intrinsic capabilities of a comprehensive health sciences institution enable MUSC to be a national resource for the scientific investigation of environmental health issues. EBPs success as a nationally prominent research program is due, in part, to its ability to task-organize scientific expertise from multiple disciplines in addressing these complex problems Current research projects have focused EBP talent and resources on providing the scientific basis for risk-based standards, risk-based decision making and the accelerated clean-up of widespread environmental hazards. These hazards include trichloroethylene (TCE), polychlorinated biphenyls (PCBs), asbestos and low-dose ionizing radiation. A project is also being conducted in the use of geographical information system technology to analyze population health risks related to environmental hazards as a tool for risk-based decision-making.

  13. AFRRI Reports, Third-Fourth Quarters

    DTIC Science & Technology

    1998-02-01

    Aldrich Chemical Co., Inc. Milwau- lived free radical with a spin trap, usually a nitrone kee , WI. Randomly labeled 3C-TCE (,-50% 𔃼 C or nitroso... dak XAR film. Both positive and negative control reactions or 0.5 .-g splenic total RNA, 50 mM Tris-HCI (pH 8.3), 3 mM showed the appropriate response...Biochim. Biophys. Acta 1133, J. Leukocyte Biol. 37, 395-406. 275-285. 53. Tosk, J., Lau , B. H. S., Myers, R. C., and Torrey, R. R. (1989) 23. Belloc

  14. Environmental Biosciences Program Fourth Quarter Report

    SciTech Connect

    Lawrence C. Mohr, M.d.

    2003-04-30

    In May 2002, the United States Department of Energy (DOE) signed Assistance Instrument Number DE-FC09-02CH11109 with the Medical University of South Carolina (MUSC) to support the Environmental Biosciences Program (EBP). This funding instrument replaces DOE Assistance Instrument Number DE-FC02-98CH10902. EBP is an integrated, multidisciplinary scientific program, employing a range of research initiatives to identify, study and resolve environmental health risk issues. These initiatives are consistent with the Medical University's role as a comprehensive state-supported health sciences institution and the nation's need for new and better approaches to the solution of a complex and expansive array of environment-related health problems. The intrinsic capabilities of a comprehensive health sciences institution enable the Medical University to be a national resource for the scientific investigation of environmental health issues. EBP's success in convening worldwide scientific expertise is due in part to the inherent credibility the Medical University brings to the process of addressing these complex issues.

  15. Bench-scale testing of on-line control of column flotation using a novel analyzer. Third quarterly technical progress report, April 1, 1993--June 30, 1993

    SciTech Connect

    Not Available

    1993-08-24

    This document contains the third quarterly technical progress report for PTI`s Bench-Scale Testing Project of a circuit integrating PTI`s KEN-FLOTETM Column Flotation Technology and PTI`s On-Line Quality Monitor and Control System. The twelve-month project involves installation and testing of a 200--300 lb/hr. bench-scale flotation circuit at PETC`s Coal Preparation Process Research Facility (CPPRF) for two bituminous coals (Upper Freeport and Pittsburgh No. 8 Seam Raw Coals). Figure 1 contains the project plan, as well as the approach to completing the major tasks within the twelve-month project schedule. The project is broken down into three phases, which include: Phase I -- Preparation: The preparation phase was performed principally at PTI`s Calumet offices from October through December, 1992. It involved building of the equipment and circuitry, as well as some preliminary design and equipment testing; Phase II -- ET Circuit Installation and Testing: This installation and testing phase of the project was performed at PETC`s CPPRF from January through June, 1993, and was the major focus of the project. It involved testing of the continuous 200--300 lb/hr. circuit; and Phase III -- Project Finalization: The project finalization phase is occurring from July through September, 1993, at PTI`s Calumet offices and involves finalizing analytical work and data evaluation, as well as final project reporting. This Third Quarterly Technical Progress Report principally summarizes the results from the benchscale testing with the second coal (Pittsburgh No. 8 Seam Coal), which occurred in April through June, 1993. It also contains preliminary economic evaluations that will go into the Final Report, as well as the plan for the final reporting task.

  16. Development and testing of a high efficiency advanced coal combustor phase III industrial boiler retrofit. Quarterly technical progress report No. 9, 1 October 1993--31 December 1993

    SciTech Connect

    Jennings, P.; Borio, R.; McGowan, J.G.

    1994-03-01

    This report documents the technical aspects of this project during the ninth quarter of the program. During this quarter, the natural gas baseline testing at the Penn State demonstration boiler was completed, results were analyzed and are presented here. The burner operates in a stable manner over an 8/1 turndown, however due to baghouse temperature limitations (300{degrees}F for acid dewpoint), the burner is not operated for long periods of time below 75% load. Boiler efficiency averaged 83.1% at the 100 percent load rate while increasing to 83.7% at 75% load. NO{sub x} emissions ranged from a low of 0.17 Lbs/MBtu to a high of 0.24 Lbs/MBtu. After the baseline natural gas testing was completed, work continued on hardware optimization and testing with the goal of increasing carbon conversion efficiency on 100% coal firing from {approx}95% to 98%. Several coal handling and feeding problems were encountered during this quarter and no long term testing was conducted. While resolving these problems several shorter term (less than 6 hour) tests were conducted. These included, 100% coal firing tests, 100% natural gas firing tests, testing of air sparges on coal to simulate more primary air and a series of cofiring tests. For 100% coal firing, the carbon conversion efficiency (CCE) obtained this quarter did not exceed the 95-96% barrier previously reached. NO{sub x} emissions on coal only ranged from {approx} 0.42 to {approx} 0.78 Lbs/MBtu. The burner has not been optimized for low NO{sub x} yet, however, due to the short furnace residence time, meeting the goals of 98% CCE and <0.6 Lbs/MBtu NO{sub x} simultaneously will be difficult. Testing on 100% natural gas in the boiler after coal firing indicated no changes in efficiency due to firing in a `dirty` boiler. The co-firing tests showed that increased levels of natural gas firing proportionately decreased NO{sub x}, SO{sub 2}, and CO.

  17. Oxidation of phenolics in supercritical water. Combined quarterly technical progress report, December 1, 1995--May 31, 1996

    SciTech Connect

    1996-11-01

    Over the past two quarters, our work has focused on three main areas. The first area of interest involved a reexamination of the rate laws that were formed in past quarters. A possible error was discovered for the analytical methods used in the o-cresol oxidation study and the data were corrected, yielding a new rate equation. The data for hydroxybenzaldehydes were studied again, this time as a system of parallel oxidation and thermolysis reactions. The second area in which progress was made was the study of the thermolysis of nitrophenols and dihydroxybenzenes in supercritical water. These investigations were needed to determine the effect that pyrolysis or hydrolysis had on our previous supercritical water oxidation experiments. Thirdly, we have continued to investigate the use of molecular orbital theory in the determination reactivity indices. A reactivity index, such as the enthalpy of formation, may be used in a structure-reactivity relationship to summarize the kinetics for the oxidation of phenolics in supercritical water. Progress in each of these areas is summarized.

  18. Recovery and utilization of gypsum and limestone from scrubber sludge. [Quarterly] technical report, March 1, 1993--May 31, 1993

    SciTech Connect

    Kawatra, S.K.; Eisele, T.C.

    1993-09-01

    Wet flue-gas desulfurization units in coal-fired power plants produce a large amount of sludge which must be disposed of, and which is currently landfilled in most cases. Increasing landfill costs are gradually forcing utilities to find other alternatives. In principle, this sludge can be used to make gypsum (CaSO{sub 4}-2H{sub 2}O) for products such as plaster-of-Paris and wallboard, but only if impurities such as unreacted limestone and soluble salts are removed, and the calcium sulfite (CaSO{sub 3}) is oxidized to calcium sulfate (CaSO{sub 4}). This project is investigating methods for removing the impurities from the sludge so that high-quality, salable gypsum products can be made. Work done in the previous quarter concentrated on developing a low-cost froth flotation process that could remove limestone, unburned carbon, and related contaminants from the sludge while recovering the bulk of the calcium sulfite and gypsum. In the current quarter, experiments to remove impurities from the sludge using a water-only cyclone were conducted. The cyclone has been found to be effective for removing the coarser limestone impurities, as well as removing contaminants such as fine gravel and grinding-ball chips. These results show that the cyclone will be very complementary with froth flotation, which mainly removes the very fine impurities.

  19. Preparation and characterization of composite membrane for high temperature gas separation. Quarterly technical report, September 1--November 30, 1994

    SciTech Connect

    Ilias, S.; King, F.G.

    1994-12-31

    To develop a new class of permselective inorganic membranes, the authors have identified electroless plating as a potential route to deposit a thin metal film on a porous substrate. Electroless plating is a controlled autocatalytic deposition of continuous film on the surface of a substrate by the interactions of a metal salt and a chemical reducing agent. This method can give thin films of metals, alloys and composites on both conducting and nonconducting surfaces. The objective of this project is to develop thin film palladium membranes for separation of hydrogen in high temperature applications. The authors plan to use electroless plating to deposit thin palladium films on microporous ceramic and silver substrates. They plan to characterize the membrane in terms of permeability and selectivity for gas separation. To accomplish the research objective, the project requires three tasks: Development of a process for composite membrane formation; Characterization of fabricated composite membrane; and Development of theoretical model for hydrogen gas separation. During this quarter, the authors attempted to measure the diffusivity and permeability of hydrogen gas through the palladium composite membrane. While running the diffusion measurements at elevated temperature and pressure, leakage of hydrogen was observed. This is a serious problem and it needs to be resolved. Currently, they are working on this problem. During this quarter, they also designed a diffusion cell to test thin-film palladium membrane in tubular structure. The diffusion cell is being fabricated and assembled by a local machine shop.

  20. Applied Meteorology Unit (AMU) Quarterly Report Fourth Quarter FY-14

    NASA Technical Reports Server (NTRS)

    Bauman, William H.; Crawford, Winifred C.; Watson, Leela R.; Shafer, Jaclyn

    2014-01-01

    Ms. Crawford completed the final report for the dual-Doppler wind field task. Dr. Bauman completed transitioning the 915-MHz and 50-MHz Doppler Radar Wind Profiler (DRWP) splicing algorithm developed at Marshall Space Flight Center (MSFC) into the AMU Upper Winds Tool. Dr. Watson completed work to assimilate data into model configurations for Wallops Flight Facility (WFF) and Kennedy Space Center/Cape Canaveral Air Force Station (KSC/CCAFS). Ms. Shafer began evaluating the a local high-resolution model she had set up previously for its ability to forecast weather elements that affect launches at KSC/CCAFS. Dr. Watson began a task to optimize the data-assimilated model she just developed to run in real time.

  1. Applied Meteorology Unit (AMU) Quarterly Report Fourth Quarter FY-13

    NASA Technical Reports Server (NTRS)

    Bauman, William; Crawford, Winifred; Watson, Leela; Shafer, Jaclyn; Huddleston, Lisa

    2013-01-01

    Ms. Shafer completed the task to determine relationships between pressure gradients and peak winds at Vandenberg Air Force Base (VAFB), and began developing a climatology for the VAFB wind towers; Dr. Huddleston completed the task to develop a tool to help forecast the time of the first lightning strike of the day in the Kennedy Space Center (KSC)/Cape Canaveral Air Force Station (CCAFS) area; Dr. Bauman completed work on a severe weather forecast tool focused on the Eastern Range (ER), and also developed upper-winds analysis tools for VAFB and Wallops Fl ight Facility (WFF); Ms. Crawford processed and displayed radar data in the software she will use to create a dual-Doppler analysis over the east-central Florida and KSC/CCAFS areas; Mr. Decker completed developing a wind pairs database for the Launch Services Program to use when evaluating upper-level winds for launch vehicles; Dr. Watson continued work to assimilate observational data into the high-resolution model configurations she created for WFF and the ER.

  2. Cross-flow, filter-sorbet catalyst for particulate, SO{sub 2} and NO{sub x} control. Fourth quarterly technical progress report

    SciTech Connect

    Not Available

    1990-11-01

    This report describes a new concept for integrated pollutant control: A cross-flow filter comprised of layered, gas permeable membranes that act as a particulate filter, an SO{sub 2} sorbent, and a NO{sub x} reduction catalyst.

  3. The development and testing of a fieldworthy system of improved fluid pumping device and liquid sensor for oil wells. Fourth quarter technical progress report, 1991

    SciTech Connect

    Buckman, W.G.

    1991-12-31

    A major expenditure to maintain oil and gas leases is the support of pumpers, those individuals who maintain the pumping systems on wells to achieve optimum production. Many leases are marginal and are in remote areas and this requires considerable driving time for the pumper. The Air Pulse Oil Pump System is designed to be an economical system for the shallow stripper wells. To improve on the economics of this system, we have designed a Remote Oil Field Monitor and Controller to enable us to acquire data from the lease to our central office at anytime and to control the pumping activities from the central office by using a personal computer. The advent and economics of low-power microcontrollers have made it feasible to use this type of system for numerous remote control systems. We can also adapt this economical system to monitor and control the production of gas wells and/or pump jacks.

  4. Pyrite surface characterization and control for advanced fine coal desulfurization technologies. Fourth quarterly technical progress report, June 1, 1991--August 31, 1991

    SciTech Connect

    Wang, Xiang-Huai

    1991-12-31

    The objective of this project is to conduct extensive studies on the surfaces reactivity of pyrite by using electrochemical, surface analysis, potentiometric and calorimetric titration, and surface hydrophobicity characterization techniques and to correlate the alteration of the coal-pyrite surface with the efficiency of the pyrite rejection in coal flotation. The product as well as their structure, the mechanism and the kinetics of the oxidation of coal-pyrite surfaces and their interaction with various chemical reagents will be systematically studied and compared with that of mineral-pyrite and synthetic pyrite to determine the correlation between the surface reactivity of pyrite and the bulk chemical properties of pyrite and impurities. The surface chemical studies and the studies of floatability of coal-pyrite and the effect of various parameters such as grinding media and environment, aging under different atmospheres, etc., are directed at identifying the cause and possible solutions of the pyrite rejection problems in coal cleaning.

  5. The effect of turbulence on the stability of liquid jets and the resulting droplet size distributions. Fourth quarterly technical report, October 1, 1993--December 31, 1993

    SciTech Connect

    Mansour, A.; Chigier, N.

    1993-12-31

    In this progress report the authors report on progress in making experimental measurements to describe the rheological properties of non-Newtonian fluids. Non-Newtonian liquids exhibit a non linear relationship between the shear stress and the shear rate. A typical time-dependent rheological phenomenon is thixotropy. Thixotropic fluids show a limited decrease in the shear viscosity of the fluid with time under a suddenly applied constant stress. Thixotropic fluids also show a hysteresis loop and a decaying stress on the shear stress-shear rate plot. Here the authors are using a power law model to describe the behavior of such non-Newtonian liquids.

  6. Anaerobic fluid-bed treatment of coal conversion wastewater: Fourth quarterly technical progress report for the period May 15 to August 15, 1987

    SciTech Connect

    Suidan, M.T.; Pfeffer, J.T.; Nakhala, G.F.; Traegner, U.K.

    1987-01-01

    Anaerobic fluidized-bed GAC reactors have been proven successful for the treatment of biologically inhibiting wastewaters such as coal conversion wastewaters. However, in treating such wastewaters which contain compounds that not only resist biodegradation but also inhibit the degradation of other compounds, adsorption on granular activated carbon (GAC) is a viable strategy for the removal of these inhibitory compounds. Since the adsorptive capacity of the reactor media is limited, partial replacement of the carbon bed is then necessary to maintain the concentration of inhibitory compounds below threshold levels. The cost of the GAC replacement thus represents a major operating cost of the system. The hydraulic detention time and the associated carbon inventory represent the single most important capital cost parameter. The objectives of this research are to determine, using experimental and modeling strategies, the effects of hydraulic detention time and the schedule of GAC replacement on the performance of fluidized bed GAC anaerobic reactors during the treatment of coal conversion wastewater. 7 figs., 2 tabs.

  7. Large scale solubilization of coal and bioconversion to utilizable energy. Technical progress report, July 1, 1994--September 30, 1994, fourth quarterly

    SciTech Connect

    Mishra, N.C.

    1994-11-01

    In order to develop a system for a large scale coal solubilization and its bioconversion to utilizable fuel, we plan to clone the genes encoding Neurospora protein that facilitate depolymerization of coal. We also plan to use desulfurizing bacteria to remove the sulfur in situ and use other microorganisms to convert biosolubilized coal into utilizable energy following an approach utilizing several microorganisms (Faison, 1991). In addition the product of coal solubilized by fungus will be characterized to determine their chemical nature and the mechanism of reaction catalyzed by fungal product during in vivo and in vitro solubilization by the fungus or purified fungal protein.

  8. Increased oil production and reserves from improved completion techniques in the Bluebell Field, Uinta Basin, Utah. Fourth quarterly technical progress report, July 1, 1994--september 30, 1994

    SciTech Connect

    Morgan, C.D.

    1994-12-31

    Bluebell field ill tile Uinta Basin, Utah, is a rich petroleum reserve. The field has produced over 125 million barrels of oil from the lacustrine rocks of the Green River Formation. Standard completion techniques, which consist of perforating up to thousands of feet of section at one time, have resulted in opening thief, water-producing and non-productive zones. Low recoverabilitv is largely due to the lack of understanding of the relationship between heterolithic facies, reservoir fracture systems and clay migration. These areas were investigated by analyzing over 1,500 feet of core from the Bluebell area. Approximately 60% of the core consists of carbonates and 40% consists of clastics (predominantly sandstones). The carbonate rocks in general have good porosity and randomly oriented, interconnected macrofractures, whereas the macrofractures in the sandstones are more vertical and isolated. The sandstones however, do have the best reservoir capacity due to inherent interparticle porosity. Some shales display overpressured hydro-microfractures. Preliminary analysis of clay types indicates swelling illite-smectite mixed layer clays as well as kaolinite in both the clastic and carbonate rocks. These swelling, clay types combine with the high pour point waxy oils to reduce production efficiency and total recovery.

  9. Development of automated welding process for field fabrication of thick walled pressure vessels. Fourth quarter technical progress report for period ending September 28, 1980

    SciTech Connect

    Not Available

    1980-01-01

    Progress is reported in research aimed at optimizing an automated welding process for the field fabrication of thick-walled pressure vessels and for evaluating the welded joints. Information is included on the welding equipment, mechanical control of the process, joint design, filler wire optimization, in-process nondestructive testing of welds, and repair techniques. (LCL)

  10. Advanced sulfur control concepts in hot-gas desulfurization technology. Quarterly technical progress report, July--September 1995

    SciTech Connect

    Harrison, D.P.

    1995-10-01

    Both the Antek total sulfur analyzer and the modifications to the Shimadzu GC-14A gas chromatograph to be used for analysis for SO{sub 2} and H{sub 2}S were delivered during the quarter. Problems were faced during the installation and calibration phases of both instruments. By the end of the quarter we believe that the GC problems have been solved, but problems remain with the Antek analyzer. It appears that too much sulfur (as SO{sub 2}) reaches the UV detector and causes it to become saturated. This shows up as a maximum in the instrument calibration curve. At 200 psia, the capillary flow restrictor allows a total flow rate of about 180 sccm, and the maximum occurs at about 1 % H{sub 2}S in the calibration gas. Reducing the pressure so that the total flow is reduced to about 25 sccm shifts the calibration curve maximum to about 5.7% H{sub 2}S. It appears that we must reduce the total flow rate to the detector or provide additional dilution. This may be accomplished by increasing the resistance of the capillary restrictor, by diverting a portion of the flow leaving the pyrotube to vent, or adding an inert such as N{sub 2} to the gases exiting the pyrotube. We are in contact with Antek representatives about the problem. Both the atmospheric pressure and high pressure electrobalances were used during the quarter to study the regeneration of FeS in atmospheres of O{sub 2}/N{sub 2} or H{sub 2}O/N{sub 2}. In the atmospheric pressure unit the effects of temperature (600 - 800{degrees}C), flow rate (130 - 500 sccm), and reactive gas mol fraction (0.005 to 0.03 O{sub 2} and 0.1 to 0.5 H{sub 2}O) are being studied. Regeneration tests completed to date in the high pressure unit have utilized only O{sub 2}/N. and the parameters studied include temperature (600 - 800{degrees}C), flow rate (500 - 1000 sccm), pressure (1 - 15 atm) ad O{sub 2} mol fraction (0.005 - 0.03).

  11. Removal of CO{sub 2} from flue gases by algae. [Quarterly] technical report, March 1, 1993--May 31, 1993

    SciTech Connect

    Akin, C.; Pradhan, S.

    1993-09-01

    The objective of this research program is to determine the feasibility of the alga Botryococcus braunii as a biocatalyst for the photosynthetic conversion of flue gas CO{sub 2} to hydrocarbons. The research program involves the determination of the biocatalytic characteristics of free and immobilized cultures of Botryococcus braunii in bench-scale studies, and the feasibility study and economic analysis of the Botryococcus braunii culture systems for the conversion of flue gas CO{sub 2} to hydrocarbons. The objective of the third quarter of this research program was to determine the growth and hydrogen formation characteristics of free and immobilized cells of Botryococcus braunii in bench-scale photobioreactors. Raceway and inclined surface type bioreactors were used for free cell and immobilized cell studies respectively. The free cell studies with air and CO{sub 2} enriched air [10% (v/v) CO{sub 2} in air] in media with and without NaHCO{sub 3} were conducted.

  12. Vapor pressures and heats of vaporization of primary coal tars. Quarterly technical progress report, July 1 - September 31, 1996

    SciTech Connect

    Suuberg, E.M.; Oja, V.; Lilly, W.D.

    1996-12-31

    The vapor pressure correlations that exist at present for coal tars are very crude and they are not considered reliable to even an order of magnitude. This project seeks to address this important gap in the near term by direct measurement of vapor pressures of coal tar fractions, by application of well-established techniques and modifications thereof. The principal objectives of the program are to: (1) obtain data on the vapor pressures and heats of vaporization of tars from a range of ranks of coal; (2) develop correlations based on a minimum set of conveniently measurable characteristics of the tars; and (3) develop equipment that would allow performing such measurements in a reliable, straightforward fashion. During this quarter we have extended the work on measurements of vapor pressures of coal tars, using the continuous Knudsen effusion technique. These results need further analysis and therefore in this report we describe only the general idea behind the technique, and also show some typical results.

  13. Photovoltaic mechanisms in polycrystalline thin film silicon solar cells. Quarterly technical progress report No. 1, July 30-October 31, 1980

    SciTech Connect

    Sopori, B.

    1980-07-30

    Major accomplishments during the first quarter of the contract period are reported. Small area diode fabrication and analysis has been continued. This technique has further been applied to many RTR ribbons. An optical technique for determination of crystallite orientations has been placed in operation. This technique has many distinct advantages. These are: (1) rapid; (2) can be set-up very inexpensively; (3) well suited for polycrystalline substrates of small grain size; and (4) can easily characterize twins. Accuracies obtained with this technique are about the same as that of the Laue technique. A technique to qualitatively evaluate grain boundary activity in unprocessed substrates has been used and valuable results obtained. Further analysis is being done to use this technique for quantitative evaluation. A major study of G.B. orientation effects is underway. Initial results on RTR ribbons have shown a good correlation of G.B. barrier height with misorientation (tilt boundaries).

  14. An advanced control system for fine coal flotation. Fifth quarterly technical progress report, October 1, 1996--December 31, 1996

    SciTech Connect

    Adel, G.T.; Luttrell, G.H.

    1997-03-04

    A model-based flotation control scheme is being implemented to achieve optimal performance in the handling and treatment of fine coal. The control scheme monitors flotation performance through on- line analysis of ash content. Then, based on the economic and metallurgical performance of the circuit, variables such as reagent dosage, pulp density and pulp level are adjusted using model-base control algorithms to compensate for feed variations and other process disturbances. Recent developments in sensor technology are being applied for on-line determination of slurry ash content. During the fifth quarter of this project, all work was on hold pending the final novation of the contract to Virginia Polytechnic Institute and State University.

  15. Integration of advanced geoscience and engineering techniques to quantify interwell heterogeneity. Quarterly technical report, January 1, 1996--March 31, 1996

    SciTech Connect

    Buckley, J.S.; Ouenes, A.

    1996-06-01

    The objective of this project is to integrate advanced geoscience and reservoir engineering concepts with the goal of quantifying the dynamics of fluid-rock and fluid-fluid interactions as they relate to reservoir architecture and lithologic characterization. This interdisciplinary effort will integrate geological and geophysical data with engineering and petrophysical results through reservoir simulation. The essence of the work completed in the first quarter of 1996 is summarized in the following three statements: automatic log digitizing software is superior to hand digitizing; laboratory wettability tests suggest that the reservoir is mixed-wet and results of the non-reactive tracer test were used to revise the mechanics of the wettability test design to include tracer injection below a packer.

  16. Plant response to FBC waste-coal slurry solid mixtures. [Quarterly] technical report, September 1--November 30, 1993

    SciTech Connect

    Darmody, R.G.; Dunker, R.E.; Dreher, G.B.; Roy, W.R.; Steel, J.D.

    1994-03-01

    The goal of this project is to test the feasibility of stabilizing coal slurry solids (CSS) wastes by directly seeding plants into the waste. This is not done conventionally because the waste can generate toxic amounts of sulfuric acid. Our approach is to neutralize the potential acidity by mixing fluidized bed combustion (FBC) waste into the slurry. If successful, this approach would both help dispose of FBC wastes while providing a more economical slurry stabilization technique. The project involves growing forage plants in CSS-FBC mixtures in the greenhouse. This is the first quarter of the project. We have designed the experiment, secured greenhouse space, purchased the seeds, collected and dried the FBC and CSS samples. The samples represent a typical range of properties. We retrieved two FBC and two CSS samples. One CSS sample appears to have a higher pyrite content than the other.

  17. Coal combustion: Effect of process conditions on char reactivity. Ninth quarterly technical report, September 1, 1992--December 1, 1993

    SciTech Connect

    Zygourakis, K.

    1993-12-31

    Our efforts during the past quarter focused on the development of an image processing technique for characterizing the macropore structure of chars produced from Illinois No. 6 coal. Pyrolysis experiments were carried out in a microscope-stage reactor in inert and reacting atmospheres and at various pyrolysis heating rates. Particles from several pyrolysis runs were embedded in an epoxy resin block and polished sections . were prepared. Digital images of char particle cross-sections were acquired and analyzed to measure the structural properties of the chars. The macropore analysis procedure is presented here in detail. Future reports will present the data showing the effects of pyrolysis conditions on the macropore structure of Illinois No. 6 chars.

  18. Superior catalysts for selective catalytic reduction of nitric oxide. Quarterly technical progress report, October 1, 1994--December 31, 1994

    SciTech Connect

    Li, W.B.; Yang, R.T.

    1994-12-31

    During the past quarter, progress was made in three tasks. The poisoning effects of alkali metals (as Na{sub 2}O, K{sub 2}0 and Cs{sub 2}O) on iron oxide pillared clay (Fe-Bentonite) catalyst for selective catalytic reduction (SCR) of NO with NH{sub 3} were investigated. The effects of sulfur dioxide and water vapor on the performance of the high activity catalyst, that is, Ce-doped Fe-Bentonite pillared clay (Ce-Fe-Bentonite) were examined. In addition, an iron ion-exchanged titania pillared clay (Ti-PILC) was prepared and its catalytic activity for the SCR of NO with NH{sub 3} was studied, which showed a high activity and a high S0{sub 2} and H{sub 2}0 resistance at high temperatures (i.e., above 400{degree}C).

  19. Field study of disposed wastes from advanced coal processes. Quarterly technical progress report, October--December 1992

    SciTech Connect

    Not Available

    1992-12-31

    The specific objectives for the reporting period of October, 1992 to December, 1992 were as follows: (1) Finish analyzing leachates from the third annual core samples from the Ohio site, collected in August 1992; (2) Collect and analyze the sixth quarterly water samples from the first Illinois test case in August, 1992. Make field measurements and collect data from the data logger; (3) Begin construction of the second Illinois test case; (4) Continue production of a video presentation on the project; (5) Load all remaining EERC data on the Colorado and Ohio sites into the project database; (6) Finalize plans with METC for continued monitoring at the Colorado and Ohio sites beyond the initial three year period, and (7) Submit and the Final Case Report on the Colorado site to the DOE and EPRI.

  20. Bioconversion of coal-derived synthesis gas to liquid fuels. Quarterly technical progress report, April 1, 1993--June 30, 1993

    SciTech Connect

    Jain, M.K.; Worden, R.M.; Grethlein, H.

    1993-07-16

    The overall objective of the project is to develop two stage fermentation process for conversion of coal-derived synthesis gas to a mixture of alcohols. This is achieved in two steps. In the first step, B .methylotrophicum converts carbon monoxide (CO) to butyric and acetic acids. Subsequent fermentation of the acids by Clostridium acetobutylicum leads to the production of butanol and ethanol. The tasks for this quarter were: Development/isolation of superior strains for fermentation of syn gas; optimization of process conditions for fermentation of syn gas; evaluation of bioreactor configuration for improved mass transfer of syn gas; and optimization of process conditions for reducing carbon and electron loss by H{sub 2}-CO{sub 2} fermentation.